IR 05000483/1986002

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SALP Rept 50-483/86-02 for June 1985 - May 1986.Category 1 Ratings Assigned in Areas of Surveillance Testing,Fire Protection,Security,Outages & Training
ML20209J131
Person / Time
Site: Callaway Ameren icon.png
Issue date: 05/31/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20209J101 List:
References
50-483-86-02, 50-483-86-2, NUDOCS 8609160164
Download: ML20209J131 (33)


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SALP 6 SALP BOARD REPORT U. S. NUCLEAR REGULATORY COMMISSION

REGION III

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE 50-483/86002

Inspection Report

Union Electric Company

Name of Licensee

Callaway Plant

Name of Facility

June 1, 1985 - May 31, 1986

Assessment Period

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I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance based upon this

information.

SALP is supplemental to normal regulatory processes used to

ensure compliance to NRC rules and regulations.

SALP is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

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resources and to provide meaningful guidance to the licensee's management

to promote quality and safety of plant construction and operation.

An NRC SALP Board, composed of staff members listed below, met on

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August 8, 1986, to review the collection of performance observations

and data to assess the licensee's performance in accordance with the

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guidance in NRC Manual Chapter 0516, " Systematic Assessment of Licensee

Performance." A summary of the guidance and evaluation criteria is

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provided in Section II. of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at Callaway for the period June 1, 1985 through May 31, 1986.

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SALP Board for Callaway:

NAME

TITLE

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J. A. Hind

Director, Division of Reactor Safety and Safeguards

C. E. Norelius

Director, Division of Reactor Projects

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R. M. Lerch

Project Inspector, Reactor Projects 1A

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B. H. Little

Senior Resident Inspector

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W. L. Forney

Chief, Reactor Projects Section 1A

N. J. Chrissotimos Deputy Director, Division of Reactor Safety

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L. R. Greger

Chief, Facilities Radiation Protection Section

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M. C. Schumacher

Chief, Independent Measurements and Environmental

Protection Section

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P. W. O'Connor

Project Manager, Division of Licensing, Office

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of Nuclear Reactor Regulation

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J. R. Kniceley

Safeguards Inspector

E. R. Schweibinz

Chief, Technical Support Section

M. P. Phillips

Chief, Operational Programs Section

C. F. Gill

Reactor Inspector, Facilities Radiation Protection

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Section

J. P. Patterson

Emergency Preparedness Analyst

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II.

CRITERIA

Licensee performance is assessed in selected functional areas, depending

upon whether the facility is in a construction, preoperational, or operating

phase.

Functional areas normally represent areas significant to nuclear

safety and the environment.

Some functional areas may not be assessed

because of little or no licensee activities, or lack of meaningful

observations.

Special areas may be added to highlight significant

observations.

One or more of the following evaluation criteria were used to assess each

functional area.

1.

Management involvement and control in assuring quality

2.

Approach to the resolution of technical issues from a safety standpoint

3.

Responsiveness to NRC initiatives

4.

Enforcement history

5.

Operational and Construction events (including response to, analyses

of, and corrective actions for)

6.

Staffing (including management)

However, the SALP Board is not limited to these criteria and others may

have been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories.

The definitions of

these performance categories are:

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Category 1.

Reduced NRC attention may be appropriate.

Licensee

management attention and involvement are aggressive and

oriented toward nuclear safety; licensee resources are

ample and effectively used so that a high level of

performance with respect to operational safety and

construction quality is being achieved.

Category 2.

NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident

and are concerned with nuclear safety; licensee resources

are adequate and are reasonably effective so that

satisfactory performance with respect to operational safety

and construction quality is being achieved.

Category 3.

Both NRC and licensee attention should bc increased.

Licensee management attention or involvement is acceptable

and considers nuclear safety, but weaknesses are evident;

licensee resources appear to be strained or not effectively

used so that minimally satisfactory performance with

respect to operational safety and construction quality is

being achieved.

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III. SUMMARY OF RESULTS

The regulatory performance of the Callaway Plant is very good.

Although

the ratings in Surveillance and Security improved and the rating for

Licensing Activities declined, performance improved to some extent in

most areas.

Rating Last

Rating This

Functional Area

Period

Period

A.

Plant Operations

2

B.

Radiological Controls

2

C.

Maintenance

2

D.

Surveillance

1

E.

Fire Protection

1

F.

Emergency Preparedness

2

G.

Security

1

H.

Outages

1 (Fuel Loading)

1 (Refueling)

I,

Quality Programs and

Administrative Controls

Affecting Quality

2

J.

Licensing Activities

2

K.

Training and Qualification

Effectiveness

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IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

Portions of seven inspections were performed in this area

by the resident inspectors and region based inspectors which

included direct observation of operating activities.

Extensive

inspections were performed during the seven week Cycle 1

refueling outage which included assist inspections by NRC

resident inspectors from the Byron and Wolf Creek Plants.

The

operations portions of these inspections focused on overall

control room discipline and specifically on shift crew

performance during normal and off-normal conditions and shift

relief and turnover activities.

The inspections included a

review of logs and records, interviews with plant personnel

and followup of significant operating events to ascertain

facility operations in conformance with the Technical

Specifications and administrative procedures.

One violation

was identified as follows:

Severity Level IV - Failure to operate within the Axial Flux

Difference target band as required by Technical Specifications.

(Inspection Report No. 50-483/85016).

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The violation involved operating the reactor beyond the

allowable Axial Flux Difference (AFD) limits allowed by

Technical Specification (TS).

Technical Specifications

require that with the indicated AFD outside of the above

required target band and with thermal power greater than

or equal to 90% of rated thermal power, within 15 minutes,

either restore the indicated AFD to within the required

target band limits, or reduce thermal power to less than

90% of rated thermal power.

Although there are four channels of power range flux difference

indication, an NIS Recorder, and a CRT display provided on the

control room " front panel" to indicate AFD conditions, the

allowable AFD band was exceeded by approximately 1% for

135 minutes before an operator noted and corrected the condition.

This event indicates a lack of operator attention which resulted

in exceeding the allowable Axial Flux Difference.

NRC

inspection determined that the event posed no technical safety

problem; however, the event was considered significant as it

resulted from a lack of operator attention to plant parameters

and conditions.

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Escalated enforcemert is being considered involving two examples

of the licensee's failure to maintain plant / instrumentation

systems operable as required by Technical Specifications and

one example of failure to meet NRC reporting requirements.

(1) The Intermediate Head Safety Injection System was

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inoperable for approximately six hours.

The event resulted

from a combination of procedural and personnel performance

errors.

(2) The Auxiliary Feedwater Pumps (AFPs) Engineered

Safety Features Actuation System (ESFAS) blocking switches

were in " block" position for approximately 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />, which

defeated the automatic start feature of the AFPs upon loss

of the main feedwater pumps.

(3) The licensee failed to

notify NRC within four hours of a condition which rendered

the Intermediate Head Safety Injection System inoperable.

NRC inspections determined that the two events posed no

significant threat to public/ plant safety; however, escalated

enforcement action is being considered to emphasize the

importance of conducting activities in full compliance with

the facility license, and to underscore the importance of

procedural discipline and operator attentiveness.

The licensee's initial evaluation of reportability by the

operating crew classified the event as a 30 day Licensee Event

Report (LER).

Licensee's followup review process failed to

identify the appropriate reportability of the event.

Although the above violations directly involved plant operations,

other violations which indicate direct or indirect involvement

by plant operations are discussed in Sections IV.B., Radiological

Controls, and IV.I., Quality Programs.

In addition, NRC

inspections determined that plant operations personnel were

involved in procedural and Technical Specification violations

for which Notices-of Violations were not cited because the

violations were of lesser safety significance, and the licensee

identified, thoroughly evaluated, factually reported, and

provided prompt corrective measures.

Overall, the number of LERs issued during the assessment period

indicate a downward trend.

However, the number attributed to

personnel error is greater than expected.

For example, during

the last three months of this assessment period, 12 of the

20 LER events which occurred are attributed to personnel

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performance problems.

Of those attributed to " personnel",

seven events relate to containment / control room ventilation

isolations involving inoperable radiation monitors.

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Licensee events receive a high level of management attention.

In addition to disciplinary action / supervisory consultations,

management holds bi-monthly " fire-side" chats with the

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operating crews. These meetings focus on increasing operator

awareness of LERs and reactor trips and have stressed personal

accountability.

LER/ reactor trip performance trends are posted

on plant status boards.

To reduce performance errors the

licensee has added sign-off action steps to I&C and maintenance

procedures, placed warning signs at radiation monitors and

electrical controls, and conducted special training sessions

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on radiation monitors. Written LERs, received during this

assessment period, are summarized further in the " Supporting

Data and Summaries,"Section V.G.I. of this report.

There were no events during this assessment period which were

classified as an " Unusual Event." There were four unusual

events during the previous assessment period.

A total of 83 events were reported to the NRC Operations Center

via telephone. Of these, 42 were non-security events reported

under the requirements of 10 CFR 50.72 and 41 were LER notifications

made per 10 CFR 50.73. Review of the LERs indicates that about

half of them involved minor technical specification violations

and were not significant enough to be reported to the Operations

Center.

There were fourteen (14) reactor trips which occurred during the

period from June 1, 1985 through May 31, 1986. Twelve were

from power levels greater than 15% power and 2 were from less

than 15% power or during shutdown conditions. Of these, nine

were related to equipment deficiencies and five resulted from

personnel errors. The NRC and the Licensee consider this

number of reactor trips to be excessive. The Licensee has

established a set of goals for seven reactor trips between the

period January 1 through December 31, 1986.

If the plant has

seven trips their performance goal will be met; if there are

five trips their performance will be considered excellent by

the licensee, and if there are three or fewer trips their

performance will be considered outstanding by the licensee.

Of the 42 non-security events reported per 50.72, 22 events

involved actuations of engineered safety features. A large

number of these events involved spurious Containment Purge

Isolation (CPI), Control Room Ventilation Isolation (CRVI),

and Fuel Building Ventilation Isolation (FBVI). Two events

were caused by personnel error. A number of events were due

to spurious signals generated during gas sampling evolutions.

In 1985 (note the SALP period is 6/1/85 through 5/31/86), the

reactor critical hours of operation were 8,161, the forced

outage rate was 6.4% or 536.8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, and the unit had 20 scrams

which is equivalent to 2.45 scrams per 1000 critical hours of

operation, which is much higher than the industry average of

1.47 scrams /1000 critical hours in 1985. However, the plant

availability factor for 1985 was 90% which is much higher than

the 61% national average availability factor for 1985. This

high availability factor in spite of the high number of scrams

is because the plant was not refueled during 1985, the outages

that occurred were of fairly short duration, and plant staff

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performance was good.

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NRC inspection of licensee events has found that " event

reduction" has been given a high level of management attention

and support.

This includes the implementation of a Plant Trip /

Incident Reduction Program which is discussed in more detail

in Section I., Quality Programs. The licensee has provided

prompt and thorough evaluation of causal factors and prompt

implementation of corrective measures.

Corrective measures

specified by the licensee usually include performance goals

such as the attainment of main control panel " black boards"

for example. Operational improvements attributable to

management atteni. ion include reductions in the number of

reactor trips and reportable events, and reduction in the

backlog of work items including the reduction of alarming

control room annunciators. Management attention to operating

events is evident in the quality of LER reports.

An evaluation

of LER reports by the Office for Analysis and Evaluation of

Operational Data found the content and quality of a sample of

LERs to be higher than the industry average.

See the summary

in Section V.G.1 of this report.

Inspection of licensee performance relating to control room

behavior was performed routinely by the resident inspectors and

Region III inspectors.

The extended coverage during the

refueling outage provided observation of the licensee's shift

crew performance during days, off-shift, and weekends, including

shift turnovers.

The control room operators and supervisors were attentive to

plant conditions'and displayed a professional attitude toward

the control and operations of the plant.

Plant alarms, and

both planned and unplanned events were promptly responded to,

appropriately communicated, and logged.

The operating logs,

status boards, and equipment out of service logs were being

maintained and reflected current plant and system conditions.

Administrative and operating procedures were adhered to.

Crew shift relief and turnovers were performed in a thorough

manner and included discussions of past, current, and planned

activities, the review of logs, and panel walkdowns.

Control

room access is limited and enforced. The inspectors noted

that licensee management and quality assurance personnel

provided frequent in plant observations of the shift crews'

performance.

During site visits on June 24, 1985, August 28, 1985 and

April 29, 1986, headquarters staff toured several plant areas

including the reactor building, turbine building, auxiliary

building, radwaste building, and the control room.

The

staff found that the plant was in good order with respect to

cleanliness and housekeeping.

Activities in the control room

were observed to be conducted in a professional manner with

assigned personnel appearing to be alert and attentive to duty.

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2.

Conclusion

The licensee is rated Category 2 in this area.

This is the

same rating as the previous assessment period.

3.

Board Recommendations

None.

B.

Radiological Controls

1.

Analysis

Four inspections were conducted during this assessment period

by region based inspectors.

These inspections included

radiation protection, radioactive waste management, TMI

Action Plan Items, chemistry / radiochemistry, confirmatory

measurements, and environmental monitoring. The resident

inspectors also reviewed this area during routine inspections.

Four violations were identified as follows:

a.

Severity Level IV - Failure to follow procedures for

sampling the unit vent radioactive gaseous effluent,

resulting in failure to identify inoperability of the

unit vent gaseous monitor.

(Inspection Report

No. 50-483/85017)

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b.

Severity Level IV - Failure to implement specified

actions (alternate sampling and report to NRC) required

due to inoperability of unit vent gaseous monitor.

(Inspection Report No. 50-483/85017)

c.

Severity Level IV - Failure to leak test two sealed

sources at required frequency.

(Inspection Report

No. 50-483/85017)

d.

Severity Level IV - Failure to implement specified actions

(auxiliary sampling or termination of releases) required

due to isolation of the radwaste building vent iodine and

particulate sampler.

(Inspection Report No. 50-483/86014)

Violations a. and b. resulted when, due to personnel error, a

sample line was not reconnected following maintenance on the

unit vent sample pump.

Due in part to another personnel error,

the disconnected sample line was not detected for thirteen days,

during which time required gaseous monitoring or alternate

sampling was not performed. Violations c. and d., although

identified by the licensee, were cited because licensee

corrective actions were inadequate.

The violations appear to

reflect minor programmatic failures of licensee personnel and

administrative systems to effectively recognize and implement

oporational requirements.

At the end of this SALP assessment

period, the plant had been operational for approximately

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17 months. The number of personnel and administrative system

failures in this functional area during this initial operational

period has been typical for new plants.

Staffing continues to be a licensee strength.

The number

of technician and supervisory personnel is ample, with

essentially all positions filled and has been very stable

with losses generally limited to internal promotions.

This

stability should enhance the staff's performance as experience

is gained. Additionally, an adequate number of well qualified

contract radiation protection technicians were utilized during

the extended maintenance outage.

Positive management involvement in this functional area

continued to be demonstrated.

There is consistent evidence

that supervision is directly involved in day-to-day activities.

A radiation protection representative attends all outage

planning meetings.

Plant work group managers are utilized to

support correction of radiation protection infractions by their

workers.

The radiation work violation reporting system for

documenting and correcting problems appears to be working well.

Quality assurance auditors are well qualified and have

performed timely and thorough audits of this functional area.

Responsiveness to the audit specific findings has been good.

However, an improved system is needed to obtain timely

responses to programmatic weaknesses identified by audits

and evaluations.

Management shortcomings in this functional

area were evidenced in continued delays in resolution of

ventilation system filter housing drain problems and certain

TMI Action Item analysis issues. The filter housing drain

issue was resolved near the end of this assessment period;

however, the TMI Action Item issue remains open from the

previous SALP assessment period.

An additional recurrent

problem area requiring licensee attention was radioactive

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effluent leakage from piping systems, which was straining

the decontamination work force; many of these leaks were

repaired during the refueling outage near the end of this

assessment period.

Responsiveness to NRC issues was acceptable.

The licensee has

resolved or initiated actions for several NRC concerns, including

fuel manipulator crane area monitors, ventilation system deluge

and drain provisions, painting of concrete surfaces in potentially

contaminated areas, control room ventilation charcoal desorption

potential, fluid calibrations of liquid and gaseous effluent

monitors, radon levels, and sample line iodine plateout.

Additional licensee actions are needed concerning TMI Action

Items and contaminated leakage from piping systems.

Generally, a conservative approach to resolution of technical

issues continues to be exhibited.

Personal radiation exposures

for the first eighteen months of operation were about

240 person-rems which is consistent with early PWR operations.

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The licensee's ALARA program is well organized and amply staffed.

Plant and work group goals have been established in numerous

areas and have been updated, as necessary, to reflect existing

conditions.

Additional work requests for repair of contaminated

system leakage necessitated upward revision of the ALARA goal

for the total contaminated plant area.

The ALARA program places

emphasis on contaminated area controls.

The decontamination

work force appears well organized under the Radwaste

Superintendent but suffers somewhat from understaffing and

inexperience.

Several noteworthy ALARA improvements were

implemented during this assessment period including expanded

use of temporary, job-specific air filtration equipment and

use of temporary shielding during reactor head gasket

replacement.

Liquid, airborne, and solid radioactive releases during this

assessment period were consistent with early PWR operation.

No transportation problems were identified.

The licensee has performed and implemented a satisfactory

water chemistry control program for the primary and secondary

system chemistry which addresses the major elements of the PWR

Owners Guidelines designed to minimize localized corrosion in

the steam generators and turbines.

The Radiological Controls Technicians demonstrated satisfactory

capability for collecting samples and analyzing them for key

chemical parameters.

The licensee also has adequate capability

to monitor conductivity, pH, sodium and dissolved oxygen

through on-line monitors on different plant systems to ensure

the appropriate water quality is maintained.

The licensee

maintains awareness of the water quality through trend plotting

of analytical data over time and will impose action levels if

necessary when monitored chemical parameters are confirmed to

be outside normal operating values.

The licensee has demonstrated a satisfactory QA/QC program

through control charts on chemical parameters and on counting

data using performance check sources.

Licensee participation

in an interlaboratory cross check program involving radiological

and nonradiological sampics has been satisfactory.

The

licensee's results in the confirmatory measurements program

are excellent with all agreements for the comparisons made.

Conduct of the Radiological Environmental Monitoring program

during this period is satisfactory with no significant

discrepancies noted during the review of the Annual Operating

Report.

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2.

Conclusion

The licensee is rated Category 2 in this area.

Although

the rating for the last SALP was Category 2 also, overall

performance this assessment period was better than the

majority of SALP Category 2 plants.

3.

Board Recommendations

None.

C.

Maintenance

1.

Analysis

Inspections in this functional area were routinely included

in seven inspections performed by resident inspectors, region

based inspectors, and a resident inspector from another site.

The inspections included a review and observation of the

maintenance programs, staffing, staff training, and records.

In addition to selected preventive and corrective maintenance

and system modifications surveyed to verify that these

activities were completed in accordance with Technical

Specifications and the licensee's quality assurance program

requirements, followup inspections were performed on

significant equipment problems.

Discussions were held with

craftsmen, maintenance supervision, and plant management.

The following items were also considered during these

inspections:

the limiting conditions for operation were

met while components or systems were removed from service;

approvals were obtained prior to initiating the work;

activities were accomplished using approved procedures and were

inspected as applicable; functional testing and/or calibrating

were performed prior to returning the components or systems to

service; parts and materials that were properly certified;

radiological controls were implemented as necessary; and, fire

prevention controls were in place.

No violations or deviations were identified.

One LER was issued relating to instrumentation & control

maintenance during the assessment period.

This event involved

troubleshooting that resulted in a signal being injected

into the incorrect Reactor Protection System trains which

caused an inadvertent reactor trip.

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An inspection assessed the licensee's programs for equipment

classification, vendor interface, and post maintenance testing

and found them to be adequate.

An inspection was conducted to perform an in-depth evaluation

of maintenance related events.

The maintenance program was

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determined to be basically sound with the licensee addressing

some minor weaknesses. The licensee management has shown an

aggressive posture in dealing with the maintenance program and

the implementation problems including a thorough evaluation

of root causes.

Maintenance scheduling and performance consistently shows

improvement and evidence of good planning and assignment of

priorities.

This was evident during the outage when a large

effort was incorporated in the maintenance program to reduce

the number of backlogged items as well as during routine

operations.

The corrective actions performed appear to be

effective as indicated by the lack of repetitive work orders.

Management involvement is also evident in the concern placed

on the reduction of work order items backlog.

The maintenance

records were found to be clear and retrievable.

The staffing appears to be sufficient for routine work demands.

During the evaluation period, contractors were onsite working

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to reduce the number of backlogged work orders.

During this

period, the number of work orders were reduced from over

5000 to approximately 2000.

The events and occurrences in this functional area have

received a high level of management involvement.

" Crew

chats" have been used and procedures have been revised (with

additional action step signoffs) to reduce performance errors.

Specialized training in specific areas has also been

incorporated to reduce the number of events.

The maintenance

area is also included in the " Plant Trip / Incident Reduction

Program."

2.

Conclusion

The licensee is rated Category 2 in this area.

The rating for

the last SALP was Category 2.

3.

Board Recommendations

None.

D.

Surveillance

1.

Analysis

Inspections were routinely performed in this functional area

during five inspections by the resident inspectors and two

inspections by regional based inspectors.

No violations were

identified in this area.

The resident inspectors reviewed or observed selected portions

of Technical Specifications required surveillance testing

during power operations and mode changes during startup from

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the refueling outage.

Items which were considered during the

inspections included whether adequate procedures were used to

perform the testing, test instrumentation was calibrated, test

results conformed with Technical Specifications and procedural

requirements, and the test was performed within the required

time limits.

The inspectors determined that the test'results

were reviewed by someone other than the personnel involved with

the performance of the test, and that any deficiencies

identified during the testing were reviewed and resolved by

appropriate management personnel.

Two inspections were performed by regional based inspectors to

review the calibration and surveillance testing programs.

The

programs were found to be sound and well implemented.

A

regional based inspector performed a review and evaluation of

the in-service inspection of the piping system components.

The

activities were controlled through the use of well stated

procedures. The review showed that the activities had received

good planning and priorities had been assigned. Observation

of the in-service inspection activities indicated that

personnel have a good understanding of work practices and that

procedures were followed.

Records were found to be essentially complete, well maintained,

and available.

The records also indicated that equipment and

material certifications were current and complete and that the

personnel performing nondestructive examinations were trained

and certified.

Discussions held with personnel performing the

examinations indicated they were knowledgeable of their job.

Three reportable licensee events, which included two reactor

trips were classified in this area.

This number of events

is considered acceptable in relationship to the number of

surveillances that were performed during this period.

Technical Specification requirements have been converted

to verification test requirements and the schedule

placed on the computer.

Only two tests were tardy this

period.

These occurred during unusual conditions that had

not been factored in from the Technical Specifications and,

therefore, are not a programmatic problem.

These deficiencies,

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and others that have been identified, have been promptly

documented, evaluated, and corrected.

The program was

considered to be fully implemented on June 1, 1985, and it

appears that the planning and scheduling portion of the

program has been very effective.

The computerizing of the surveillance schedule and designating

a group to followup performance of the surveillance tests has

essentially eliminated missed or late performance of the tests.

Review of individual procedures has shown these to be quality

procedures, which include the appropriate acceptance criteria.

The test results were reviewed and evaluated in a timely manner.

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.

.

The planning and scheduling group also schedules maintenance

on equipment at the same time as the surveillance is to be

performed. This feature helps keep safety-related equipment

out-of-service to a minimum.

In response to comments provided in the previous SALP report,

improvements were implemented in the field performance

activities.

The NRC inspections determined that the licensee

has implemented a comprehensive surveillance program in which

identified deficiencies are evaluated and corrected promptly.

The licensee has been very receptive to comments and suggestions

by the NRC and demonstrated a conservative and conscientious

attitude toward maintaining a quality surveillance testing

program.

The licensee's staffing levels have been adequate to perform

and followup in the area of surveillance tests.

The management

involvement in this area has been consistently evident in

planning and the assignment of priorities.

The LERs classified

in the area of the surveillance program are included in the

" event reduction" study which has received a high level of

management attention.

2.

Conclusion

The licensee is rated Category 1 in this area.

The rating for

.

the last SALP was Category 2.

3.

Board Recommendations

None.

E.

Fire Protection

1.

Analysis

The inspections in this functional area were conducted during

the six routine inspections performed by the resident inspectors.

The inspections did not include the verification of conformance

to Appendix R requirements.

The inspections did include

observation of the on shift fire brigade training drills,

housekeeping, storage, and control of flammable liquids and

combustibles, status and condition of manual fire fighting

equipment, and the condition of the emergency breathing

equipment and " turn out" gear.

No violations or deviations were issued.

Nine LERs were issued in this functional area.

Seven involved

improperly stationed fire watch patrols.

One LER reported

missing conduit smoke and fire seals due to a construction

installation inadequacy.

The remaining LER identified a number

of fire dampers that may not have had the necessary clearances

.

.

had a fire occurred.

Licensee reviews of the reportable events

were timely, thorough, and technically sound, and the corrective

actions appear to have been timely and effective.

The improperly stationed fire watch patrols were of minor

significance to safety-related equipment.

The patrols were

tardy due to misunderstanding or misinterpreting the

requirements or the patrols were simply late at a checkpoint.

The five dampers that were reported were of minor safety

significance due to associated fire sensing and/or suppression

systems.

The licensee implemented appropriate temporary

controls until the fire dampers are corrected.

The fire protection / prevention equipment and procedures have

been found to be maintained at an excellent level.

Two drills

and portions of other exercises were observed.

The fire

brigade performance during the drills was noted to be

business-like and the functional performances were very

professional. The inspections showed that housekeeping in

the plant had been maintained at a high level.

During the

outage, the licensee utilized additional personnel to maintain

the cleanness of the plant. The inspectors' walkdowns

performed during the outage indicated that housekeeping was

maintained at a very good level throughout the outage.

2.

Conclusion

The licensee is rated Category 1 in this area.

This is based

on operational inspections and not an inspection of 10 CFR

Appendix R implementation. The rating for the last SALP was

Category 1.

3. ' Board Recommendations

None.

F.

Emergency Preparedness

1.

Analysis

Two inspections were performed during the assessment period.

One of these was an evaluation of the annual emergency

preparedness (EP) exercise conducted on June 5, 1985.

The

other was a routine inspection which included a review of

emergency detection and classification, protective action

decisionmaking, notifications and communication, changes to

the emergency program, shift staffing and augmentation,

training, and licensee audits.

No violations were identified.

Two weaknesses were identified during the exercise.

One was

lack of a health physics (HP) control point for radiological

.

.

.

self-monitoring at the Technical Support Center (TSC),

Maintenance Operational Support Center (OSC), and the HP

Access Control Point.

The other weakness was inadequate

communications in the OSC, e.g., telephone reception

interference, poor audibility of Gaitronics, and ineffective

use of radios for contacting in plant teams.

Correction of

these two weak areas was successfully demonstrated and

reviewed during the July 30, 1986 annual emergency exercise.

The routine inspection included a thorough review of the

" Classification of Emergencies" procedure including the

Emergency Action Level (EAL) classification criteria.

The

inspectors recommended that certain EALs be modified, revised

or restated to more accurately identify emergency plant

operating conditions.

Proper management attitude and

involvement was demonstrated by the licensee's commitment to

review the EALs and consider changes to the EAL format.

A new computerized dose assessment program has been initiated

by the licensee.

This program, Radiological Release

Information System (RRIS), while functional, appeared to have

been designed to run with current meteorological data only,

and was unable to use forecast meteorological data.

As

evaluated by the inspection team, the program needed several

software changes to make it function as a predictive device for

calculating projected releases of radioactivity.

Management's

response to the EAL and dose assessment issues has indicated an

understanding of the issues, and a willingness to address NRC

Concerns.

To correct a shift augmentation drill which failed to obtain

minimum required responses, an additional drill was successfully

performed in April 1986, and monitored by the NRC Senior

Resident Inspector.

Additional drills will be monitored for

assurance that reliability has been developed in the shift

augmentation area.

Independent audits of the program have been timely and thorough,

with the findings needing corrective actions being identified

by Quality Assurance (QA) auditors.

Follow-up corrective

actions were taken and upper management was made aware of

the findings.

Responsiveness to NRC initiatives and other

issues has been viable, generally sound, and thorough in most

instances.

Enforcement history has been very good,

Corrective

actions have been timely and effective in most cases.

The

training program has steadily improved.

EP training has now

been incorporated into simulator training for control room

personnel with emergency response functions.

A Job Task

Analysis has been developed by the Training Department to

better define the objectives and responsibilities of each

emergency response position.

As a result, three lesson plans

have been established for each of the 55 emergency response

-

I.

  • positions.

The Emergency Preparedness Required Reading

i

Procedure has been revised to make the supervisor accountable

for assuring that the procedure is adhered to by those with

emergency preparedness responsibilities.

The training program

is well defined and implemented with dedicated resources and

a means for feedback experience.

.

Two activations of the Callaway Radiological Emergency Response

Plan (RERP) were identified during this SALP-6 period. Both

events were categorized correctly and proper notifications were

made in a timely manner to State, local agencies, and the NRC.

With the addition of the ring down phone in the control room

and emphasis on correctly completing the notification form,

l

this aspect of communications has improved from the previous

j

SALP period.

2.

Conclusion

<

The licensee is rated Category 2 in this area.

Licensee

I

performance was determined to be improving near the close

of the assessment period.

The rating for the last SALP

was Category 2.

3.

Board Recommendations

None.

G.

Security

1.

Analysis

One routine inspection and one reactive inspection were

conducted by regional based inspectors during this assessment

i

period.

The resident inspectors also made periodic inspections

!

of security activities assessing routine program implementation

and providing initial response to security events. One

j

violation was identified as follows:

Severity Level IV - The licensee failed to have a fully

adequate barrier from the owner controlled area to the

I

protected area.

(Inspection Report No. 50-483/86005)

During the assessment period, the region received allegations

of security improprieties and communicated telephone threats

,

to the plant.

The allegations were not substantiated. The

l

licensee's investigative actions and increased security

-

!

measures pertaining to the security related telephone threats

!

were comprehensive, timely, and adequately reported, although

initial evaluation of the significance and reaction to the very

l

first event required regional management discussions with the

l

security organization.

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_ _ _ _ _ _ _ _ _ _ _

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_ _ _ _ _ _ _ _ _ _ _ _

.

'

The licensee's senior management demonstrated an awareness of

security issues and has been effective and responsive to

identifying, resolving, and recommending solutions for security

issues.

Concerns and observations receive the same exceptionally high

level of management attention normally associated with violations.

The security management is responsive to all NRC initiatives and

suggestions that can strengthen their program, rather than

concentrating on just minimum compliance required by the security

plan.

Full management support has been demonstrated by site

management, and the security organization operates in a highly

supportive environment. The weaknesses identified during the

previous SALP period were adequately corrected.

The lack of

significant violations is attributable to the security force's

high caliber of performance. Weaknesses identified by the

licensee were not repetitive and not indicative of a programmatic

breakdown.

Corrective actions were prompt and effective.

Management has established policies and procedures that are

well written and effectively enforced.

The licensee's staffing levels are adequate to fulfill security

plan commitments.

Positions within the security organization

are identified and authority and responsibilities are well

defined.

Training policies and procedures have ensured that

all security personnel are trained and qualified to perform

assigned security related tasks or duties.

There were no technical security issues with respect to plant

safety that required resolution during this assessment period.

Additionally, no regulitory issues which required a licensee

response were identified during the assessment period.

Security events were properly and accurately reported to the

NRC under 10 CFR 73.71(c).

There have been eight such events

during the assessment period.

These events pertained mainly

to computer hardware problems which were adequately resolved.

The licensee properly analyzed the events and initiated

appropriate corrective action.

The licensee's Quality Assurance Department, which conducts

independent security program audits, has been effective in

identifying security program weaknesses and has been

instrumental in strengthening the security program.

In summary, the licensee's security staff has been highly

effective in the operation and implementation of the security

program.

The security staffing is adequate and departmental

support for the security program has been effective.

Supervision of the security force is aggressive which results

in a stable, well trained security force.

.

.

'

.

2.

Conclusion

l'

Because of the excellent enforcement history and management

involvement in problem resolution, the licensee is rated

Category 1 in this area.

The rating for the last SALP was

Category 2.

,

,

3.

Board Recommendation

None.

/

H.

Outages

,

,

1.

Analysis

Three inspections were performed in this functional area by

regional based and resident inspectors. Only one major outage

occurred during this period, the first refueling and maintenance

outage.

The inspections included the receiving inspection of

new fuel assemblies, defueling and refueling, various maintenance

and surveillance activities, radiological protection, and planning.

No violations were identified.

Extensive management involvement was evident several months

prior to and during the initial refueling outage.

The personal

involvement of management was observed at advanced planning and

y

daily planning meetings and frequent in plant tours.

The

outage was well planned and administered.

The licensee has

a permanent outage group that schedules the outages.

The

outage group held twice daily meetings with all concerned

i

groups for problems and information dissemination.

The detail

i

of jobs to be performed during the next three days was issued

at this time.

Outage coordinators were onsite around the clock

to make any schedule changes that were found to be necessary.

The licensee provided additional staffing and supervision,

special equipment checkout, and training.

Advanced planning

also provided detailed / integrated subnets for major work and

activities and assignment of task performance responsibilities.

Personal accountability was evident during the outage meeting

and was effective in resolving technical problems.

The need

for increased plant security was recognized in the planning

and was subsequently provided.

The refueling operations were performed by licensee personnel

with contracted fuel loading supervision.

Refueling

operations were performed smoothly with only minor equipment

problems occurring.

The radiological controls were enhanced with the advanced

planning and the hiring of the contract rad technicians that

>

provided sufficient personnel to cover the jobs in progress.

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_ _ _

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_ _ _ _ _

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,

The advanced planning / scheduling set the outage at 42 days and

I,A.;

.

the actual outage was completed in 49 days. The licensee

-

b

stated that this was the shortest initial refueling outage for

,

a Westinghouse four-loop plant to date.

The outage schedule

i

'

(

was developed with no contingency time built in.

The seven day-

j

outage extension was the accumulation of delays in the critical

'

t

.

path items due to equipment failures, jobs taking longer to

complete than historical information indicated, and other

'

miscellaneous reasons.

The major projects completed during

-

the outage were inspection of main turbine and generators,

,

i

local leak rate tests of containment valves, steam generators

tube inspection, secondary side inspection of steam generators,

and maintenance on reactor coolant pumps and feedwater pumps.

No major spills or contamination occurred during the outage

,0

and housekeeping was maintained at a high level of cleanliness.

, 1:

The commitments for the Safety Parameter Display System (SPDS)

'

to be operable were completed during the outage and the Reactor

'

'. >

Vessel Level Indicating System was made functional. The

/l

modifications to reduce the number of alarms lit continued

and reduced the number to less than ten.

(This program remains

,

',. -

ahead of schedule.) There were 103 modifications performed

during the outage with the majority being considered in the

operational upgrade category.

NRC inspections during the Cycle 1 refueling outage determined

that the licensee had provided adequate staffing, supervision,

,

and training for the outage activities.

Procedures were

detailed and adhered to by the performing groups.

Exceptional

performance was noted by the operating crews' conduct and control

of the outage activities, health physics, controls and practices,

and overall maintenance.

Subsequent startup testing was also

conducted with no significant problems.

Plant-wide maintenance

and housekeeping control / practices and conditions were

exceptionally well maintained.

2.

Conclusion

The licensee is rated Category 1 in this functional area.

This is the first SALP rating of this area.

3.

Board Recommendations

None.

I.

Quality Programs and Administrative Controls Affecting Quality

1.

Analysis

The licensee's Quality Assurance (QA) Program, including

quality verification and oversight activities, was routinely

assessed in six inspections by the resident inspectors during

t

.

.

observations of plant activities in the areas of testing,

operations, maintenance, and surveillance.

The licensee's

implementation of its Quality Assurance / Quality Control (QA/QC)

Administration and Audit Programs was also the subject of two

inspections by region based inspectors.

No violations or

deviations were identified.

Escalated enforcement is being considered for failure to

environmentally qualify electrical equipment. The violation

involved two examples of the use of non-environmentally

qualified (EQ) electrical connectors on the Reactor Vessel

Head Vent Valves, and the Containment Isolation Valve for

the Chemical Volume and Control System.

NRC inspection determined that the licensee's use of the

non-EQ connectors resulted from deficient oversight of a

modification and a design change.

Upon discovery, this matter

received a high level of management attention.

Licensee

corrective actions included a re-review of EQ documents and

a 100% in plant inspection of all valves and limit switches

requiring EQ (Conax) connectors.

No additional deficiencies

were identified.

In the areas of QA/QC administration, the licensee developed

new procedures to address the preparation and control of

quality assurance planning guides and the parts Q-list data

base.

Another procedure was revised to accommodate the SNUPPS

computer program requirements.

The licensee made good progress

in addressing these.

In the area of audit implementation, the licensee proceeded

with their audit programs in four separate areas:

Operations,

Operations Support, Technical Support, and Quality Systems.

These audits were conducted in accordance with their program

schedules, by certified auditors, using approved plans and

checklists, and with proper attention to corrective action

requirements.

The NRC expressed minor concerns regarding the

flexibility granted to the auditors to vary from the planned

checklists, the lack of auditor identity on all the

certification papers, and the similarity between the 1985

and 1986 overall audit schedules.

The licensee promptly

responded to these items and committed to a thorough review

of their practices.

There was adequate evidence of management

involvement in planning and assignment of priorities for the

control of these activities.

Management's high degree of attention, frequent site visits,

and personal involvement in quality programs has been

continually evident at Callaway.

Both corporate and site

management frequently met with the resident inspectors.

During

these meetings, the licensee has been open and forthright in

!

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discussing events, problems, corrective actions, and enhancement

programs.

Management's influence in this area is evident

throughout the licensee's staff.

The effectiveness of the licensee's quality programs during

this assessment period, has been demonstrated by the favorable

reduction in the number of reactor trips and reportable events,

and the reduction in the backlog of work items including

alarming control room annunciators. Other favorable indicators

include the licensee's achievement of a fully accredited

training program and operator's performance on licensing exams.

The operating crews demonstrated a high degree of professional

conduct during routine operation and the ability to effectively

control unplanned events.

Inspection results and the licensee's good performance during

the refueling outage demonstrated that administrative controls

were well applied to outage activities including training,

staffing, supervision, and planning.

A major strength relates to the licensee's selection and staffing

of operations and support organizations including key advisory

personnel.

Oversight functions have been adequately staffed

and effectively utilized in the evaluation process of

operational activities and plant events.

These activities

include:

Onsite Review Committee (ORC), Independent Safety

Engineering Group (ISEG), Senior Operations Advisory Panel

(SOAP), Operating Advisors (0A), Compliance, and Quality

l

Assurance (QA).

Observation of group performance and

individual discussions with group members show them to be

dedicated and capable people who are responsive to industry

and NRC activities.

!

During the previous assessment period (SALP 5) NRC expressed

concerns regarding the excessive number of reactor trips and

other reportable events.

The licensee has been responsive in

this matter.

Inspections have found that the licensee has

continually provided a high degree of attention and resources

to the area of unplanned events, not only in evaluating them

but also in instituting corrective and preventive measures to

preclude their recurrence.

In September 1985, the licensee

implemented a Plant Trip / Incident Reduction Program.

This

program included a seven member team to assess plant events,

determine root and contributing causes, and recommend corrective

measures.

An overall reduction in both the number of events

and reactor trips indicates that the licensee has been effective

in this effort, most notably during the last half of this

assessment period.

Notwithstanding the favorable trend, the

number of recent events attributed to personnel errors is

considered high resulting in LERs and in the Technical

Specification violations discussed in Section A., Plant

Operations.

I

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The licensee's Site QA Organization is professionally organized

and staffed.

The QA audit and surveillance programs are well

defined and effectively implemented.

QA engineers provided

extensive surveillance coverage (including off-shifts and

weekends) during the refueling outage, startup, and power

ascension periods.

NRC inspection has determined that the

site QA is functionally independent and assertive and has

been effective in the identification and resolution of quality

concerns. Management's support of QA activities has been

evident.

2.

Conclusion

The licensee is rated Category 2 in this area.

This area was

rated Category 2 in the previous assessment period.

3.

Board Recommendations

None.

J.

Licensing Activities

1.

Analysis

During the current rating period, the primary licensing

activity involved the resolution of license conditions which

remained from the full power license issuance and the completion

of licensing actions relating to first cycle operations and the

approval of Reload 2 for cycle 2 operation.

The licensee's management has participated in licensing

activities and has assured timely response to the staff's

requirements.

In particular, the UE management has been

actively involved in major licensing activities such as the

Cycle 2 reload that they considered to be a critical path item

for the UE operational schedule.

UE is generally aware of NRC requirements and usually provides

the staff with adequate technical information to resolve staff

concerns.

However, on two occasions during the first half of

this rating period licensing actions were delayed by deficient

"no significant hazards considerations" analyses provided by UE

in support of amendment requests.

The basis for this appraisal was the licensee's performance in

..

support of amendment requests and responses to generic letters

which have been reviewed and evaluated by the staff during the

rating period.

The subjects involved include the following:

!

{

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. _ -.

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T

.

Generic Reviews:

Plant Specific Reviews:

Reactor Trip System

Enrichment Increase in Spent

Reliability (B-80)

Fuel Pool (Amendment 12)

Detailed Control Room

Fire pump Diesel Inspection

Design (F-71)

(Amendment 11)

Post-Trip Review (B-85)

Surveillance Interval

Safety Parameter Display

Extension (Amendment 8)

System (F-09)

Deletion of Fuse Testing

(Amendment 9)

Low Temperature Overpressure

Protection

Organization Change

(Amendment 10)

Revised Value of Pa

(Amendment 13)

Quality Systems Department

Change (Amendment 14)

Reload for Cycle 2

(Amendment 15)

Fuel Drop Accident Inside

Containment

Low Temperature Over Pressure

Circuitry

Use of Code Case N416

Extension of Performance on

Type C tests

During the present rating period the licensee's management

demonstrated active participation in licensing activities

and kept abreast of current and anticipated licensing actions.

In addition, the management's involvement in licensing

activities assured timely response to the requirements of the

Commission's rules related to Environmental Qualification of

Electrical Equipment and license conditions related to Detailed

Control Room Design Review, Emergency Response Capabilities,

and Regulatory Guide 1.97.

The implementation schedules

have been met by the licensee and their submittals have

generally been of high quality and have not required

significant rework to satisfy staff requirements.

UE management was particularly effective in assuring that high

quality submittals were provided to the staff during the

preparation and review of the UE's reload submittal for Cycle 2

operation. The submittal was timely and more than usually

complete. UE requested a pre-review meeting with the staff in

order to facilitate their submittal and our review.

.

The licensee's management and its staff have demonstrated sound

technical understanding of issues involving licensing actions.

Their approach to resolution of technical issues has demonstrated

extensive technical expertise in all technical areas involving

.

_ _ _

_ _..

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f

.

.

licensing actions. The decisions related to licensing issues

have routinely exhibited conservatism in relation to significant

safety matters. The licensee's clear understanding of the staff's

concerns assured sound technical discussions regarding

resolution of safety issues.

UE is generally aware of NRC requirements and their licensing

submittals usually provide the staff with the information needed

to complete its review without extensive requests for additional

information.

On two occasions the staff was unable to prepare a "no significant

hazards consideration" (NSHC) finding related to a UE amendment

request because the NSHC analysis provided by UE was deficient.

In both cases the required notice to the public was delayed

while UE was requested to provide by A NSHC analysis that

satisfied the requirements of 10 CFR 50.91(a)(1).

The licensee has been generally responsive to NRC initiatives.

During the rating period, they have made efforts to meet the

established commitments as illustrated by their response to

TMI action items I.D.1.2, and to the rules related to

environmental qualification of safety-related electrical

equipment.

In several subject areas the licensee responded

in a timely and thorough manner.

In response to NRC requests

and suggestions related to the staff's review of generic issues

and license amendment requests, the requested information

was usually provided quickly and was adequate to allow

the staff to resolve the issue promptly.

All scrams were promptly corrected and reported to the NRC

Operations Center.

2.

Conclusion

,

l

The licensee is rated Category 2 in this functional area.

!

The licensee has been responsive and technically competent in

pursuing its licensing activity during this SALP rating period.

Concerns relative to the "no significant hazards consideration"

l

findings during the first half of this period appear to have

i

been resolved.

The rating for the last SALP was Category 1.

3.

Board Recommendations

!

[

None.

i

K.

Training and Qualification Effectiveness

1.

Analysis

Resident and regional inspectors have evaluated training and

qualification effectiveness during inspection of specific

program areas.

In addition, an inspection was conducted to

'

.

.

.

evaluate the effectiveness of the licensee's licensed and

'

non-licensed personnel training programs.

No violations

were identified.

During inspections of licensee activities personnel were

knowledgeable and effective in implementing their duties.

l

Training appeared to be well planned and adequately presented.

In cases where abnormal incidents had occurred at the plant,

the licensee prepared an Incident Report (IR).

The licensee's

review of the event in the IR not only evaluated whether

personnel error contributed to the event, but in the cases

where it did, the licensee also evaluated the cause of the

personnel error.

This evaluation included an assessment of

whether the training program had been effective or could have

contributed to the cause of the event.

In all cases, completed

irs were forwarded to the Training Department for independent

evaluation to determine if the formal training program could

be improved to prevent a recurrence of the incident.

In

addition, the Training Department was conducting evaluations of

licensee LERs, INP0 SOERs, and NRC inspection report findings

to determine if improvements could be made to the training

program.

The licensee had developed a program whereby personnel can

suggest modifications to the training program based on their

first hand field knowledge.

In addition, training department

instructors conducting licensed operator training were required

,

to stand one watch per month as part of their regular duties.

Overall, the licensee appeared to have a good method for

operational feedback into the training program.

For the maintenance groups, the training program appears to

have been well defined and implemented with dedicated resources

and a means provided for feedback of experiences.

Inadequate

training could only rarely be traced as part of the cause of

events occurring during this rating period.

The licensee's training program provided several means of

disseminating information related to incidents and recent

events; however, the training program was not as effective in

providing training on plant modifications prior to the

modification being declared operational.

In addition, the

licensee's recordkeeping of training related records was

fragmented, with required readings and OJT completions being

documented in one department, formal classroom training was

l

documented in the Training Department, and old test results

were microfiched and kept by the Document Control Department.

i

l

During the assessment period, examinations were administered to

six Senior Reactor Operator and one Reactor Operator applicants.

The overall pass rate was 86%.

This passing rate exceeds the

overall nc.tional average passing rate.

During the last

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assessment period, the pass rate was also above the national

average.

Based on these results, the operator license training

program at Callaway was very effective.

In addition to adequate technician and general employee

training programs, radiological controls special radiation

protection training programs were implemented for maintenance

workers, contract radiation protection technicians,

decontamination workers, and outage work groups.

A 36-month

apprentice training program was developed to allow plant

helpers to qualify as Assistant Radiation-Chemical

Technicians specializing in radiation protection, chemistry,

or radwaste. The licensee's radiological training and

qualification program is well defined and implemented and is

comprehensive in terms of the workers encompassed.

The licensee has completed INP0 accreditation of all training

programs subject to accreditation.

These programs are

non-licensed operator, control room operator, senior control

room operator, shift technical advisor, instrument and control

technician, mechanical maintenance personnel, electrical

maintenance personnel, radiological protection technician,

chemistry technician, and onsite technical staff and managers.

The licensee was the third utility in the nation to complete

INP0 accreditation of all subject areas.

In cases where the NRC recommended improvements to a training

course, the licensee was very responsive in modifying the

content of lesson plans to address NRC concerns.

2.

Conclusions

The licensee is rated Category 1 in this functional area.

This is based on the licensee's timely completion of INP0

accreditation in all training categories and the excellent

feedback program setup to improve the training program based

on operational events.

This functional area was not rated

separately in previous SALPs.

l

3.

Board Recommendations

l

l

None.

I

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.

V.

SUPPORTING DATA AND SUMMARIES

A.

Licensee Activities

During SALP 6, assessment period June 1, 1985 through May 31,

1986, the following significant licensee activities occurred.

The plant was in its first refueling starting on February 28, 1986.

The plant resumed operation on April 15, 1986.

The Linion Electric Company training program became the third utility

to become fully accredited by INPO.

On May 19, 1986 the plant was shutdown to repair a S/G feedwater

check valve and was restarted on May 25, 1986.

B.

Inspection Activities

The inspection program at Callaway consisted of routine resident

and region based inspections including inspections of the outage

activities of the first refueling.

Inspection Reports Nos. 85015-85019

Inspection Reports Nos. 85021-85024

Inspection Reports Nos. 86001-86010

Inspection Reports Nos. 86012-86014

Table 1

Enforcement Activity

Number of Violations in Each Severity Level

Functional Areas

I

II

III

IV

V

l

--

--

--

A.

Plant Operations

--

B.

Radiological Controls

--

--

--

--

C.

Maintenance

--

--

--

--

--

i

D.

Surveillance

--

--

--

--

--

E.

Fire Protection

--

--

--

--

--

F.

Emergency Preparedness

--

--

--

--

--

'

G.

Security

--

--

--

--

,

H.

Outages

--

--

--

--

--

l

-.

_

-____.

!

.

Functional Areas

I

II

III

IV

V

I.

Quality Programs and

Administrative Controls

--

--

--

--

--

J.

Licensee Activities

--

--

--

--

--

K.

Training and Qualification

Effectiveness

--

--

--

--

--

TOTALS

0

6

C.

Investigations & Allegations Review

There were four allegation files opened.

Subsequent inspections of

the allegations did not identify any violations or deviations.

1.

An anonymous allegation was received that several improper

security practices were being allowed.

Inspection did not

substantiate any of the allegations.

2.

A former contractor employee alleged that some magnetic

particle tests were improperly performed.

Inspection could

not substantiate the allegation.

3.

An anonymous allegation was received by the Office of

Inspection and Enforcement regarding drug use by specific

names of prior employees of a licensee contractor.

This

information was forwarded to the licensee to investigate.

Followup inspection determined that the licensee received

the information and reviewed it in the context of their

drug policies and construction programs, and concluded there

was no evidence to substantiate the allegations against

individuals or to question the integrity of safety-related

construction.

4.

An anonymous letter was received by the Office of Inspection

and Enforcement with concerns over new security restrictions.

The licensee was notified of a concern received from an employee,

and review by safeguards inspectors found that the security

actions referred to were appropriate.

D.

Escalated Enforcement

1.

Civil Penalties

..

,

No civil penalties were issued.

2.

Orders

No orders were issued.

i

, -.

-

-

_ - - - - - -,. _

_,. _ - - - - - _ - - -,

-. _.

-_

. -.

. --

.

.

E.

Management Conferences Held During the Appraisal Periods

August 28, 1985, Management meeting with representatives of the

Union Electric Company to present the Systematic Assessment of

Licensee Performance Report (SALP 5) for the Callaway Plant.

February 5,1986, Licensee presentation on trip reduction program

and Quality Systems Department.

April 9-10, 1986, Management plant tour and meeting with licensee

management regarding actions which were taken as a result of the

recent threat against the plant.

Region III management toured the

plant and met with licensee personnel before the conclusion of the

first refueling outage.

In addition, potential violations regarding

equipment not environmentally qualified were discussed.

June 3, 1986, Management meeting and enforcement conference to

discuss the inadvertent isolation of the intermediate head injection

system.

June 10, 1986, regional managemer.t toured the site. The

licensee presented their findings and actions regarding an error

which blocked auxiliary feedwater initiation signals on main

feedwater pump trip.

F.

Confirmation of Action Letters (CAls)

There were no Confirmatory Action Letters issued during this

assessment period.

G.

Review of Licensee Event Reports, and 10 CFR 21 Reports Submitted

by the Licensee

1.

Licensee Event Reports

During SALP six assessment period, June 1, 1985 thru May 31,

1986, there were 45 Licensee Event Reports submitted.

These

events constituted LERs 85-25 thru 85-54; 86-01 thru 86-15.

An evaluation of the content and quality of a representative

sample of the Licensee Event Reports (LERs) submitted by

Callaway 1 during the June 30, 1985 to May 31, 1986 Systematic

Assessment of Licensee Performance (SALP) period was performed

using a refinement of the basic methodology presented in

NUREG/CR-4178.

The results of this evaluation indicate that

Callaway 1 has an overall average LER score of 9.0 out of a

possible 10 points, compared to a current industry average

score of 7.8 for those units / stations that have been evaluated

.

to date using this methodology.

NRC rated Callaway LERs as

the best in the nation.

l

--

,.

--

,

_

, _ - -, - -, - -,. -,, - -

,.., - - -. -,,,. - -,,

.

f

.

A

A strong point for Callaway 1 LERs is that the root cause

information for most events is discussed very well as is the

mode, mechanism, and effect of failed components.

Callaway's LER scores are indicative of an apparent commitment

to provide LERs that meet the requirements of 10 CFR 50.73(b).

LERs BY CAUSE

Total June 1, 1985

Cause*

to May 31, 1986

Personnel Error

Equipment Failure

Design

Procedure

_2

TOTAL

  • Cause assigned by the licensee

The total of 45 LERs is an improvement over the 74 LERs issued

in the previous SALP period; however, the proportion of LERs

attributed to personnel errors went from 33.7% to 57.7%.

This

resulted mostly from a corresponding reduction in equipment

failure LERs from a proportion of 54% to 33%. Overall,

continued reduction in the number of LERs appears feasible

with most improvement to be made in reducing personnel errors.

2.

Part 21 Reports

There were no 10 CFR Part 21 reports submitted by the licensee

in this assessment period.

H.

Licensing Activities

1.

NRR/ Licensee Meetings

To Discuss Reload 2

12/05/85

To Discuss low-temperature over pressure

protection system

11/07/85

2.

NRR Site Visits / Meetings

Training to obtain unescorted access and

06/24/85 &

meeting with resident inspector

08/28/85

Site Tour with regional personnel to discuss SALP

report and meeting with resident inspector

04/29/86

3.

Commission Meetings

NONE

!

-

.

'

4.

Schedular Exemptions Granted

NONE

5.

Reliefs Granted

NONE

6.

Exemptions Granted

NONE

7.

License Amendments Issued

Amendment 8

Extension of initial 18 month

10/03/85

surveillance interval

Amendment 9

Deletion of resistance testing of

11/19/85

certain fuses

Amendment 10

Revision to unit organizational

11/19/85

chart

Amendment 11

Revision to fire pump diesel engine

01/22/86

surveillance requirement

Amendment 12

Spent fuel pool enrichment limit

01/24/86

. Amendment 13

Revised value of Pa

03/04/86

Amendment 14

Quality Systems Department

03/04/86

organization

Amendment 15

Reload 2

04/04/86

8.

Emergency Technical Specification Changes

NONE

9.

Orders Issued

NONE

10.

NRR/ Licensee Management Conferences

NONE

.

.

.

..

.-

--