IR 05000397/2009002

From kanterella
Jump to navigation Jump to search
IR 05000397-09-002 Columbia Generating Station Inspection Report 01/01 - 03/28/2009
ML091200761
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 04/30/2009
From: Webb Patricia Walker
NRC/RGN-IV/DRP/RPB-A
To: Parrish J
Energy Northwest
References
IR-09-002
Download: ML091200761 (36)


Text

April 30, 2009

Mr. J. Chief Executive Officer Energy Northwest P.O. Box 968, Mail Drop 1023 Richland, WA 99352-0968

Subject:

COLUMBIA GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000397/2009002

Dear Mr. Parrish:

On March 28, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Columbia Generating Station. The enclosed integrated inspection report documents the inspection findings, which were discussed on April 7, 2009, with Mr. T. Lynch, Plant General Manager, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents one NRC-identified finding and one-self-revealing finding of very low safety significance (Green). One of these findings was determined to involve a violation of NRC requirements. However, because of the very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a noncited violation, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest this violation or the significance of the finding, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E. Lamar Blvd.,

Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Columbia Generating Station facility. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at the Columbia Generating Station. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.

UNITED STATES NUCLEAR REGULATORY COMMISSION R E GI ON I V 612 EAST LAMAR BLVD, SUITE 400 ARLINGTON, TEXAS 76011-4125

Energy Northwest

- 2 -

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its enclosure, will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Wayne C. Walker, Chief Project Branch A Division of Reactor Projects

Docket 50-397 License:

NPF-21

Enclosure:

NRC Inspection Report 05000397/2009002 w/Attachment: Supplemental Information

REGION IV==

Docket:

50-397 License:

NPF-21 Report:

05000397/2009002 Licensee:

Energy Northwest Facility:

Columbia Generating Station Location:

Richland, Washington Dates:

January 1, 2009 through March 28, 2009 Inspectors:

R. Cohen, Senior Resident Inspector, Project Branch A, DRP C. Graves, Health Physicist, Plant Support Branch 2, DRS N. Hernandez, Project Engineer, Project Branch A, DRP Approved By:

W. Walker, Chief, Project Branch A, Division of Reactor Projects

- 2 -

Enclosure

SUMMARY OF FINDINGS

IR 05000397/2009002; 01/01/2009 - 03/28/2009; Columbia Generating Station; Equipment

Alignments; Event Followup The report covered a 3-month period of inspection by resident inspectors. One green noncited violation and one green finding was identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

The inspectors reviewed a self-revealing finding for the failure of Energy Northwest to perform an adequate site acceptance test of the digital electro-hydraulic system. Specifically, Energy Northwest failed to verify that the quad voter solenoid valves in the digital electro-hydraulic system could be replaced with the main turbine on-line. Consequently, when an on-line valve replacement was performed, the system experienced a pressure transient which resulted in a fast closure of the main turbine governor valves and a subsequent reactor scram. Energy Northwest entered the issue into the corrective action program and conducted a root cause evaluation.

This finding is greater than minor because it was a human performance error that affected the initiating events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The finding was of very low risk significance because the finding did not result in the loss of a safety function of a single train for greater than its technical specification allowed outage time. This finding was determined to have the crosscutting aspect of human performance with a decision making component, because Energy Northwest failed to perform an adequate effectiveness review to identify the possible unintended consequences of on-line replacement of quad voter solenoid valves in the digital electro-hydraulic system

H.1.b]. (Section 4OA3.1)

Cornerstone: Mitigating Systems

Green.

The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, for Energy Northwests failure to follow procedure PPM 10.2.53, Seismic Requirements for Scaffolding, Ladders,

Man-Lifts, Tool Gang Boxes, Hoists, Metal Storage Cabinets, and Temporary Shielding Racks, Revision 26. Specifically, the position of equipment is required to meet specific criteria to prevent damage to safety-related equipment during a seismic event. Contrary to this procedure, the inspectors identified that equipment was routinely positioned next to safety-related equipment without a supporting engineering evaluation.

This finding is greater than minor because it was a human performance error which affected the mitigating systems cornerstone objective to ensure the availability and reliability of systems that respond to initiating events to prevent undesirable consequences. This was determined to be consistent with NRC Manual Chapter 0612, Power Reactor Inspection Reports, Appendix E, Example 4.a. for being more than minor risk significance because Energy Northwest had routinely failed to perform the requisite engineering evaluation. The finding was determined to be of very low risk significance (Green) because no actual loss of safety function occurred and the finding did not screen as potentially risk significant due to external events.

Specifically, the as-found position of the equipment was determined to not adversely affect seismic qualification of the affected safety-related components. A crosscutting aspect in human performance with a work control component was identified in that Energy Northwest failed to appropriately plan work on multiple occasions, resulting in job site conditions which may have impacted plant components H.3.a].

(Section 1R04).

Licensee-Identified Violations

None

REPORT DETAILS

Summary of Plant Status

The inspection period began with Columbia Generating Station operating at 100 percent power.

On January 16, the station reduced power to 65 percent power to perform work on reactor feed water drive turbine 1B speed control system. Following this work, the station returned to 100 percent power on January 18, 2009. On February 8, the station reduced power to 75 percent to facilitate maintenance of the main turbine digital electro-hydraulic system. Later on February 8, the reactor was subsequently shutdown following an automatic reactor scram and entered forced outage 09-01 due to a malfunction of the main turbine digital electro-hydraulic system.

The station returned to 100 percent power on February 13, 2009. The facility operated at 100 percent power, with the exception of scheduled reductions in power to support minor maintenance and testing, for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

1R01 Adverse Weather Protection

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of the licensees adverse weather procedures for seasonal extremes (e.g., extreme high temperatures, extreme low temperatures, or hurricane season preparations). The inspectors verified that weather-related equipment deficiencies identified during the previous year were corrected prior to the onset of seasonal extremes; and evaluated the implementation of the adverse weather preparation procedures and compensatory measures for the affected conditions before the onset of, and during, the adverse weather conditions.

During the inspection, the inspectors focused on plant-specific design features and the licensees procedures used to mitigate or respond to adverse weather conditions.

Additionally, the inspectors reviewed the Updated Final Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:

These activities constitute completion of one readiness for seasonal adverse weather sample as defined in Inspection Procedure 71111.01-05.

b. Findings

No findings of significance were identified.

.2 Readiness for Impending Adverse Weather Conditions

Since extreme cold and high wind conditions were forecast in the vicinity of the facility for February 27, 2009, the inspectors reviewed the licensees overall preparations/protection for the expected weather conditions. On February 27, 2009, the inspectors walked down the reactor building ventilation system because its safety-related functions could be affected or required as a result of the extreme cold conditions forecast for the facility. The inspectors reviewed licensee procedures and discussed potential compensatory measures with control room personnel. The inspectors focused on plant managements actions for implementing the stations procedures for ensuring adequate personnel for safe plant operation and emergency response would be available. Specific documents reviewed during this inspection are listed in the attachment.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignments

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • Division 1 Diesel Generator, February 20, 2009
  • Standby Liquid Control System, March 4, 2009 The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two partial system walkdown samples as defined in Inspection Procedure 71111.04-05.

b. Findings

Introduction:

The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for Energy Northwests failure to conduct engineering evaluations in accordance with the stations seismic requirement procedure as it relates to equipment positioned adjacent to safety-related components.

A crosscutting aspect in human performance with a work control component was also identified.

Description:

On March 5, 2009, during a walkdown of the standby liquid control system, the inspectors noted that an emergency operating procedure equipment storage container had been positioned adjacent to standby liquid control pump 1B. This barrel had been moved in an effort to control radioactive contamination following a steam leak in the reactor water cleanup heat exchanger room the night before. The container consisted of an approximately six foot high steel barrel with emergency operating procedure hoses inside. The inspectors noted that this container was positioned such that it could over turn in an earthquake and potentially impact the safety-related standby liquid control system. The inspectors notified main control room personnel of the condition and operators immediately moved the barrel into a safe position away from the standby liquid control system. This was documented in AR/CR 193537.

The inspectors questioned the Energy Northwest staff if this met the requirements of procedure PPM 10.2.53, Seismic Requirements For Scaffolding, Ladders, Man-Lifts, Tool Gang Boxes, Hoists, Metal Storage Cabinets, And Temporary Shielding Racks, to properly secure or analyze equipment in close proximity to safety-related equipment to prevent seismically-induced interactions. Step 7.2.2 of PPM 10.2.53 states that transient equipment used in the reactor building is to be stored so it does not over turn in an earthquake and impact safety-related equipment. Tripping could occur if these items impacted adjacent structures such as curbs, pedestals, etc., in their lower 1/3 height.

This was a concern because the barrel did not meet this requirement. Energy Northwest staff concluded the damage that could result from an impact of the improperly staged barrels and the standby liquid control system during a seismic event was inconclusive.

During recent inspector walkdowns of safety related equipment, the inspectors identified five instances where scaffolding and transient equipment was staged in the vicinity of safety-related equipment without having an evaluation in accordance with PPM 10.2.53:

  • PER 207-0443, Protective Cover Over 125VDC Safety Related Battery, December 3, 2007
  • AR/CR 57437, Scaffolding Touching RHR-P-2B, No Engineering Evaluation, December 3, 2007
  • AR/CR 187910, Staging Touching MCC Room 250 VDC Electrical Cabinet, No Engineering Evaluation, October 27, 2008
  • AR/CR 187808, Clearance Issue Between RHR-P-2C Ventilation Duct Work and Scaffolding, No Engineering Evaluation, October 23, 2008
  • AR/CR 193537, Emergency Operating Procedure Barrels Positioned Adjacent to Standby Liquid Control Pump1A, March 5, 2009

Energy Northwest subsequently identified another instance of transient equipment not meeting the requirements of PPM 10.2.53:

  • AR/CR194193, Cart with unchecked wheels near safety related equipment, March 23, 2009.
Analysis:

The performance deficiency associated with this finding is the failure of Energy Northwest to adhere to procedure PPM 10.2.53 to evaluate if specified items positioned adjacent to safety related equipment is acceptable. There have been six recent occurrences where a supporting engineering evaluation was not performed to assure that seismic qualification of safety related equipment was maintained. This finding was more than minor because it was a human performance error which affected the Mitigating Systems Cornerstone objective to ensure the availability and reliability of systems that respond to initiating events to prevent undesirable consequences.

Although Energy Northwest assessed the as-found concerns as acceptable during subsequent analysis, the inspectors concluded that the failure to evaluate each condition in accordance with procedure PPM 10.2.53 was not commensurate with ensuring the reliability and availability of safety-related equipment in the plant. This was determined to be consistent with NRC Manual Chapter 0612, Power Reactor Inspection Reports, Appendix E, Example 4.a., for being more than minor risk significance because Energy Northwest had routinely failed to perform the requisite engineering evaluations. The finding was determined to be of very low risk significance (Green) because no actual loss of safety function occurred and the finding did not screen as potentially risk significant due to external events. A crosscutting aspect in human performance with a work control component was identified in that Energy Northwest failed to appropriately plan work on multiple occasions, resulting in job site conditions which may have impacted plant components H.3.a].

Enforcement:

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, provides, in part, that activities affecting quality shall be accomplished in accordance with documented instructions appropriate to the circumstances. Contrary to this requirement, on March 5, 2009 and other dates, Energy Northwest failed to adhere to procedure PPM 10.2.53 resulting in the failure to conduct an engineering evaluation to assess the seismic interaction of equipment staged adjacent to safety related components. Because this finding was of very low safety significance and was entered into the licensees corrective action program as AR/CR 193537, this violation is being treated as a noncited violation, consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000397/2007009-01; Failure to Perform Engineering Evaluation to Determine Seismic Qualification of Safety-related Equipment). Energy Northwest implemented corrective actions to assess an adverse trend associated with failure to perform engineering evaluations, AR/CR 193537.

.2 Complete Walkdown

a. Inspection Scope

On January 7, 2009, the inspectors performed a complete system alignment inspection of the Residual Heat Removal System Train C to verify the functional capability of the system. The inspectors selected this system because it was considered both safety-significant and risk-significant in the licensees probabilistic risk assessment. The inspectors walked down the system to review mechanical and electrical equipment line-ups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. The inspectors reviewed a sample of past and outstanding work orders to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the corrective action program database to ensure that system equipment-alignment problems were being identified and appropriately resolved. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as defined in Inspection Procedure 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:

  • DG-2/1, Division 1 Diesel Generator Room, February 19, 2009
  • RC-6/2, Division 2 Battery Room, February 23, 2009
  • R-8/1, Low Pressure Core Spray Pump Room, February 23, 2009
  • RC-8/2 Division 2 Switchgear Room, March 17, 2009

The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant

transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of six quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, the flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; reviewed the corrective action program to determine if licensee personnel identified and corrected flooding problems; inspected underground bunkers/manholes to verify the adequacy of sump pumps, level alarm circuits, cable splices subject to submergence, and drainage for bunkers/manholes; and verified that operator actions for coping with flooding can reasonably achieve the desired outcomes. The inspectors also walked down the three areas listed below to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers. Specific documents reviewed during this inspection are listed in the attachment.

  • General floor area, Reactor Building 522 Elevation, March 3, 2009
  • MCC Rooms 410 and 411, Reactor Building 522 Elevation, March 3, 2009
  • RWCU Pump Rooms 1A and 1B, Reactor Building 522 Elevation, March 3, 2009

These activities constitute completion of one flood protection measures inspection sample as defined in Inspection Procedure 71111.06-05.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

.1 Annual Inspection

a. Inspection Scope

The inspectors reviewed licensee programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for the

Residual Heat Removal Heat Exchanger 1B. The inspectors verified that performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552, "Heat Exchanger Performance Monitoring Guidelines;" the licensee properly utilized biofouling controls; the licensees heat exchanger inspections adequately assessed the state of cleanliness of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one heat sink inspection sample as defined in Inspection Procedure 71111.07-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

On March 23, 2009, the inspectors observed a crew of licensed operators in the plants simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • Licensed operator performance
  • Crews clarity and formality of communications
  • Crews ability to take timely actions in the conservative direction
  • Crews prioritization, interpretation, and verification of annunciator alarms
  • Crews correct use and implementation of abnormal and emergency procedures
  • Control board manipulations
  • Oversight and direction from supervisors
  • Crews ability to identify and implement appropriate technical specification actions and emergency plan actions and notifications The inspectors compared the crews performance in these areas to pre-established operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed operator requalification program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk significant systems:

  • Control Room Normal Outside Air Intake Isolation Valve WOA-V-51C Failed to Close, February 20, 2009 The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • Manitowoc Crane Movement, January 23, 2009
  • Work Order 01161641, OSP-SLC/IST-Q701, Standby Liquid Control Pumps Operability Test, March 12, 2009 The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • Diesel Generator 2, Fuel Oil Filter Position, January 10, 2009
  • Diesel Generator 1, Failed Speed Switch, January 26, 2009
  • DMA-M-AD22/1, January 26, 2009
  • RWCU-RV-3 Leaking into RWCU Room, AR/CR 193562, March 11, 2009

The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Updated Safety Analysis Report to the licensees evaluations, to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.

Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four operability evaluations inspection samples as defined in Inspection Procedure 71111.15-05

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed the following temporary modification to verify that the safety functions of important safety systems were not degraded:

  • TMR-09-004, Digital Electrical Hydraulic Quad Voter Solenoid Trip Valve Supplemental Cooling, January 23, 2009 The inspectors reviewed the temporary modification and the associated safety evaluation screening against the system design bases documentation, including the Updated Final Safety Analysis Report and the Technical Specifications, and verified that the modification did not adversely affect the system operability/availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers.

These activities constitute completion of one sample for temporary plant modifications as defined in Inspection Procedure 71111.18-05

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:

  • Work Order 01160713, OSP-ELEC-M703, HPCS Diesel Generator Monthly Operability Test, February 25, 2009 The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities for the following (as applicable):
  • The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed
  • Acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate The inspectors evaluated the activities against the technical specifications, the Updated Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of six postmaintenance testing inspection sample(s) as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Forced Outage that occurred from February 8 - 13, 2009, to confirm that licensee personnel had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth.

During the forced outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below.

  • Configuration management, including maintenance of defense-in-depth, is commensurate with the outage safety plan for key safety functions and compliance with the applicable technical specifications when taking equipment out of service.
  • Clearance activities, including confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing.
  • Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error.
  • Status and configuration of electrical systems to ensure that technical specifications and outage safety-plan requirements were met, and controls over switchyard activities.
  • Reactor water inventory controls, including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss.
  • Controls over activities that could affect reactivity.
  • Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one outage inspection sample as defined in Inspection Procedure 71111.20-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure requirements, and technical specifications to ensure that the fifteen surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems, structures, and components not meeting the test acceptance criteria were correct
  • Reference setting data
  • Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
  • OSP-SW-Q101, SW Spray Pond Average Sediment Measurement, March 17, 2009 Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four samples including: one inservice test, and three surveillance testing inspection samples as defined in Inspection Procedure 71111.22-05.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on March 9, 2009, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the simulator, Emergency Response Facility and the Technical Support Center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures.

The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the corrective action program. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71114.06-05.

b. Findings

No findings of significance were identified.

.2 Training Observations

a. Inspection Scope

The inspectors observed a simulator training evolution for licensed operators on January 13, 2009, which required emergency plan implementation by a licensee operations crew.

This evolution was planned to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the postevolution critique for the scenario. The focus of the inspectors activities was to note

any weaknesses and deficiencies in the crews performance and ensure that the licensee evaluators noted the same issues and entered them into the corrective action program. As part of the inspection, the inspectors reviewed the scenario package and other documents listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71114.06-05.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Unplanned Scrams per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical Hours performance indicator for the period from the 1st quarter 2008 through the 4th quarter 2008. To determine the accuracy of the performance indicator data reported during those periods, performance indicator definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports and NRC integrated inspection reports for the period of 1st quarter 2008 through the 4th quarter 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of one unplanned scrams per 7000 critical hours sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.2 Unplanned Scrams with Complications

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams with Complications performance indicator for the period from the 1st quarter 2008 through the 4th quarter 2008. To determine the accuracy of the performance indicator data reported during those periods, performance indicator definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports and NRC integrated inspection reports for the period of 1st quarter 2008 through the 4th quarter 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had

been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of one unplanned scrams with complications sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.3 Unplanned Power Changes per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Power Changes per 7000 Critical Hours performance indicator for the period from the 1st quarter 2008 through the 4th quarter 2008. To determine the accuracy of the performance indicator data reported during those periods, performance indicator definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports and NRC integrated inspection reports for the period of 1st quarter 2008 through the 4th quarter 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of one unplanned power changes per 7000 critical hours sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included: the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic

implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings of significance were identified.

.3 Selected Issue Follow-up Inspection

a. Inspection Scope

During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting emergency diesel air dampers operating contrary to design documents, AR/CR 191600, dated February 23, 2009. The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment and corrective maintenance issues but also considered the results of daily inspector corrective action program item screening discussed in Section 4OA2.1. The review also included issues documented outside the normal corrective action program in system health reports, corrective maintenance work orders, component status reports, and maintenance rule assessments. The inspectors review nominally considered the six-month period of October 2008 through March 2009, although some examples expanded beyond those dates when the scope of the trend warranted. Corrective actions associated with identified trends were reviewed for adequacy.

These activities constitute completion of 1 in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.

b. Findings

No findings of significance were identified.

4OA3 Event Follow-up

.1 February 8, 2009 Automatic Reactor Scram

a. Inspection Scope

On February 8, 2009 the inspectors observed and evaluated Energy Northwests response to a scram while the reactor was operating at 75 percent power. Specifically, failure to adequately vent the digital electro-hydraulic system following on-line replacement of quad voter solenoid valve DEH-SV-TRIP/B caused the digital electro-hydraulic system header to momentarily depressurize during post maintenance testing, which resulted in fast closure of the main turbine governor valves and a reactor scram.

The inspectors responded to the site and verified plant conditions by observing key plant parameters, annunciator status, and observing the current status of safety related mitigating equipment to ensure that the reactor plant was stable. The inspectors also observed reactor operator actions in response to the reactor scram and senior reactor operators evaluation of plant conditions and oversight of the reactor operators to ensure that operators were adhering to plant procedures. The inspectors also reviewed Energy Northwests evaluation of the root cause of the scram.

b. Findings

Introduction:

A self-revealing Green finding was reviewed for the failure of Energy Northwest to perform an adequate site acceptance test of the digital electro-hydraulic system. Specifically, Energy Northwest failed to verify that the quad voter solenoid valves in the digital electro-hydraulic system could be replaced with the main turbine on line. Consequently, when an on-line valve replacement was performed, the system experienced a pressure transcient which resulted in a fast closure of the main turbine governor valves and a subsequent reactor scram.

Description:

On February 8, 2009, following on-line replacement of quad voter solenoid valve DEH-SV-TRIP/B, the digital electro-hydraulic system trip header momentarily depressurized during post maintenance testing. This generated a reactor protection system governor valve fast closure trip signal which caused a reactor scram. This condition was documented in AR/CR 191843.

Energy Northwest concluded in their root cause evaluation that the direct cause of the reactor scram was the instantaneous recompression of an air bubble trapped in the intervalve cavity between the A and B quad voter valves. Collapsing this bubble resulted in backflow of digital electro-hydraulic system fluid from the emergency trip header into the intervalve cavity between the A and B valves when DEH-SV-TRIP/B was reenergized during the post maintenance test. The air bubble had entered the quad voter assembly during on-line replacement of DEH-SV-TRIP/B and was not effectively removed during the venting process. There are no vent valves in the high pressure supply line or trip headers. Therefore, maintenance planning included cycling the A & B quad voter valves two times each to vent as much air as possible out of the lines and into the digital electro-hydraulic system drain header. The sequence of steps established in WO 01166095 was expected to ensure adequate venting based on tests

performed by the vendor. A separate work order, WO 01166172, was generated to perform the weekly surveillance OSP-MT-W701 immediately following valve replacement as a post maintenance test to demonstrate operability of the newly installed valve. The surveillance was performed with the digital electro-hydraulic system in the automatic mode, which tests one solenoid valve approximately every 12 seconds in A-B-C-D sequence. Testing had been completed on quad voter valve DEH-SV-TRIP/B and the valve had just been reenergized when the reactor automatically scrammed on a governor valve fast closure signal. The quad voter solenoid valve trip headers briefly depressurized as evidenced by the first reactor trip signal, which came as a result of governor valve trip header low pressure (pressure less than 1270 psig). This was immediately followed by a reactor protection system trip signal due to throttle valve less than full open when the throttle valves momentarily closed then re-opened. This valve motion was not caused by a turbine trip signal since the main turbine trip did not occur until approximately 1.5 minutes later.

Energy Northwest determined the root cause to be design deficiencies in the on-line serviceable quad voter assembly, which allowed system conditions that resulted in a reactor trip following performance of on-line maintenance activities. During factory acceptance testing, the vendor conducted tests to assess the impact of potential air bubble formation in the quad voter valves, however, differences between the test setup and actual plant configurations may have masked the effect of an air bubble in the system. The vendor and Energy Northwest consequently concluded that air bubble formation and its potential impact on the emergency trip header pressure were not potential vulnerabilities. The corrective action would have been to install check valves to prevent unnecessary pressure transients in the emergency trip header. The licensee determined the corrective action to be unnecessary because the digital electro-hydraulic system would not be subject to air intrusion during normal operation. This resulted in a missed opportunity to correct the design deficiency. In addition, the site acceptance test program did not contain specific test sequences to verify that the trip solenoid valves could be replaced with the main turbine on-line. The inspectors reviewed Energy Northwests root cause evaluation and could not provide any information to the contrary.

Energy Northwest Procedure DES 2-1, Plant Design Changes, Revision 27, step 4.3.37 states that, results and conclusions of design verification testing or other design verification activities performed by vendor(s), as well as exceptions and resolutions to deviations to acceptance criteria in vendor design tests shall be evaluated for impact to plant design. Contrary to this, Energy Northwest failed to perform an adequate site acceptance test to verify that maintenance on the digital electro-hydraulic system could be performed with the main turbine on-line.

Analysis:

Energy Northwests failure to perform an adequate site acceptance test is a performance deficiency. Specifically, failure to analyze differences between the vendors factory acceptance test and actual plant conditions resulted in a failure of the site acceptance test program to identify that the online replacement of the quad voter solenoid valves could result in a pressure transcient in the DEH system leading to a plant trip.

The inspectors used NRC Inspection Manual Chapter 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, to determine that the finding was more than minor because it was a human performance error that affected the initiating events cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. The inspectors evaluated the finding in accordance with Manual Chapter 0609, Appendix A, Significance Determination Process, Phase 1 Worksheet. The finding was determined to be of very low safety significance (Green) because the finding did not result in the loss of a safety function of a single train for greater than its Technical Specification allowed outage time. This finding was determined to have a crosscutting aspect of human performance with a decision making component, because Energy Northwest failed to perform an adequate effectiveness review to identify the possible unintended consequences of on-line replacement of quad voter solenoid valves in the digital electro-hydrolic system H.1.b].

Enforcement:

No violations of NRC requirements were identified since the affected component, digital electro-hydraulic system, is non-safety related (FI 05000397/2009002-02; Failure to perform an adequate site acceptance test).

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors performed observations of security force personnel and activities to ensure that the activities were consistent with Columbia Generating Stations security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

4OA6 Meetings

Exit Meeting Summary

On April 7, 2009, the inspectors presented the inspection results to Mr. T Lynch, Plant General Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Parrish, Chief Executive Officer
D. Atkinson, Vice president, Nuclear Generation
G. Cullen, Manager, Regulatory Programs
J. Frisco, General Manager, Engineering
S. Gambhir, Vice President, Technical Services
W. LaFramboise, System Engineering Manager
T. Lynch, Plant General Manager
F. Schill, Licensing
C. Whitcomb, Vice President, Organizational Performance and Staffing

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000397/2009002-01 NCV Failure to Perform Engineering Evaluation to Determine Seismic Qualification of Safety related Equipment (Section 1R04)
05000397/2009002-02 FIN Failure to Perform an Adequate Site Acceptance Test (Section 4OA3)

LIST OF DOCUMENTS REVIEWED