Information Notice 1990-04, Cracking of the Upper Shell-to-Transition Cone Girth Welds in Steam Generators,

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Cracking of the Upper Shell-to-Transition Cone Girth Welds in Steam Generators,
ML031470418
Person / Time
Issue date: 01/26/1990
From: Rossi C
Office of Nuclear Reactor Regulation
To:
References
IN-90-004
Download: ML031470418 (3)


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Home > Electronic Reading Room > Document Collections > General Communications > Information Notices > 1990 > IN 9 UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555 January 26, 1990

Information Notice No. 90-04: CRACKING OF THE UPPER SHELL-TO-TRANSITION

CONE GIRTH WELDS IN STEAM GENERATORS

Addressees

All holders of operating licenses or construction permits for Westinghouse- designed and Combustion Engineering-designed nuclear power reactors.

Purpose

This information notice is intended to alert addressees to continuing

problems related to cracking of the upper shell-to-transition cone girth

welds in the steam generators (SGs) originally described in Information

Notices 82-37, Cracking in the Upper Shell to Transition Cone Girth Weld of

a Steam Generator at an Operating Pressurized Water Reactor, and 85-65,

'Crack Growth in Steam Generator Girth Welds., It is expected that

recipients will review the in-formation for applicability to their facilities

and consider actions, as appropriate, to avoid similar problems. However, suggestions contained in this information notice do not constitute NRC

requirements; therefore, no specific action or written response is required.

Description of Circumstances

During the 1989 refueling outage at Zion Unit 1, a scheduled inservice

inspection (ISI) was performed on the SG D- upper shell-to-transition cone

girth weld. The ultrasonic testing (UT) detected flaw indications that

exceeded the allowable standard of Section XI of the ASME Code, Article

IWC-3000 (Table IWB-3511-1). Based upon these results, the extent of UT was

initially expanded to include the girth weld in SG C' and further expanded

to include SGs "A' and B.' All surface indications were removed by

grinding, contoured to established profiles, and accepted by magnetic

particle testing (MT) methods. The deepest repair excavation was

approximately 0.50 inch in depth by 6.45 inches in length. Boat samples

were removed for metallography. The results of the metallography are still

under investigation by the licensee.

During the 1987 refueling outage at Indian Point Unit 2, flaw indications

were detected during a scheduled ISI of the same upper shell-to-transition

cone girth weld. Visual examination of the inside circumference revealed

essentially horizontal intermittent linear indications around the entire

weld length of SG #22. Subsequently, UT and MT were extended to essentially

100 percent of this girth weld in all SGs. A total of 291 surface

indications were reported in the four SGs, with the most severe cracking

occurring in SG #22. The linear indications were predominantly in the

vicinity of the weld heat-affected zones.

9001220165 IN 90-04 January 26, 1990 http://www.nrc.gov/reading-rm/doc-collections/gen-comm/info-notices/1 990/in90004.html 03/13/2003

tnformation Notice No. 90-04: A repair program was completed that included progressive grinding to

established profiles and nondestructive examination. All observed cracks

detected by MT were removed; however, the corrosion pits outside the repair

areas were not removed before the plant started up after the refueling

outage. The repair resulted in a series of grooves that extended around

essentially the entire circumference of SG #22 with the maximum depth of

excavation approximately 1.07 inch, whereas the wall thickness is typically

3.5 inches. Eight boat samples were removed for metallurgical analysis. On

the basis of this analysis, the licensee concluded that the cracking was

most likely caused by corrosion fatigue.

During the 1989 refueling outage at Indian Point Unit 2, an MT was initially

conducted on one third of the inside circumference of the SG #22 girth weld.

Linear indications were detected during this examination. Subsequently, 100

percent of the inside circumferences of the girth welds in all SGs were

inspected. Linear indications were also detected in these additional

examinations. All observed cracks were ground out again; the maximum depth

of grinding to remove the new flaw indications was 0.95 inch. A weld repair

of localized areas and a post-weld heat treatment PWHT) were accomplished

on SG #22. An MT performed after the PWHT detected additional surface

indications, which were later removed. The licensee concluded that the

probable cause of the cracking was corrosion fatigue resulting from the

combined action of thermal cycling, oxygen in the auxiliary feedwater, and

copper alloys from the feedwater system. The licensee removed the downcomer

flow resistance plate to minimize the thermal cycling mechanism. The

licensee also committed to shutdown for an MT inspection during a mid-cycle

outage to evaluate the effectiveness of corrective actions.

Discussion:

Cracks and linear indications on the inner circumference have been detected

in the upper shell-to-transition cone girth weld in 18 SGs in the United

States. In addition, linear indications have been found at one foreign

plant. The degree of cracking ranges from severe in the case of Indian

Point Unit 2 to isolated and dispersed at Zion Unit 1. At the domestic

plants flaws have been observed only in Westinghouse Model 44 and Model 51 vertical recirculating U-tube SGs with the feedwater ring design.

The manufacturer, the affected licensees, and the NRC staff are still

evaluating the available information to establish the root cause of the

cracking problem and its generic implication. A common factor was the

general corrosion pitting on the inside surface of the SGs. Metallography

found that the surface pits served as crack initiation sites. The current

information indicates that the degradation probably results from

corrosion-assisted thermal fatigue. Thermal cycling results from relatively

cold water that impinges upon the weld region during reactor trips from full

power and certain transient operations. At Indian Point Unit 2, copper

alloys from the feedwater system and the downcomer flow resistance plate

probably were contributing factors.

IN 90-04 January 26, 1990 The flaw indications can be detected with enhanced UT procedures that are

performed by experienced nondestructive examination personnel. The upper

shell-to-transition cone weld is located at a gross structural

discontinuity. The weld is relatively wide and typically has an irregular

crown. These inherent geometric features commonly result in innocuous

reflectors. In addition, subsurface flaw indications are known to exist

near the inside diameter surface of SGs at several plant sites. In order to

distinguish innocuous reflectors from cracks, the following processes may be

necessary: scanning at a high gain, the use of multiple transducers with

optimum angles, careful plotting of reflector locations, and examination by

experienced personnel.

The rules of Section XI of the ASME Code require a volumetric examination of

one upper shell-to-transition cone weld during each 10-year inspection

interval. The required examinations may be limited to one SG or may be

distributed among all the SGs. However, if general corrosion pitting of the

http://www.nrc.gov/reading-rmldoc-collections/gen-commlinfo-notices/1990/in90004.html 03/13/2003

Information Notice No. 90-04: SG shell is known to exist, the requirements of Section XI of the ASME Code

may not be sufficient to differentiate isolated cracks from inherent

geometric conditions. In lieu of volumetric examinations, visual and MT

examinations of the interior circumference of the girth weld were used by

the licensee of Indian Point Unit 2 to detect the surface-connected flaws.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate NRR project

manager.

Charles E. Rossi, Director

Division of Operational Events Assessment

Office of Nuclear Reactor Regulation

Technical Contacts: Martin R. Hum, NRR

(301) 492-0932 Robert A. Hermann, NRR

(301) 492-0911 Attachment: List of Recently Issued NRC Information Notices

.ENDEND

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