IR 05000400/1999007

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Informs That NRC Region 2 Will Conduct Triennial Fire Protection Baseline Insp 50-400/99-07 at Harris Facility on 991101-05.Insp Objection Will Be to Evaluate Fire Protection Program Implementation
ML18017A916
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 10/07/1999
From: Landis K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Scarola J
CAROLINA POWER & LIGHT CO.
References
50-400-99-07, NUDOCS 9910210094
Download: ML18017A916 (39)


Text

October 6, 1999

SUBJECT:

NRC INTEGRATED INSPECTION REPORT 50-400/99-06

Dear Mr. Scarola:

On October 9, 1999, the NRC completed an inspection at your Shearon Harris facility. The enclosed report presents the results of that inspection.

The results of that inspection were discussed with you and other members of your staff on October 21, 1999.

The inspection was an examination of activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

Within these areas, the inspection consisted of a selective examination of procedures and representative records, observations of activities, and interviews with personnel.

Based on the results of this inspection, the NRC has determined that one violation of NRC requirements occurred.

This violation is being treated as a Non-Cited Violation (NCVj, consistent with Appendix F of the Enforcement Policy. This NCV is described in the subject inspection report.

Ifyou contest the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to the Regional Administrator, Region II; the NRC Resident Inspector at Shearon Harris Nuclear Power Plant; and the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001.

CP8L

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice,". a copy of this letter and its enclosure will be placed in the NRC Public Document Room (PDR).

Sincerely, (Original signed by B. Bonser)

Brian Bonser, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket No.:

50-400 License No.:

NPF-63

Enclosure:

Inspection Report

REGION II==

Docket No:

License No:

50-400

NPF-63

Report No:

50400/99-06

Licensee:

Carolina Power 8 Light (CP8L)

Facility:

Shearon Harris Nuclear Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill, NC 27562

Dates:

August 29 - October 9, 1999

Inspectors:

J. Brady, Senior Resident Inspector

R. Hagar, Resident Inspector

Approved by:

B. Bonser, Chief, Projects Branch 4

Division of Reactor Projects

Enclosure

SUMMARYOF FINDINGS

Shearon Harris Nuclear Power Plant, Unit 1

NRC Inspection Report 50-400/99-'06

The report covers a six-week period of resident inspection

Inspection findings were assessed

according to potential risk significance, and were assigned

colors of GREEN, WHITE, YELLOW, or RED. GREEN findings are indicative of issues that,

while not necessarily desirable, represent little risk to safety. WHITEfindings would indicate

issues with some increased risk to safety, and which may require additional NRC inspections.

YELLOWfindings would be indicative of more serious issues with higher potential risk to safe

performance and would require the NRC to take additional actions.

RED findings represent an

unacceptable

loss of margin to safety and would result in the NRC taking significant actions that

could include ordering the plant shut down. Those findings that cannot be evaluated for a direct

effect on safety with the Significance Determination Process,

such as those findings that affect

the NRC's ability to oversee licensees,

are not assigned

a color.

Cornerstone:

Barrier Integrity

~

GREEN. The licensee failed to take appropriate corrective action under 10 CFR 50.65

(a)(1) when a maintenance rule (a)(1) performance goal was exceeded for the Target

Rock Position Indication performance monitoring group in system 9001, containment

isolation valves. The established goal of no more than one failure in 18 months was

exceeded

on June 11, 1999, but was not recognized by the licensee, and appropriate

corrective action was not taken until another functional failure occurred on August 17,

1999. This issue was characterized

as a Non-Cited Violation and was determined to

have low risk significance because failure of the Target Rock position indicators did not

prevent operators from determining valve positions, and other more time-consuming

methods were available.

Second, the failure to recognize that a maintenance

rule goal

had been exceeded did not affect the ability of any valve to operate (Section 1R12).

Re ort Details

The unit was at essentially 100 percent power until September 9, when power was reduced to

86 percent due to problems with the steam generator preheater bypass valves.

Power was

returned to 100 percent on September

11 and remained at 100 percent for the remainder of the

pe nod.

REACTOR SAFETY

Cornerstones:

Initiating Events, Mitigating Systems, Barrier Integrity

1R01

Adverse Weather Pre arations

The inspectors reviewed the licensee's preparations for Hurricane Floyd on

September

15, 1999.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

The inspectors reviewed the following emergent items, as described in the referenced

Work Request/Job

Orders (WRJOs) and/or Action Requests

(ARs)':

Reference

WR/JO 99-AGUP1

WR/JO 99-AGNX1

AR 004097004097AR 007914

Preheater bypass valve actuator air leaks

Boron totalizer replacement

Letdown pressure control valve (PCV 145) problems

SSPS relay problem during MST l0417

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R04

E ui ment Ali nment

The'inspectors performed reviews of the motor-driven auxiliary feedwater system when

the turbine-driven pump was inoperable for preventive maintenance,

and the control

room ventilation system during preventive maintenance.

b.

Observations and Findin s

No findings'were identified and documented through this inspection.

1R05

Fire Protection

The inspectors reviewed the condition reports (CRs), work orders, and impairments

associated with the fire suppression system.

The inspectors reviewed the status of

surveillance activities to determine whether they were current to support the operability

of the fire protection system.

The inspectors observed a fire drill associated with a direct

current (DC) battery charger in the B switchgear room.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R09

Inservice Testin

IS

of Pum

s and Valves

I

The inspectors reviewed the performance of the following IST tests:

Number

Rev.

Title

OST 1051

"Reactor AuxiliaryBuilding Emergency Exhaust System IST

Quarterly" for damper 1AV-3

OST 1038

"Sampling, Chemical Addition, and Main Steam Drain ISI Valve

,Test"

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R11

Licensed 0 erator Re uglification

The inspectors reviewed, licensed operator requalification simulator examinations for

operations crew C.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R12

Maintenance Rule Im lementation

Ins ection Sco

e

The inspectors reviewed the licensee's implementation of the Maintenance Rule

(10 CFR 50.65) with respect to the equipment issues described

in the following CRs and

Engineering Service Request (ESR):

CR

99-02358

Target Rock containment isolation valve position indication

CR

99-01918

Containment isolation valve 1AF-157 stroke time problems

ESR

97-00547

Essential Services Chilled Water nonessential

isolation valve

b

Observations and Findin s

The inspectors found that significant CR 99-02358 described two failures of Target Rock

valve position indicators under system 9001, containment isolation valves (CIV). The

description stated that the goats set forth in CR 97-03489 for the Target Rock Position

Indication performance monitoring group (PMG) under system 9001 had been exceeded.

The goal was for no more than one functional failure due to reed switch failure during an

18-month period starting at the completion of refueling outage (RFO)8 on December 2,

1998.

Some 20 valves which were not CIVs were added to the PMG which included

CIVs because the a(1) corrective actions had included a modification to upgrade the

position indicators.

The inspectors reviewed the maintenance rule database

to confirm the status of the

Target Rock PMG in system 9001. The inspectors confirmed that the PMG was in a(1)

status, that CR-97-03489-1 established the goals for the a(1) to a(2) transition, and that

the goal was no more than one failure in the 18-month period between RFO8 and RFO9.

The inspectors reviewed the maintenance

rute event log and found that functional

failures under the Target Rock Position Indication PMG had occurred on January 18,

1999 (CR 99-00164); June 11, 1999 (CR 99-00699); and August 17, 1999 (CR 99-

02358).

Only the last one identified that the goal had been broken.

None of these

functional failures involved a failure of the valves to perform their containment isolation

function. The inspectors questioned why the occurrence on June 11 (CR 99-00699) had

not been considered as the functional failure that caused the goal to be exceeded.

The licensee reviewed the associated

information and initiated significant AR

00008315, Failure to Recognize Exceeding a Maintenance Rule a(1) Goal, as a result of

their review. The AR identified that procedures ADM-NGGC-0101, Maintenance Rule

Program, and CAP-NGGC-0001, Corrective Action Management, require that when an

a(1) goal is exceeded,

a "significant adverse" CR is to be initiated for the purpose of

evaluating the need for additional corrective action.

10 CFR 50.65 a(1), Maintenance Rule, requires that when the performance or condition

of a structure, system, or component does not meet established goals, appropriate

corrective action shall be undertaken.

As stated above, the licensee failed to recognize

that the established goal of no more than one failure in 18 months was exceeded

on

June 11, 1999, and therefore did not take appropriate corrective action based on that

until another functional failure occurred on August 17, 1999. This is considered

a

violation of 10 CFR 50.65 a(1) for not taking appropriate corrective action when a

Maintenance Rule goal was not met. This violation is being treated as a Non-Cited

Violation, consistent with Appendix F of the NRC Enforcement Policy. This violation is in

the licensee's corrective action program

as AR 00008315. The inspectors have

designated this violation NCV 50-400I99-06-01, Failure to Recognize That an a(1) Goal

Was Exceeded.

This issue had relatively low ("green") risk significance, for two reasons:

~, First, failure of the Target Rock position indicators did not prevent operators from

determining valve positions, because other, more time-consuming methods were

available.

~

Second, the failure to recognize that a maintenance

rule goal had been exceeded did

not affect the ability of any valve to operate.

1R13

Maintenance Work Prioritization 8 Control

The inspectors reviewed the licensee's assessments

of the risk impacts of removing

from service those components associated with the emergent work items listed in

Section 1R03.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R14

Nonroutine Plant Evolutions

The inspectors reviewed the operating crew's performance during the following non-

routine evolutions:

~

Unexpected shutting of all three steam generator preheater bypass valves on

September 9 and associated

power reduction to 86%.

~

The planned shutting of the preheater bypass valves at 100% power on

September

17.

Observations and Findin s

No findings were identified and documented through this inspection.

1R15 0 erabilit

Evaluations

The inspectors reviewed the operability evaluations described in the following ESRs:

ESR 99-00114 RO

P-4 Operability Determination

ESR 99-00142 RO

Essential Services Chilled Water Operability Evaluation for Shut

Non-Nuclear-Safety Isolation Valves

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R16 0 erator Work-Arounds

The inspectors reviewed an operator work-around associated

with the essential service

chilled water non-essential isolation valves.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R19

Post Maintenance Testin

The inspectors reviewed the following post-maintenance

tests:

Number

OST-1 077

OST-1085

EPT-33

Test Procedure

Title

"AuxiliaryFeedwater Valves

Operability Test Quarterly

Interval Mode 4-5-6"

"1A-SA Diesel Generator

Operability Test"

"Emergency Safeguards

Sequencer System Test"

Related maintenance task

Steam generator preheater bypass

valve air pump leak repair

Diesel generator preventive

maintenance

Sequencer relay calibration.

b.

Observations and Findin s

No findings were identified and documented through this inspection.

1R22

Surveillance Testin

The inspectors reviewed the following surveillance tests:

Number'ev.

Title

MST-I0027

FPT-3004

"Steam generator B Narrow Range Level (L-0485)Calibration-

ATWS portion"

"Main Fire Pump Flow Test, Annual Interval"

.b.

Observations and Findin s

No findings were identified and documented through this inspection.

4.

OTHER ACTIVITIES

4OA4 Other

Closed

LER 50-400/98-004-00 and 01: Design deficiency related to inadequate runout

protection for the Turbine Driven AFW Pump. This LER did not involve a violation of

regulatory requirements and was closed.

4OA5 Mana ement Meetin s

Exit Meetin

Summa

The inspectors presented the inspection results to members of licensee management

on

October 21, 1999. The licensee acknowledged the findings presented.

The inspectors asked the. licensee whether any of the material examined during the

inspection should be considered proprietary.

No proprietary information was identified.

PARTIALLIST OF PERSONS CONTACTED

NRC

B. Bonser, Chief, Reactor Projects Branch 4

R. Laufer, Harris Project Manager, NRR

Licensee

D. Alexander, Regulatory Affairs Manager

C. Burton, Director of Site Operations

B. Clark, Harris Plant General Manager,

J. Cook, Outage Manager

R. Field, Nuclear Assessment

Manager

T. Hobbs, Acting Operations Manager

J. Holt, Outage and Scheduling Manager

M. Keef, Training Manager

G. Kline, Harris Engineering Support Services Manager

J. Scarola, Harris Plant Vice President

B. Waldrep, Maintenance Manager

E. Wills, Environmental & Radiation Control Manager

~Oened

50-400/99-06-01

Closed

50400/99-06-01

50-400/98-004-00

50%00/98-004-01

ITEMS OPENED, CLOSED, AND DISCUSSED

NCV

Failure to recognize that an a(1) goal was exceeded

(Section 1R12)

NCV

Failure to recognize that an a(1) goal was exceeded

(Section 1R12)

LER

Design deficiency related to inadequate runout protection for the

Turbine Driven AFW Pump.

(Section 4OA4)

LER

Design Deficiency related to inadequate runout protection for the

Turbine Driven AFW Pump. (Section 4OA4)

0