IR 05000395/2007005

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IR-05000395-07-005, on 10/01/2007 - 12/31/2007, Virgil C. Summer Nuclear Station, Examination of Activities Conducted Under License as Related to Safety and Compliance with Commission Rules and Regulations and License Conditions
ML080240280
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 01/24/2008
From: Eugene Guthrie
Division Reactor Projects II
To: Archie J
South Carolina Electric & Gas Co
References
IR-07-005
Download: ML080240280 (31)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ary 24, 2008

SUBJECT:

VIRGIL C. SUMMER NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000395/2007005

Dear Mr. Archie:

On December 31, 2007, the United States Nuclear Regulatory Commission (NRC) completed an inspection at your Virgil C. Summer Nuclear Station. The enclosed integrated inspection report documents the inspection results, which were discussed with you and other members of your staff on January 10, 2008.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents two NRC-identified findings of very low safety significance (Green) which were determined to be violations of NRC requirements. However, because of the very low safety significance of the issues and because they were entered into your corrective action program, the NRC is treating these violations as non-cited violations (NCVs) consistent with Section VI.A. of the NRCs Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Virgil C. Summer Nuclear Station.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the

SCE&G 2 NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eugene F. Guthrie, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket No.: 50-395 License No.: NPF-12

Enclosure:

NRC Integrated Inspection Report 05000395/2007005 w/Attachment: Supplemental Information

REGION II==

Docket No.: 50-395 License No.: NPF-12 Report No.: 05000395/2007005 Licensee: South Carolina Electric & Gas (SCE&G) Company Facility: Virgil C. Summer Nuclear Station Location: P. O. Box 88 Jenkinsville, SC 29065 Dates: October 1, 2007 - December 31, 2007 Inspectors: J. Zeiler, Senior Resident Inspector J. Polickoski, Resident Inspector W. Fowler, Reactor Inspector (Section 1R02 and 1R17.2)

C. Moore, Licensing Examiner, Region III (Section 1R11)

R. Moore, Senior Reactor Inspector (Section 1R02 and 1R17.2)

C. Peabody, Reactor Inspector (Section 1R02 and 1R17.2)

D. Mas Penaranda, Reactor Inspector (Section 1R02 and 1R17.2)

L. Miller, Senior Emergency Preparedness Inspector (Section 1EP4)

Approved by: Eugene F. Guthrie, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000395/2007-005; 10/01/2007 - 12/31/2007; Virgil C. Summer Nuclear Station;

Maintenance Risk Assessment and Emergent Work Control and Surveillance Testing.

The report covered a three-month period of inspection by two resident inspectors,

Region II reactor inspectors, an emergency preparedness inspector and a Region III licensing examiner. Two Green findings, which were non-cited violations (NCVs), were identified by the NRC. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified Findings

Cornerstone: Initiating Events

Green.

A Green non-cited violation (NCV) of Technical Specifications (TS)

Limiting Condition for Operation (LCO) 3.4.6.1, Leak Detection Systems, was identified by the inspectors for failure to maintain two required reactor coolant system (RCS) leak detection systems operable and complete the required TS actions. Specifically, the Reactor Building Cooling Unit (RBCU) condensate drain flow detector (IFS01900A) was discovered to be inoperable for a significant period of time due to debris clogging the flow detector flow path. During the last three years prior to October 4, 2007, this condition was coincident with multiple time periods when the reactor building atmosphere gaseous and particulate radioactivity monitors were also inoperable for greater than six hours. The licensee immediately cleaned the condensate flow detector piping, calibrated the detector, restored compliance with TS, and documented this issue in their corrective action program as CR-07-02167 and CR-07-03332.

This finding was more than minor because it affected the availability, reliability, and maintenance of the barrier integrity equipment performance attribute of the initiating events cornerstone and adversely affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. With the RBCU condensate flow detector inoperable coincident with reactor building atmosphere gaseous and particulate radioactivity monitors, the capability of performing the TS, design bases function was lost for a significant period of time.

The finding was evaluated using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process, Phase I Worksheet for initiating events.

The finding is determined to be of very low safety significance because at least one method of RCS leak detection (reactor building sump level) was available to the licensee and no actual leakage above one gpm (the TS required limit for RCS unidentified leakage) was indicated through the RCS water balance surveillance test during the reviewed time period. The finding directly involves the cross-cutting area of Human Performance under the Complete Documentation and

Component Labeling aspect of the Resources component, in that, the condensate flow detector TS surveillance procedure failed to test the capability of the system to perform its specified function to include support and auxiliary equipment (H.2.c). (Section 1R22)

Cornerstone: Barrier Integrity

Green.

A Green non-cited violation (NCV) of Technical Specifications (TS)

Limiting Condition for Operation (LCO) 3.6.4, Containment Isolation Valves, was identified by the inspectors for the failure to implement required administrative controls when opening the normally locked closed inner and outer manual containment isolation valves (CIVs) 8767-DN and 8768-DN, in containment penetration XRP0231. The licensee drained the penetration, returned the valves to their locked closed positions, and documented this violation in their corrective action program as CR-07-02894.

The failure to implement TS required administrative controls when opening normally locked closed CIVs 8767-DN and 8768-DN constituted a performance deficiency and a finding. This finding is more than minor because it affected the containment boundary configuration control attribute of the barrier integrity cornerstone and affected the cornerstone objective of providing reasonable assurance that the containment physical design barrier protects the public from radionuclide releases caused by accidents or events. The finding was evaluated using Inspection Manual Chapter 0609, Significance Determination Process,

Appendix H, Containment Integrity Significance Determination Process. This finding is of very low safety significance (Green) because of the short duration both valves were open and the small size of the piping (one-inch) penetrating containment. The finding directly involves the cross-cutting area of Human Performance under the Work Planning aspect of the Work Control component, in that, appropriate work plans were not implemented to ensure that operators were stationed locally to close both valves in the event of a design bases accident resulting in a violation of TS 3.6.4 (H.3.a). (Section 1R13)

Licensee-Identified Violations

None.

REPORT DETAILS

Summary of Plant Status

The unit began the inspection period at 100 percent rated thermal power (RTP). The unit operated at or near RTP for the entire inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

Seasonal Weather Susceptibilities

a. Inspection Scope

The inspectors performed one adverse weather inspection for readiness of cold weather.

The inspectors verified the licensee had implemented applicable sections of operations administrative procedure (OAP)-109.1, Guidelines for Severe Weather, and heat trace instrument control procedures. The inspectors walked down three accessible areas of risk-significant equipment, including level instrumentation associated with the condensate storage tank, safety-related tanks in the refueling water storage tank (RWST) pit, and service water pump house cooling coil realignment, to assess whether the equipment was adequately protected from cold weather conditions. Also, the inspectors reviewed the licensees corrective action program (CAP) database to verify that freeze protection problems were being identified at the appropriate level, entered into the CAP, and appropriately resolved.

b. Findings

No findings of significance were identified.

1R02 Evaluations of Changes, Tests or Experiments

a. Inspection Scope

The inspectors reviewed selected samples of evaluations to confirm that the licensee had appropriately considered the conditions under which changes to the facility, Final Safety Analysis Report (FSAR), or procedures may be made, and tests conducted, without prior NRC approval. The inspectors reviewed evaluations for five changes and additional information, such as calculations, supporting analyses, the FSAR, and drawings to confirm that the licensee had appropriately concluded that the changes could be accomplished without obtaining a license amendment. The evaluations reviewed are listed in the Attachment to this report.

The inspectors also reviewed samples of changes for which the licensee had determined that evaluations were not required to confirm that the licensees conclusions to screen out these changes were correct and consistent with 10 CFR 50.59. The sixteen screened out changes reviewed are listed in the Attachment to this report.

The inspectors also reviewed self assessments and condition reports (CRs) to verify that problems were identified at an appropriate threshold, were entered into the CAP, and appropriate corrective actions had been initiated.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors conducted three partial equipment alignment walkdowns (listed below) to evaluate the operability of selected redundant trains or backup systems with the other train or system inoperable or out of service (OOS). Correct alignment and operating conditions were determined from the applicable portions of drawings, system operating procedures (SOPs), FSAR, and technical specifications (TS). The inspections included review of outstanding maintenance work orders (WOs) and related CRs to verify that the licensee had properly identified and resolved equipment alignment problems that could lead to the initiation of an event or impact mitigating system availability. Documents reviewed are listed in the Attachment to this report.

  • B service water booster pump (SWBP) (while A SWBP was OOS for scheduled maintenance);

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown

a. Inspection Scope

The inspectors performed one complete review and walkdown of the safety-related reactor building cooling system to identify any discrepancies between the current operating system equipment lineup and the designed lineup. This walkdown included the control room instrumentation and accessible areas outside the containment. In addition, the inspectors reviewed completed surveillance procedures, system health reports, and related CRs to verify that the licensee had properly identified and resolved equipment problems that could affect the availability and operability of the system.

Documents reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Fire Protection - Tours

a. Inspection Scope

The inspectors reviewed recent CRs, WOs, and impairments associated with the fire protection system. The inspectors reviewed surveillance activities to determine whether they supported the operability and availability of the fire protection system. The inspectors assessed the material condition of the active and passive fire protection systems and features and observed the control of transient combustibles and ignition sources. The inspectors conducted routine inspections of the following nine areas (respective fire zones also noted):

  • 1DA switchgear room (fire zone IB-20);
  • 1DB switchgear rooms and heating, ventilation, and air-conditioning (HVAC)rooms (fire zones IB-16, 17, and 22.2);
  • Intermediate building 412' general area (fire zones IB-25.1.1, 1.2, 1.3 and 1.5);
  • Auxiliary building switchgear room (fire zone AB-1.29);
  • Battery and charger rooms A and B (fire zones IB-2, 3, 4, 5, and 6);
  • Turbine driven emergency feedwater (TDEFW) pump room (fire zone IB-25.2);
  • Charging pump rooms A, B, and C (fire zones AB-1.5, 1.6, 1.7);
  • Auxiliary building 374' elevation (fire zones AB-1.1, 1.2, and 1.3); and,

b. Findings

No findings of significance were identified.

.2 Fire Protection - Drill Observation

a. Inspection Scope

The inspectors observed the performance of the licensees fire drills on July 30, September 5, October 31, and November 14, 2007. The inspectors evaluated the readiness of licensee personnel to prevent and fight fires including the following aspects:

  • Observe whether turnout clothing and self-contained breathing apparatus (SCBA) equipment were properly worn;
  • Determine whether fire hose lines were properly laid out and nozzle pattern simulated being tested prior to entering the fire area of concern;
  • Verify that the fire area was entered in a controlled manner;
  • Review if sufficient firefighting equipment was brought to the scene by the fire brigade to properly perform their firefighting duties;
  • Verify that the fire brigade leaders fire fighting directions were thorough, clear and effective, and that, if necessary, offsite fire team assistance was requested;
  • Verify that radio communications with plant operators and between fire brigade members were efficient and effective;
  • Confirm that fire brigade members checked for fire victims and fire propagation into applicable plant areas;
  • Observe if effective smoke removal operations were simulated;
  • Verify that the fire fighting pre-plans were properly utilized and were effective; and,
  • Verify that the licensee pre-planned drill scenario was followed, drill objectives met the acceptance criteria, and deficiencies were captured in post drill critiques.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

Internal Flooding

a. Inspection Scope

The inspectors reviewed and walked down two areas (the diesel generator building and intermediate building IB-412' elevation) regarding internal flood protection features and equipment to determine consistency with design requirements, FSAR, and flood analysis documents. Risk significant structures, systems, and components (SSCs) in this area included the EDGs, emergency feedwater (EFW) pumps, component cooling water (CCW) pumps, and safety-related battery HVAC chiller rooms. The inspectors reviewed the licensees CAP database to verify that internal flood protection problems were being identified at the appropriate level, entered into the CAP, and appropriately resolved.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

Resident Inspector Quarterly Review

a. Inspection Scope

On October 2, the inspectors observed performance of senior reactor and reactor operators on the plant simulator during an emergency preparedness biennial exercise.

The scenario involved an earthquake with reactor fuel damage followed by a small break loss of cooling accident and containment leakage to outside atmosphere (EPP-07-01A).

From the simulator control room, the inspectors assessed emergency procedure usage and verified the operators were properly classifying the emergency events and making the required notifications and protective action recommendations in accordance with emergency plan procedures (EPP)-001, Activation and Implementation of Emergency Plan, EPP-001.1, Notification of Unusual Event, EPP-001.2, Alert, EPP-001.3, Site Area Emergency, and EPP-002, Communication and Notification. The inspectors evaluated the adequacy of the licensees conduct of the simulator critique performance and verified that any significant drill performance issues were captured by the licensee in their CAP.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors evaluated three equipment issues described in the CRs listed below to verify the licensees effectiveness of the corresponding preventive or corrective maintenance associated with SSCs. The inspectors reviewed maintenance rule (MR)implementation to verify that component and equipment failures were identified, entered, and scoped within the MR program. Selected SSCs were reviewed to verify proper categorization and classification in accordance with 10 CFR 50.65. The inspectors examined the licensees 10 CFR 50.65(a)(1) corrective action plans to determine if the licensee was identifying issues related to the MR at an appropriate threshold and that corrective actions were established and effective. The inspectors review also evaluated if maintenance preventable functional failures (MPFF) or other MR findings existed that the licensee had not identified. The inspectors reviewed the licensees controlling procedures, i.e., engineering services procedure (ES)-514, Maintenance Rule Implementation, and the Virgil C. Summer Important To Maintenance Rule System Function and Performance Criteria Analysis, to verify consistency with the MR requirements.

  • CR-06-04466, Nuclear instrumentation N35 failed low due to A-4 pre-amplifier card failure;
  • CR-07-02827, B HVAC chiller tripped on low lube oil pressure.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors evaluated, as appropriate, for the five selected work activities listed below:

(1) the effectiveness of the risk assessments performed before maintenance activities were conducted;
(2) the management of risk;
(3) that, upon identification of an unforseen situation, necessary steps were taken to plan and control the resulting emergent work activities; and,
(4) that emergent work problems were adequately identified and resolved. The inspectors evaluated the licensees work prioritization and risk characterization to determine, as appropriate, whether necessary steps were properly planned, controlled, and executed for the planned and emergent work activities listed below:
  • Work Week 2007-40, risk assessment for scheduled maintenance and/or testing on TDEFW, A service water pump, and reactor building cooling unit (RBCU)condensate drain flow detector troubleshooting and repair;
  • Work Week 2007-42, risk assessment for scheduled maintenance and/or testing on B RHR pump, B motor driven emergency feedwater pump (MDEFP), C charging pump, B reactor building (RB) spray system valves, and solid state protection system (SSPS) testing with reactor trip breaker rotation;
  • Work Week 2007-43, risk assessment for scheduled maintenance and/or testing on A EDG, A EDG air-start compressors, and A RHR pump and valve operating test, and emergent maintenance on A chill water pump and B steam generator (SG) power operated relief valve (PORV) upstream manual isolation valve;
  • Work Week 2007-45, risk assessment for scheduled maintenance and/or testing on B EDG, B EDG air-start compressors, and B component cooling water (CCW) pump; and,
  • Work Week 2007-47, risk assessment for corrective maintenance replacing the primary power supply for the turbine closed cycle cooling digital control system cabinet.

b. Findings

Introduction:

A Green non-cited violation (NCV) of TS Limiting Condition for Operation (LCO) 3.6.4, Containment Isolation Valves, was identified by the inspectors for the failure to implement required administrative controls when opening the normally locked closed inner and outer manual containment isolation valves (CIVs) 8767-DN and 8768-DN, in containment penetration XRP0231.

Description:

On October 5, 2007, with the unit operating in Mode 1, the inspectors noted that the licensee had established demineralized water via two CIVs (8767-DN and 8768-DN) in penetration XRP0231 to containment in order to provide a source of water for flushing debris found in piping upstream of the RBCU condensate drain flow detector, IFS01900A. These two CIVs were normally locked closed manual valves as required by TS Surveillance Requirement (SR) 4.6.1.1 to ensure primary containment integrity during accident conditions. TS 3.6.4 requires each CIV to be operable and allows normally locked closed manual CIVs to be opened on an intermittent basis under administrative control. These administrative controls include; stationing an operator at the valve controls, maintaining constant communication with the control room with instructions to close the valve in an accident situation, and ensuring that environmental conditions will not preclude access to close the valves. The inspectors questioned the on-shift Shift Supervisor on how the operators were controlling the opening of CIVs 8767-DN and 8768-DN. The inspectors learned that the CIVs had been opened between 10:27 am and 1:42 pm, without implementing administrative controls. The inspectors determined that the operators had erroneously assumed that since the penetration was declared inoperable because it was not in its normally drained condition, the administrative controls were not necessary. Subsequently, the licensee drained the penetration, returned the valves to their locked closed positions, and documented the problem in their corrective action program as CR-07-02894.

Analysis:

The failure to implement TS required administrative controls when opening normally locked closed CIVs 8767-DN and 8768-DN constituted a performance deficiency and a finding. This finding is more than minor because it affected the containment boundary configuration control attribute of the barrier integrity cornerstone and affected the cornerstone objective of providing reasonable assurance that the containment physical design barrier protects the public from radionuclide releases caused by accidents or events. The finding was evaluated using Inspection Manual Chapter 0609, Significance Determination Process, Appendix H, Containment Integrity Significance Determination Process. This finding is of very low safety significance (Green) because of the short duration both valves were open and the small size of the piping (one-inch) penetrating containment. The finding directly involves the cross-cutting area of Human Performance under the Work Planning aspect of the Work Control component, in that, appropriate work plans were not implemented to ensure that operators were stationed locally to close both valves in the event of a design bases accident resulting in a violation of TS 3.6.4 (H.3(a)).

Enforcement:

TS LCO 3.6.4, Containment Isolation Valves, requires each CIV to be operable and allows normally locked closed manual CIVs to be opened on an intermittent basis under specified administrative control. These administrative controls include; stationing an operator at the valve controls, maintaining constant communication with the control room with instructions to close the valve in an accident situation, and ensuring that environmental conditions will not preclude access to close the valves. Contrary to the above, on October 5, 2007, between 10:27 am and 1:42 pm, the licensee opened normally locked closed CIVs 8767-DN and 8768-DN in containment penetration XRP0231 without implementing any appropriate administrative controls.

Because this violation was determined to be of very low safety significance and was placed in the corrective action program as CR-07-02894, this violation is being treated as a NCV in accordance with Section VI.A.1 of the NRC Enforcement Policy, and is identified as NCV 05000395/2007005-01, Failure to Implement TS Required Administrative Controls When Opening Containment Isolation Valves 8767-DN and 8768-DN.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed three operability evaluations affecting risk significant mitigating systems to assess, as appropriate:

(1) the technical adequacy of the evaluations; (2)whether operability was properly justified and the subject component or system remained available, such that no unrecognized increase in risk occurred;
(3) whether other existing degraded conditions were considered;
(4) that the licensee considered other degraded conditions and their impact on compensatory measures for the condition being evaluated; and,
(5) the impact on TS limiting conditions for operations and the risk significance in accordance with the Significance Determination Process (SDP). Also, the inspectors verified that the operability evaluations were performed in accordance with station administrative procedure (SAP)-209, Operability Determination Process, and SAP-999, Corrective Action Program.
  • CR-07-02167, adequacy of testing and maintenance of the RBCU drain flow high alarm detectors;
  • CR-07-03082, B SG PORV upstream manual isolation valve (XVG-2808B) will not fully open.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

.1 Routine Inspection

a. Inspection Scope

The inspectors evaluated two engineering change request (ECR) packages for modifications in the initiating events and mitigating systems cornerstone areas to evaluate the modifications for adverse effects on system availability, reliability, and functional capability. The modifications and the associated attributes reviewed are as follows:

ECR-50690, Setpoint change for diesel generator crankcase pressure switches; and, ECR-50629, Loose parts monitoring system replacement

  • Plant Document Updating
  • Post-Modification Testing
  • Installation Records
  • Materials / Replacement Components For the selected modification packages, the inspectors observed portions of the as-built configuration. Documents reviewed included procedures, engineering calculations, modification design and implementation packages, work orders, site drawings, corrective action documents, applicable sections of the FSAR, supporting analyses, TS, and design basis information. The inspectors witnessed aspects of the post-modification testing of both modifications to verify adequate testing of the changes. The inspectors also reviewed selected CRs associated with the modifications to confirm that problems encountered with the implementation of the modifications were entered into the CAP.

Documents reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.2 Biennial Inspection

a. Inspection Scope

The inspectors evaluated ECR packages for nine modifications to evaluate the modifications for adverse effects on system availability, reliability, and functional capability. The nine modifications and the associated attributes reviewed are as follows:

ECR 50064, EDG air start aftercooler removal

  • Energy Needs
  • Materials/Replacement Components
  • Operations
  • Flowpaths
  • Structural
  • Licensing Basis
  • Failure Modes ECR 70442, Replace TWINAX cable from level switch to level probe for ILS01973-LD and ILS01974-LD
  • Energy Needs
  • Materials/Replacement Components
  • Control Signals
  • Operations
  • Structural ECR 50157A, Upgrade of EFW mini-flow line from non-nuclear safety related to quality related
  • Material Classification ECR 50157B, Deletion of speed controller for TDEFW pump
  • Timing
  • Control Signals
  • Structural
  • Equipment Protection
  • Materials ECR 50599, Main steam power operated relief valve circuit fix
  • Control Signal
  • Energy Needs
  • Equipment Protection ECR 70863, Replace Nuclear Instrumentation Channel 35A input power circuit breakers in Westinghouse 7300 cabinets with 30A circuit breakers
  • Control Signal
  • Energy Needs
  • Equipment Protection ECR 50478, Reactor building instrument air moisture removal upgrade
  • Materials/Replacement Components
  • Post Modification Testing
  • Plant Document Updating
  • Failure Modes
  • Operations
  • Implementation ECR 50511, EDG starting air compressor replacement
  • Materials/Replacement Components
  • Post Modification Testing
  • Plant Document Updating
  • Failure Modes
  • Operations
  • Implementation
  • Energy Needs Documents reviewed included procedures, engineering calculations, modification design and implementation packages, work orders, site drawings, corrective action documents, applicable sections of the FSAR, supporting analyses, TS, and design basis information.

Documents reviewed are listed in the Attachment to this report.

The inspectors also reviewed selected CRs associated with modifications to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

For the six maintenance activities listed below, the inspectors reviewed the associated post-maintenance testing (PMT) procedures and either witnessed the testing and/or reviewed test records to assess whether:

(1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel;
(2) testing was adequate for the maintenance performed;
(3) test acceptance criteria were clear and adequately demonstrated operational readiness consistent with design and licensing basis documents;
(4) test instrumentation had current calibrations, range, and accuracy consistent with the application;
(5) tests were performed as written with applicable prerequisites satisfied;
(6) jumpers installed or leads lifted were properly controlled; (7)test equipment was removed following testing; and,
(8) equipment was returned to the status required to perform its safety function. The inspectors verified that these activities were performed in accordance with general test procedure (GTP)-214, Post Maintenance Testing Guideline.
  • PMT for B RHR heat exchanger bypass and outlet flow control valve (FCV-603B/605B) air pressure regulators (WOs 0708487 and 0708488);
  • PMT for A EDG (WOs 0702178, 0708707 and 0711403);
  • PMT for B EDG scheduled quarterly maintenance (WOs 0709184, 0702993 and 0702179);
  • PMT for A CCW pump (WOs 0713305 and 0714024).

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed and/or reviewed the five surveillance test procedures (STPs)listed below to verify that TS surveillance requirements were followed and that test acceptance criteria were properly specified to ensure that the equipment could perform its intended safety function. The inspectors verified that proper test conditions were established as specified in the procedures, that no equipment preconditioning activities occurred, and that acceptance criteria were met.

In-Service Tests:

  • STP-205.004, RHR Pump and Valve Operability Test, Revision 6; Other Surveillance Tests:
  • STP-345.037, Solid State Protection System Actuation Logic and Master Relay Test, Train A, Critical Surveillance Test Category III, Revision 16;
  • STP-503.003B, Functional Test of B Train SW to EF Cross Connect Circuits, Revision 0, Change C;
  • STP-222.002, Component Cooling Pump Test, Revision 8; and,
  • STP-342.003, Reactor Building Cooling Unit Condensate Flow Detectors IFS01900A and IFS01900B Calibration, Revision 4.

b. Findings

Introduction:

A Green NCV of TS LCO 3.4.6.1, Leak Detection Systems, was identified by the inspectors for failure to maintain two required reactor coolant system leak detection systems operable and complete the required TS actions which were as follows; "With only two of the above required leakage detection systems OPERABLE, operation may continue for up to 30 days provided grab samples of the containment atmosphere are obtained and analyzed at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when the required gaseous or particulate radioactive monitoring system is inoperable; otherwise, be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."

Specifically, the RBCU condensate drain flow detector (IFS01900A) was discovered to be inoperable for a significant period of time due to debris clogging the flow detector flow path. The licensee review of the last three years prior to October 4, 2007, indicated that this condition was coincident with multiple time periods when the reactor building atmosphere gaseous and particulate radioactivity monitors were also inoperable for greater than six hours.

Description:

On July 25, 2007, the inspectors questioned the adequacy of the testing and maintenance of the RBCU condensate flow detectors, as documented in CR-07-02167. The inspectors noted that a portion of the RBCU condensate drain flow path from the RBCU to the flow detector was being bypassed in the surveillance procedure STP-342.003, Reactor Building Cooling Unit Condensate Flow Detectors IFS01900A and IFS01900B Calibration, Revision 4, which is intended to meet TS SR 4.4.6.1.d. For reference, the as-built RBCU condensate drain 6-inch pipe forms an S-turn P-trap where the TS required flow detector takes a tap through a pipe penetration from the bottom of the P-trap. This 1-inch pipe for the flow detector forms a parallel branch line that re-connects with the main drain pipe downstream of the P-trap. The STP, as mentioned above, performs its calibration by using a calibrated flow through a separate pipe tap on the flow detector branch line.

On October 4, 2007, the licensee entered the Reactor Building to inspect, via borescope, the A-train RBCU condensate drain pipe P-trap pipe penetration for the A-train RBCU condensate flow detector (IFS01900A). The licensee investigation revealed complete blockage of the condensate flow detector pipe penetration with 1-2 inches of hard debris that the initial licensee evaluation states has been there for a significant period of time.

The licensee immediately cleaned the condensate flow detector piping, calibrated the A-train flow detector using the existing STP, and restored compliance with TS 3.4.6.1. The licensee intends on inspecting and/or clean IFS01900B during the upcoming refueling outage in April 2008.

Further review by the inspectors revealed three sources of foreign material have been entering the RBCU condensate drain pipe for a significant period of time. First and as documented in CR-03-03487 and CR-06-03583, the carbon steel frame and cooling coil support structure of the RBCUs above the drain plenum have been experiencing material degradation for a number of years to include paint chipping and streaming rust.

This condition was noted in more than one refueling outage inspection. Also, chemical analysis of the pipe blockage debris within the stainless steel drain pipe revealed ferrous content. The above inspection observations and chemical analysis support that on-line RBCU cooling coil condensation was providing a transport medium into the drain pipe for various corrosion products. Secondly, the on-line RBCU cooling coils act as a natural filter of dirt, debris, and dust within the reactor building over the course of an operating cycle due to the high air flow rates of the RBCUs. The on-line RBCU cooling coil condensation again provides the transport medium for this dirt, dust, and debris into the drain pipe. Finally, Mechanical Maintenance Procedure (MMP) 460.022, Inspection, Cleaning, and Lubrication of Fan Coil Units, Revision 11, provided for the inspection and cleaning of the RBCUs each refueling outage. Steps 7.2.3.C and 7.2.5.B required the cleaning of the cooling coils and draining with pressurized water. As verified by the licensees mechanical maintenance department, foreign material exclusion controls were not provided for these steps as the intent was to flush dirt and debris from the RBCUs down the RBCU condensate drain flow pipe into the reactor building sump.

The inspectors concluded that STP-342.003 was inadequate to demonstrate the leakage detection system operable per TS SR 4.4.6.1.d. Without the ability to perform a channel check for the RBCU condensate flow detector and with multiple sources of known foreign material into the RBCU condensate drain pipe as discussed above, this STP was incapable of verifying the specified function of RBCU flow detector performance throughout the extent of all system components which include the RBCU drain plenum and drain pipe as support and auxiliary equipment.

Analysis:

The licensees failure to implement an adequate surveillance test procedure was a performance deficiency and a finding. This finding was more than minor because it affected the availability, reliability, and maintenance of the barrier integrity equipment performance attribute of the initiating events cornerstone and adversely affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.

With the RBCU condensate flow detector inoperable, coincident with reactor building atmosphere gaseous and particulate radioactivity monitors, the capability of performing the TS, design bases function was lost for a significant period of time. The finding was evaluated using Inspection Manual Chapter 0609, Significance Determination Process, Phase I Worksheet for initiating events. The finding was determined to be of very low safety significance (Green) because at least one method of RCS leak detection (reactor building sump level) was available to the licensee and no actual leakage above one gpm (the TS required limit for RCS unidentified leakage) was indicated through the RCS water balance surveillance test during the reviewed time period. The finding directly involved the cross-cutting area of Human Performance under the Complete Documentation and Component labeling aspect of the Resources component, in that, STP-342.003 failed to test the capability of the system to perform its specified function to include support and auxiliary equipment (H.2.c).

Enforcement:

TS LCO 3.4.6.1, Leak Detection Systems, requires in part that two of the TS required reactor coolant system leakage detection systems be operable. Contrary to the above, for multiple time periods over several years prior to October 4, 2007, the licensee failed to maintain operability of the RBCU condensate flow detector (IFS01900A) coincident with when the reactor building atmosphere gaseous and particulate radioactivity monitors were also inoperable for greater than six hours.

Additionally, the licensee failed to complete the required TS actions. Because this finding is of very low safety significance and has been entered into the corrective action program as CR-07-02167 and CR-07-03332, this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000395/2007005-02, Failure to Maintain Two Required Reactor Coolant System Leak Detection Systems Operable and Complete the Required TS Actions.

1EP4 Emergency Action Level (EAL) and Emergency Plan Changes

a. Inspection Scope

The inspectors in-office review of EP-100, Radiation Emergency Plan, revision 54 and EPP-001, Activation and Implementation of Emergency Plan, revision 29, was performed to determine that changes had not decreased the effectiveness of the plan. The review was conducted between October 31, 2007 to November 14, 2007.

The inspection was conducted in accordance with NRC Inspection Procedure 71114, 04, Emergency Action Level and Emergency Plan Changes. The applicable planning standard, 10 CFR 50.47(b)(4) and its related 10 CFR 50, Appendix E requirements were used as reference criteria. The criteria contained in NUREG-0654, Appendix 1, Emergency Action Level Guidelines for Nuclear Power Plants, Revision 1 and Regulatory Guide 1.101 were also used as references.

b. Findings

The NRC identified a violation related to the licensees implementation of EAL changes which decreased the effectiveness of the Emergency Plan associated with changes in EP-100, Radiation Emergency Plan, revision 54 and EPP-001, Activation and Implementation of Emergency Plan, revision 29. Changes to Emergency Action Level 392A, an aircraft crash into vital structures being experienced or projected with plant not in cold shutdown, resulted in the removal of the Diesel Generator Building and Intermediate Building from the list of vital buildings. Both the Diesel Generator Building and Intermediate Building were included in Revision 53 as vital structures, their removal was a decrease in effectiveness.

This violation constitutes an additional example of violation 05000395/2007502-01 and is not being cited individually. No additional response to violation 05000395/2007502-01 is required. Further corrective actions for this additional example are expected to be taken in conjunction with corrective actions for the previously cited violation.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1 Reactor Safety: Mitigating Systems Cornerstone

a. Inspection Scope

The inspectors verified the accuracy of the licensees PI submittals listed below for the period July 1, 2006, through September 30, 2007. The inspectors used the performance indicator definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, and licensee procedure SAP-1360, NRC and INPO/WANO Performance Indicators, to check the reporting for each data element. The inspectors sampled licensee event reports (LERs),operator logs, plant status reports, CRs, and performance indicator data sheets to verify that the licensee had identified the cumulative safety system unavailability and required hours, as applicable. The inspectors discussed the PI data with licensee personnel associated with performance indicator data collection and evaluation.

  • MSPI - Cooling Water Systems; and,
  • Safety System Functional Failures.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Review of Items Entered into the Corrective Action Program

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. This review was accomplished by either attending daily screening meetings that briefly discussed major CRs, or accessing the licensees computerized corrective action database and reviewing each CR that was initiated.

.2 Semi-Annual Review to Identify Trends

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, the inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The review was focused on repetitive equipment issues, but also considered trends in human performance errors, the results of daily inspector corrective action item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The review nominally considered the six-month period of July 2007 through December 2007. Documents reviewed included licensee monthly and quarterly corrective action trend reports, engineering system health reports, maintenance rule documents, department self-assessment activities, and quality assurance audit reports.

b. Assessment and Observations The inspectors identified two adverse trends, one of which was also independently identified by the licensee, as discussed below.

First, an adverse trend in site personnel human performance errors was identified by the inspectors, as well as by the licensee. The majority of these human performance errors involved personnel in the operations department. Noteworthy examples of these items included: 1) omitted steps in an EDG surveillance procedure for testing the fuel oil system, 2) maintenance personnel failure to properly conduct electrical manhole inspection (NRC identified), 3) inadvertent EDG emergency start due to wrong switch manipulation, 4) failure to implement required dedicated operator compensatory actions during EDG testing (NRC identified and subject of NCV 05000395/2007004-02), and 5)

Failure to Implement TS Required Administrative Controls When Opening Containment Isolation Valves 8767-DN and 8768-DN (NRC identified and subject of NCV 05000395/2007005-01 documented in this report). To address the adverse trend in the number of human performance errors, the licensee conducted a mandatory human performance standdown with all plant personnel on October 18, 2007. In addition, the licensee initiated CR-07-02951 to conduct a common cause evaluation of the issues specific to the operations department adverse trend.

The second adverse trend was noted in the high number of minor fire brigade performance issues identified by the inspectors during observation of fire drills conducted on July 30, September 5, October 31, and November 14, 2007, that were not being captured by the licensee during the associated post drill critiques. The licensee had incorporated the inspectors comments in their corrective action program for each of the observed drills. In addition, the licensee initiated CR-07-03384 to address the noted adverse trend.

.3 Annual Sample Review

a. Inspection Scope

The inspectors reviewed two issues in detail to evaluate the effectiveness of the licensee's corrective actions for important safety issues documented in CR-06-01941 and CR-05-04358. CR-06-01941 was associated with the Operator Work Around of placing one RHR pump in pull-to-lock during plant heatup in Mode 4. CR-05-04358 was associated with heat trace control panel and breaker issues. The inspectors assessed whether the issues were identified; documented accurately and completely; properly classified and prioritized; adequately considered extent of condition, generic implications, common cause, and previous occurrences; adequately identified root causes/apparent causes; and identified appropriate corrective actions. Also, the inspectors verified the issues were processed in accordance with SAP-999, "Corrective Action Program."

b. Findings and Observations

The inspectors identified one weakness with the licensee's documentation and corrective action. Action #7 of CR-05-04358, which was closed as complete on June 29, 2007, committed to ensuring that heat trace preventive maintenance was completed prior to the onset of cold weather each season. The corrective action weakness involved was that both the primary and redundant trains for the safety-related RWST heat trace circuits and one train of the reactor make-up water tank heat trace circuit were incomplete following Operations Department declaration that the plant was aligned and prepared for cold weather per OAP 109.1 during the first week of November 2007. The licensee initiated CR-07-03256 to document this discrepancy.

4OA3 Event Followup

.1 (Closed) LER 05000395/2007002-00 : Failure to Follow Administrative Controls Results

in Limiting Condition for Operation (LCO) 3.6.4 Violation.

The inspectors reviewed the subject LER and applicable condition report (CR-07-02894)associated with the issue to verify the LER accuracy and appropriateness of the specified corrective actions. A detailed review of the issue and cause evaluation was documented in Section 1R13 of this report. The licensees violation of TS 3.6.4 was the subject of NCV 05000395/2007005-01 documented in Section 1R13 of this report. No new findings of significance were identified. This LER is closed.

.2 (Closed) LER 05000395/2007003-00: Clogged Reactor Building Cooling Unit Drain Line

Results in Violation of LCO 3.4.6.1.

The inspectors reviewed the subject LER and applicable condition reports (CR-07-02167 and CR-07-03332) associated with the issue to verify the LER accuracy and appropriateness of corrective actions. A detailed review of the issue and cause evaluation was documented in Section 1R22 of this report. The licensees violation of TS 3.4.6.1 was the subject of NCV 05000395/2007005-02 documented in Section 1R22 of this report. No new findings of significance were identified. This LER is closed.

.3 (Closed) Unresolved Item (URI) 05000395/2007004-01: Review Risk Assessment Credit

for Dedicated Manual Operator Actions During EDG Surveillance Testing.

During a previous plant risk assessment review for routine TS surveillance testing of the EDG, the inspectors noted that dedicated manual operator risk management compensatory actions were being relied upon to allow the EDG to be considered available during portions of the surveillance while key engine components were out of their normal standby alignment. The dedicated operator actions involved repositioning these critical components (i.e., mode selector switch, removal of blocking device for fuel oil stop lever, and closure of cylinder petcock valves) in the event of an EDG emergency start demand. At the time of the earlier inspection, the licensee could not provide documentation that these compensatory actions could be completed within the time necessary for the EDG to satisfy its safety function as assumed in the Probabilistic Risk Assessment (PRA) success criteria.

The inspectors reviewed CR-07-03120 that the licensee initiated to address this issue and discussed the details with licensee PRA personnel. The licensee determined that the limiting design bases event requiring EDG functionality was a reactor coolant pump seal loss-of-coolant accident. Associated with this event, the maximum time available to reposition the associated engine components to ensure EDG availability was determined to be six minutes. Based on this, the inspectors concluded that it was reasonable that the aforementioned operator actions could be accomplished within this timeframe.

Based on the licensees additional information provided, this URI is closed.

4OA6 Meetings, Including Exit

Integrated Report Exit The inspectors presented the inspection results to Mr. Jeffrey Archie and other members of the licensee staff on January 10, 2008. The licensee acknowledged the findings. The inspectors confirmed that inspection activities discussed in this report did not contain proprietary material.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

J. Archie, Vice President, Nuclear Operations
F. Bacon, Manager, Chemistry Services
L. Bennett, Manager, Plant Support Engineering
L. Blue, Manager, Nuclear Training
M. Browne, Manager, Quality Systems
A. Cribb, Supervisor, Nuclear Licensing
G. Douglass, Manager, Nuclear Protection Services
M. Fowlkes, General Manager, Engineering Services
D. Gatlin, General Manager, Nuclear Plant Operations
R. Justice, Manager, Maintenance Services
D. Lavigne, General Manager, Organizational / Development Effectiveness
G. Lippard, Manager, Operations
P. Mothena, Manager, Health Physics and Safety Services
J. Nesbitt, Manager, Materials and Procurement
D. Shue, Manager, Planning / Outage
W. Stuart, Manager, Design Engineering
B. Thompson, Manager, Nuclear Licensing
S. Zarandi, General Manager, Nuclear Support Services

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None.

Opened and Closed

05000395/2007005-01 NCV Failure to Implement TS Required Administrative Controls When Opening Containment Isolation Valves 8767-DN and 8768-DN. (Section 1R13)
05000395/2007005-02 NCV Failure to Maintain Two Required Reactor Coolant System Leak Detection Systems Operable and Complete the Required TS Actions.(Section 1R22)

Closed

05000395/2007002-00 LER Failure to Follow Administrative Controls Results in Limiting Condition for Operation (LCO) 3.6.4 Violation (Section 4OA3.1)
05000395/2007003-00 LER Clogged Reactor Building Cooling Unit Drain Line Results in Violation of LCO 3.4.6.1 (Section 4OA3.2)
05000395/2007004-01 URI Review Risk Assessment Credit for Dedicated Manual Operator Actions During EDG Surveillance Testing (4OA3.3)

Discussed

None.

LIST OF DOCUMENTS REVIEWED