IR 05000387/2016007

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November 23, 2016

Mr. TimothyPresident and Chief Nuclear Officer Susquehanna Nuclear, LLC 769 Salem Blvd - NUCSB3 Berwick, PA 18603-0467

SUBJECT: SUSQUEHANNA STEAM ELECTRIC STATION COMPONENT DESIGN BASES INSPECTION REPORT 05000387/2016007 AND 05000388/2016007

Dear Mr. Rausch:

On October 21, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at the Susquehanna Steam Electric Station (Susquehanna), Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on October 21, 2016, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. In conducting the inspection, the team examined the adequacy of selected components to mitigate postulated transients, initiating events, and design basis accidents. The inspection involved field walkdowns, examination of selected procedures, calculations and records, and interviews with station personnel. This report documents one NRC-identified finding that was of very low safety significance (Green). This finding involved a violation of NRC requirements. Further, the report documents a licensee-identified violation which was determined to be of very low safety significance. The NRC is treating these violations as non-cited violations (NCV) consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Senior Resident Inspector at Susquehanna.

In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for the public inspection in the NRC Public Docket Room or from the Publicly Available Records component of NRC's document system (ADAMS). ADAMS is accessible from the NRC's Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ Mel Gray, Chief Engineering Branch 1 Division of Reactor Safety Docket Nos. 50-387 and 50-388 License Nos. NPF-14 and NPF-22

Enclosure:

Inspection Report 05000387/2016007 and 05000388/2016007

w/Attachment:

Supplementary Information cc w/encl: Distribution via ListServ

SUMMARY

Inspection Report Nos. 05000387/2016007 and 05000388/2016007; 9/19/16 - 10/21/16; Susquehanna Steam Electric Station (Susquehanna), Units 1 and 2; Component Design Bases Inspection. The report covers the Component Design Bases Inspection conducted by a team of four NRC inspectors and two NRC contractors. One finding of very low safety significance (Green) was identified, which was considered to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process." Cross-cutting aspects associated with findings are determined using IMC 0310, "Components Within the Cross-Cutting Areas." The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 5. NRC-Identified Findings

Cornerstone: Mitigating Systems

Green: The team identified a Green non-cited violation of Title 10 of the Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion III, "Design Control," for the failure to classify and maintain reactor core isolation cooling (RCIC) system components as safety-related as specified by Updated Final Safety Analysis Report Table 3.2-1 and Section 7.1.1. Specifically, although Talen, the operator of Susquehanna Steam Electric Station, classified the RCIC system as safety-related, this classification did not extend to the Unit 1 and Unit 2 RCIC barometric condenser relief valves. The team determined failure of the non-safety related barometric condenser relief valves could result in a loss of RCIC lube oil cooling and failure of RCIC to perform its design basis safety function. Talen entered the issue into the corrective action program as condition report 2016-23615 and performed an immediate operability determination, which concluded RCIC remained operable. The finding was more than minor because it was associated with the Design Control attribute of the Mitigating Systems cornerstone, and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The team evaluated this finding using IMC 0609, Attachment 4, "Initial Characterization of Findings," and IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," Exhibit 2 - Mitigating System Screening Questions. The team determined the finding screened as very low safety significance (Green), because the finding was a design deficiency which did not result in an actual loss of functionality of the RCIC system. This finding was not assigned a cross-cutting aspect because the performance deficiency occurred during original plant design and did not reflect current licensee performance. (Section 1R21.2.1.1)

Other Findings

A violation of very low safety significance, which was identified by the licensee, has been reviewed by the team. Corrective actions taken or planned by the licensee have been entered into the corrective action program. This violation and the licensee's corrective action tracking numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R21 Component Design Bases Inspection (IP 71111.21)

.1 Inspection Sample Selection Process

The team selected risk significant components for review using information contained in the Susquehanna Probabilistic Risk Assessment (PRA) model and the U. S. Nuclear Regulatory Commission's (NRC) Standardized Plant Analysis Risk (SPAR) model for Susquehanna Steam Electric Station (Susquehanna), Units 1 and 2 operated by Talen Energy Company (Talen). Additionally, the team referenced the Plant Risk Information e-Book (PRIB) for Susquehanna in the selection of potential components for review. In general, the selection process focused on components that had a Risk Achievement Worth (RAW) factor greater than 1.3 or a Risk Reduction Worth (RRW) factor greater than 1.005. The components selected were associated with both safety-related and non-safety related systems, and included a variety of components such as pumps, fans, heat exchangers, diesel engines, batteries, motor control centers, circuit breakers, and valves.

The team initially compiled a list of components based on the risk factors previously mentioned. Additionally, the team reviewed the previous component design bases inspection (CDBI) reports and excluded components previously inspected. The team then performed a margin assessment to narrow the focus of the inspection to 17 components, 2 time-critical operator actions, and 3 operating experience (OE) items. The team selected the 416 A/B drywell coolers/fans and an automatic depressurization system valve to review for large early release frequency (LERF) implications. The team's evaluation of possible low design margin included consideration of original design issues, margin reductions due to modifications, or margin reductions identified as a result of material condition/equipment reliability issues. The assessment also included items such as failed performance test results, corrective action history, repeated maintenance, Maintenance Rule (a)(1) status, operability reviews for degraded conditions, NRC resident inspector insights, system health reports, and industry OE. Finally, consideration was also given to the uniqueness and complexity of the design and the available defense-in-depth margins.

The team performed the inspection as outlined in NRC Inspection Procedure (IP) 71111.21. This inspection effort included walkdowns of selected components; interviews with operators, system engineers, and design engineers; and reviews of associated design documents and calculations to assess the adequacy of the components to meet design basis, licensing basis, and risk-informed beyond design basis requirements. Summaries of the reviews performed for each component and OE sample are discussed in the subsequent sections of this report. Documents reviewed for this inspection are listed in the Attachment.

.2 Results of Detailed Reviews

.2.1 Results of Detailed Component and Critical Operator Action Reviews (19 samples)

.2.1.1 Unit 1, Reactor Core Isolation Cooling Injection Valve (HV-149-F013)

a. Inspection Scope

The team inspected the Unit 1 reactor core isolation cooling (RCIC) injection valve to verify the capability of the equipment to perform its safety function of opening to provide RCIC injection under design basis transient conditions and closing, when required, for containment isolation. The team reviewed applicable portions of technical specifications (TS), the updated final safety analysis report (UFSAR), and the RCIC design basis document (DBD) to identify design basis requirements. The team interviewed design, system, and component engineers to verify the safety functions of the valve and associated RCIC system. The team reviewed safety classifications of the valve, as well as, other equipment associated with the RCIC system, to verify equipment was appropriately classified. The team verified the electrical power supply of the valve to verify the equipment's capability of operating under transient and accident conditions. The team inspected motor-operated valve (MOV) thrust and weak link calculations to verify the capability of the valve to open and close under the most limiting design conditions. The team inspected the valve control logic to verify that the RCIC system would not be subjected to damaging water hammer conditions under transient conditions. The team performed in-plant walkdowns and also inspected photographs of the valve to verify the configuration and material condition of the equipment. The team reviewed a sample of RCIC system condition reports (CR), the RCIC system health report, and applicable test results to determine if there were any adverse operating trends and to ensure that station personnel adequately identified and addressed any adverse conditions.

b. Findings

Introduction.

The team identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to classify and maintain RCIC system components as safety-related as specified by UFSAR Table 3.2-1 and Section 7.1.1. Specifically, although the licensee classified the RCIC system as safety-related, this classification did not extend to the Unit 1 and Unit 2 RCIC barometric condenser relief valves. Failure of the non-safety related barometric condenser relief valves could result in a loss of RCIC lube oil cooling and failure of RCIC to perform its design basis safety function.

Description.

Susquehanna UFSAR Table 3.2-1 and Section 7.1.1 document that RCIC is a safety-related system; specifically a Safe Shutdown system. The design bases function (UFSAR Sections 7.1.2 and 7.4.1) is to assure sufficient reactor water inventory is maintained in the reactor vessel, thus assuring continuity of core cooling when the reactor vessel is isolated and accompanied by a loss of normal coolant flow from the reactor feedwater system. UFSAR Section 3.2.2 states that quality group classifications, as defined in NRC Regulatory Guide 1.26, were determined for each component of those fluid systems relied upon to provide safe shutdown capability of the reactor and maintain it in a safe shutdown. NRC Regulatory Guide 1.26 described a method for determining acceptable quality standards for safety-related components.

Major portions of the RCIC system (i.e., turbine, pump, injection piping and valves, turbine steam supply piping and valves) were correctly specified, tested, and maintained as safety related. The team noted, however, that the RCIC barometric condenser and associated components were classified as non-safety related. The team reviewed the function of the RCIC barometric condenser components and determined the RCIC barometric condenser relief valves (PSV105F033 for Unit 1 and PSV205F033 for Unit 2), should have been classified as safety-related. Specifically, the relief valves would be required to function to establish an alternate flow path for the RCIC lube oil cooling water exhaust if the non-safety related barometric condenser condensate pump was not available. If a relief valve failed to open, this alternate flow path for the lube oil cooling water discharge would not be available, resulting in loss of lubrication and damage to the RCIC pump and turbine. The RCIC system would therefore not be capable of performing its Safe Shutdown design bases function.

The non-safety related relief valves did not receive the same quality control as safety-related components, were not procured as safety-related, and were not subject to periodic in-service testing or preventative maintenance. The most recent relief valve preventative maintenance was completed in 1996 (Unit 1) and 1997 (Unit 2). In response to the team's concerns, the licensee performed an immediate operability determination and initiated CR 2016-23615 to resolve the issue. Based on reliable RCIC barometric condenser operation during periodic RCIC flow tests, operators determined RCIC remained operable, but degraded (non-conforming). The team concluded this determination was technically sound.

Analysis.

The licensee's failure to adequately classify the RCIC barometric condenser relief valves as safety-related based on their supporting safety function, in accordance with RG 1.26 as specified by UFSAR Table 3.2-1 and Sections 3.2.2 and 7.1.1 was a performance deficiency. The performance deficiency was more than minor because it was associated with the Design Control attribute of the Mitigating Systems cornerstone, and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the inadequate classification of the relief valves affected the reliability of safety-related function of the RCIC system. The team evaluated this finding using IMC 0609, Attachment 4, "Initial Characterization of Findings," and IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," Exhibit 2 - Mitigating System Screening Questions. The team determined the finding to be of very low safety significance (Green), because the finding was a deficiency affecting the design or qualification of a mitigating SSC, and the SSC maintained its operability or functionality. This finding was not assigned a cross-cutting aspect because the performance deficiency occurred during original plant design and did not reflect current licensee performance.

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires, in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, are correctly translated into specifications, drawings, procedures, and instructions. These measures shall include provisions to assure that appropriate quality standards are specified and included in design documents and that deviations from such standards are controlled. Measures shall also be established for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the structures, systems and components. The Susquehanna UFSAR Table 3.2-1 and Section 7.1.1 stated that the RCIC system was safety related.

As of October 21, 2016, the licensee had not established adequate design control measures to assure appropriate quality standards were specified and included in design documents, and to ensure suitability of application of materials essential to the safety-related function of the Unit 1 and Unit 2 RCIC barometric condenser relief valves. Specifically, the licensee did not classify the barometric condenser relief valves as safety-related and consequently the valves were not procured, tested, or maintained to the standards required for safety-related components. Operators determined RCIC was operable based on its successful quarterly surveillance tests. In addition, the RCIC drain pumps are powered from a safety-related battery system so the pumps would have reasonable assurance of operating in an event including a postulated loss of offsite power. The relief valves were purchased as ASME Section VIII. The valves were last tested in 1996 (Unit 1) and 1997 (Unit 2). Because this violation is of very low safety significance (Green) and was entered into the licensee's corrective action program as CR 2016-23615, this violation is being treated as a NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy. (NCV 50-387 (388) 2016-07-01, Failure to Specify and Maintain Safety-Related Quality Standards and Materials Essential for Reactor Core Isolation Cooling)

.2.1.2 'C' Emergency Diesel Generator (Mechanical Review) (0G-501C)

a. Inspection Scope

The team inspected the 'C' emergency diesel generator (EDG) and its associated subsystems including the fuel oil, lube oil, starting air, intake and exhaust, jacket water cooling systems and ventilation room to ensure they could perform their respective design basis function in response to transient and accident events, including a loss of offsite power (LOOP). The team reviewed the UFSAR, TSs, design basis calculations, vendor documents, and procedures to identify the design basis, maintenance, and operational requirements for the engine and its support systems. The team reviewed the design specification for the starting air system, as well as air start test results, the normal operating pressure band, air compressor actuation setpoint and the technical specification (TS) limit for operability to verify that the starting air system was properly sized and could meet its design function for successive starts. The team reviewed EDG surveillance test results, operating procedures and maintenance work packages to determine the overall health of the EDG engine and its mechanical support systems. The team performed several field walkdowns of the 'C' EDG to independently assess the material condition and the operating environment of the EDG and associated electrical equipment. During the walkdowns, the team compared local and remote EDG control switch positions, breaker position indicating lights, and system alignments to design and licensing basis assumptions to verify configuration control adequacy. The team interviewed system engineers and operators to evaluate past performance and operation of the EDGs. The team reviewed system health reports and corrective action documents to determine if there was any adverse equipment operating trends and to ensure problems were properly identified and corrected.

b. Findings

No findings were identified.

.2.1.3 Unit 1, 416 A/B Drywell Coolers/Fans (1V-416A/B)

a. Inspection Scope

The team inspected the Unit 1 drywell coolers and fans to verify the capability of the equipment to perform its safety function of circulating air in the drywell under post-accident conditions. The team reviewed system health reports and corrective action documents to determine if there were any adverse equipment operating trends and to ensure problems were properly identified. The team interviewed design and system engineers and reviewed past fan failures to verify the adverse condition had been corrected. The team reviewed safety and seismic classifications of fans to verify the equipment were appropriately classified. The team reviewed surveillance test results and verified the electrical power supply and control logic of the non-safety related and safety related fans to verify the equipment's capability of starting and operating under accident conditions. The team also reviewed system drawings and operating procedures, and performed a walkdown of associated control room instrumentation to assess configuration control.

b. Findings

No findings were identified.

.2.1.4 Unit 1, 'A' Control Structure Chiller (0K-112A)

a. Inspection Scope

The team inspected the 'A' control structure chiller (0K-112A), which is common to both Susquehanna Units 1 and 2, to verify that it was capable of performing its design basis function. The control structure chiller is a refrigerant-based heat exchanger that provides chilled water to various cooling coils in the control room, control structure, computer room, and also the Unit 1 emergency switchgear room cooler under all plant conditions. This chilled water aids these building and room coolers to maintain the air temperature below design limits in order to ensure reliable operation of the safety-related equipment located in these areas. The team reviewed applicable portions of Susquehanna's TSs, the UFSAR, and the control structure heating ventilation and cooling DBD to identify design basis requirements for 0K-112A. The team reviewed the chiller design calculations and drawings to evaluate the ability of the chiller to provide adequate cooling to the various building and room coolers that it supported. The team reviewed the inspection and testing results, which included eddy current testing of the chiller tube bundle and visual inspection of the tubes and end bells, to verify that cleanliness and tube structural integrity were being maintained. The team also reviewed the results of completed chiller thermal performance tests and emergency service water (ESW) flow balancing to verify that the chiller was capable of removing the design basis heat load. Additionally, the team reviewed preventative maintenance and monitoring of the chiller and its subcomponents to verify that plant staff were adequately maintaining the chiller in an appropriate condition to perform its design function. The team reviewed procedures to verify that the actions specified during a failure of the chiller system could be performed and were in agreement with the control structure and room heat up calculations. The team also reviewed the breaker relay rating and setpoint calculation to verify that the chiller would remain functional during start-up, operation, and abnormal operational events.

The team interviewed engineers regarding the maintenance and operation of the system and reviewed a sample of associated CRs, system health reports, and technical evaluations to determine if there were any adverse operating trends and to ensure that Talen adequately identified and corrected any adverse conditions. The team performed walkdowns of the accessible portions of the chiller, the chiller subcomponents, and associated piping the control structure building to assess the material condition, operating environment, and configuration control.

b. Findings

No findings were identified.

.2.1.5 Unit 1, 'A' Emergency Switchgear Room Cooler/Fan (1E-257A and 1V-222A)

a. Inspection Scope

The team inspected the 'A' emergency switchgear room cooler (1E-257A) and associated fan (1V-222A) to verify that they were capable of performing their design function. Specifically, the cooler and fan maintain the temperature in the 4 kV emergency switchgear and load center rooms during normal and emergency plant operation in order to ensure reliable operation of the safety-related equipment located in these rooms. The team reviewed applicable portions of Susquehanna's TSs, the UFSAR, and the reactor building heating ventilation and cooling DBD to identify design basis requirements for 1E-257A and 1V-222A.

The team reviewed design calculations and drawings to evaluate the ability of the equipment to provide adequate cooling to the safety-related switchgear and load centers. The team reviewed inspection, testing, and calibration procedures and work orders to verify appropriate preventive maintenance was performed. The team also reviewed past test results of the fan flow rate and trend of cooler coil performance to verify that the unit was capable of removing the required design heat load. Additionally, the team reviewed procedures and completed tests to verify that both automatic and manual actions specified during a failure of the system could be performed and were in agreement with the various room heat up calculations. The team interviewed engineers regarding the maintenance and operation of the system and reviewed a sample of associated CRs, system health reports, and technical evaluations to determine if there were any adverse operating trends and to ensure that Talen adequately identified and corrected any adverse conditions. The team also performed walkdowns of the accessible portions of the emergency switchgear room cooler, fan, and exhaust/intake ductwork in the reactor building to assess the material condition, operating environment, and configuration control.

b. Findings

No findings were identified.

.2.1.6 Unit 1, 'G' Automatic Depressurization And Safety/Relief Valve (PSV-141-F013G)

a. Inspection Scope

The team inspected the Unit 1, automatic depressurization system/safety relief valve (ADS/SRV) PSV-141-F013G to verify that it was capable of meeting the design basis function. The team reviewed the UFSAR, drawings, procedures, the vendor manual, and environmental qualification design requirements to identify the design basis requirements of the valve. Design calculations and system operating parameters were reviewed to verify that the design basis had been appropriately translated into specifications and procedures. The team reviewed test procedures to verify that acceptance criteria for the tested parameters were appropriately supported by calculations and to ensure the design and licensing bases were satisfied.

The team interviewed the valve program engineer and the ADS/SRV system engineer to review maintenance issues and assess the overall reliability of the valve and associated safety components. Because the valve was inaccessible during the inspection period, the team reviewed photographs of the valve to assess the general material condition of the valve and to verify the installed valve configuration was consistent with design basis assumptions and plant drawings. Finally, corrective action documents, preventive maintenance documents, and system health reports were reviewed to verify that deficiencies were appropriately identified and resolved, and to assess the overall performance of the ADS/SRVs. The team performed a visual examination of all accessible ADS control cabinets and control switches in the main control room, the alternate shutdown panel, and the emergency switch gear room to assess material condition, the operating environment, and configuration control.

b. Findings

No findings were identified.

.2.1.7 Unit 2, Main Turbine Bypass Valve #4 (XV-201-40D)

a. Inspection Scope

The team inspected the Unit 2 main turbine bypass valve #4 to verify the capability of the equipment to perform its required function of opening under transient conditions. The team interviewed design and system engineers to discuss the operating history and preventive maintenance of the valve and associated equipment, including hydraulic oil, to verify reliable equipment operation. The team also inspected operating and test procedures associated with the valve to verify operation in accordance with the system design. The team reviewed vendor documentation and work orders to verify appropriate preventive maintenance and testing were performed. The team also reviewed a sample of associated CRs, system health reports, and technical evaluations to determine if there were any adverse operating trends and to ensure that Talen adequately identified and corrected adverse conditions. The team reviewed system drawings and operating procedures, and performed walkdowns of associated control room instrumentation to verify configuration was properly controlled.

b. Findings

No findings were identified.

.2.1.8 Unit 2, High Pressure Coolant Injection Pump And Turbine (2P-204 and 2S-211)

a. Inspection Scope

The team inspected the Unit 2 high pressure coolant injection (HPCI) pump and turbine to verify the capability of the equipment to perform its safety function of providing HPCI injection flow under design basis transient and accident. The team interviewed design, system, and component engineers and performed walkdowns to verify the material condition, operating environment, and configuration of the pump, turbine, and associated equipment. The team verified the periodic test procedures and recent test results associated with the pump and turbine to verify the equipment's capability to perform as required under the most limiting conditions. The team reviewed HPCI system calculations to verify the capability of the pump to provide the required flow under the design bases conditions.

The team inspected the valve control logic to verify that the HPCI system would not be subjected to damaging pressure transients (i.e., water hammer) and verified the periodic testing of system valve interlocks. The team evaluated the capability of the pump and turbine to start and deliver flow within the required time during periodic operation of the HPCI auxiliary oil pump. The team also evaluated potential overpressure of HPCI pump discharge piping as a result of postulated turbine overspeed conditions. Finally, the team reviewed system health reports and corrective action documents to determine if there were adverse equipment operating trends and to ensure problems were properly identified and corrected.

b. Findings

No findings were identified.

.2.1.9 Unit 2, High Pressure Core Injection Valve (HV-255-F006)

a. Inspection Scope

The team inspected the Unit 2, HPCI injection valve, HV-255-F006, to verify that the valve was capable of performing its safety function. The team reviewed the UFSAR, drawings, and procedures to identify the design basis requirements of the valve. Design calculations and system operating parameters were reviewed to verify that the design basis had been appropriately translated into specifications and procedures. The team reviewed test procedures to verify that acceptance criteria for the tested parameters were appropriately supported by calculations to ensure the design and licensing bases were satisfied. The team verified that the thermal overload bypass circuitry was appropriately tested to ensure MOV operation during a design basis event.

The team interviewed the MOV program engineer and the HPCI system engineer to review maintenance issues and assess overall reliability of the valve and the associated motor operator. Because the valve was inaccessible during the inspection period, the team reviewed photographs of the valve to assess the material condition of the valve and to verify the installed valve configuration was consistent with design basis assumptions and plant drawings. Finally, corrective action documents, preventive maintenance, and system health reports were reviewed to verify that deficiencies were appropriately identified and resolved.

b. Findings

No findings were identified.

.2.1.1 0 Unit 2, 'A' Residual Heat Removal Pump (2P-202A)

a. Inspection Scope

The team inspected the Unit 2 'A' residual heat removal (RHR) pump to verify that it was capable of meeting its design basis requirements. The team reviewed applicable portions of the UFSAR, TS, RHR system DBD, and drawings to identify the design basis requirements for the pump. The team reviewed calculations and surveillance test procedures to verify that the pump was capable of achieving design basis head/flow requirements during limiting design basis conditions, including postulated variations in emergency diesel generator frequency and voltage. The team also verified test acceptance criteria were consistent with these requirements.

The team interviewed design, system, and component engineers and performed walkdowns to verify the configuration and material condition of the pump and associated equipment, and to verify the equipment's protection from internal flooding and seismic interactions. The team also verified the capability of the RHR pump to provide injection flow in the event of an accident while the RHR was in shutdown cooling operation. In addition, the team reviewed a sample of CRs, work orders, and corrective action documents to identify failures or nonconforming issues, and to determine if deficiencies were being appropriately identified, evaluated, and corrected.

b. Findings

No findings were identified.

.2.1.1 1 Unit 1, 'A' Residual Heat Removal Heat Exchanger Service Water Inlet Valve (HV-112-10A)

a. Inspection Scope

The team inspected the 'A' RHR heat exchanger service water inlet valve (HV-112-10A) to verify that it was capable of performing its design function. The team reviewed applicable portions of Susquehanna's TSs, the UFSAR, and the RHR system DBD to identify design basis requirements for HV-112-10A. The normally closed inlet valve has a safety function in the open position to provide cooling water to the RHR heat exchanger in support of RHR System operation during normal plant operation, transients, and following any credible accident, including the design basis loss of coolant accident (LOCA).

The team reviewed design calculations, including the seismic and weak link analysis, valve specifications, and the operating history to verify that the valve met its design basis requirements. The team reviewed a sample of surveillance test results and a trend of in-service test (IST) data to verify that valve performance met the acceptance criteria and that the criteria were consistent with the design basis. The team also reviewed the thermal overload relay sizing calculation and completed relay trip tests to verify that the valve functionality would not be adversely affected. The team interviewed the system engineer and reviewed MOV diagnostic test results and trending to assess valve performance capability, design margin, and overall reliability.

The team reviewed a sample of related CRs, technical evaluations, the RHR system health report, preventive maintenance records, and applicable test results to determine if there were any adverse operating trends and to ensure that Talen adequately identified and corrected adverse conditions. The team also performed a walkdown of the valve, adjacent areas, and accessible portions of the connected system piping to assess the material condition, operating environment, and configuration control.

b. Findings

No findings were identified.

.2.1.1 2 Operator Action to Open Emergency Safeguards Service Water Pump House Doors for Residual Heat Removal Service Water Ventilation

a. Inspection Scope

The team reviewed manual operator actions to block open the emergency safeguards service water (ESSW) pump house doors and exhaust dampers in the event the pump room temperature becomes elevated due to ventilation fan failure. The ESSW pump house heating and ventilation system is designed to maintain a suitable environment for the ESW and residual heat removal service water pumps and their associated accessories. The team reviewed the associated operating procedures and loss of ventilation calculation to verify that selected operator actions could be accomplished. The team interviewed licensed operators, reviewed associated alarm response procedures, and observed a licensed operator simulate performance of selected operating procedures to independently assess the likelihood of cognitive or execution errors. The team evaluated the available time margins to perform the actions and verified the validity of procedure assumptions. The team also performed walkdowns of the pump house and required ventilation paths to ensure components were accessible and available to complete the necessary actions. Finally, the team reviewed corrective action documents and system health reports to evaluate whether there were any related adverse operating trends and to assess Talen's ability to evaluate and correct problems.

b. Findings

No findings were identified.

.2.1.1 3 Operator Action to Cross-Tie Refueling Water Storage Tank to Condensate Storage Tank with Transfer Pumps

a. Inspection Scope

The team evaluated the manual operator actions to transfer water from the refueling water storage tank (RWST) to the condensate storage tank (CST) using the cross-tie piping and valves and the associated transfer pumps. The team interviewed licensed and non-licensed operators, reviewed associated operating procedures and operator training, and observed an in-field operator perform a simulated RWST cross-tie to the CST per station procedure OP-037-003, Transferring Inventory from Refueling Water Storage Tank to CST A (B) or CST A (B) to RWST Using Intertie, Revision 30, to evaluate the operators' ability to perform the required actions.

In addition, the team walked down the RWST and CST and associated piping, pipe supports, and valves associated with the transfer to assess the material condition of the components and the likelihood of cognitive or execution errors. The team evaluated the available time margins to perform the actions to verify the reasonableness of the operating procedures and risk assumptions.

b. Findings

No findings were identified.

.2.1.1 4 'C' Emergency Diesel Generator (Electrical Review) (0G-501C)

a. Inspection Scope

The team inspected the adequacy of voltage at selected diesel starting and generator operating control components (generator field, field flash controls, starting air solenoids, and generator breaker closure circuit) for LOOP, LOCA/LOOP, and for recovery from station blackout (SBO) conditions. The team reviewed a modification for the starting air solenoid for the adequacy and implementation of design basis requirements. The team reviewed the preventive maintenance (PM) template and the PMs performed on the above components for adequacy, issues identified, and the effectiveness of corrective actions. The team reviewed the corrective maintenance and CR history on the above components to identify recurring issues affecting reliability and to evaluate whether plant staff adequately identified and corrected any adverse conditions. The team also inspected the diesel loading and load margin analyses and the EDG operating procedures to verify whether load limitations were adequately addressed. The team reviewed EDG surveillance test results, especially periodic load testing, endurance testing, and LOCA/LOOP load testing for conformance with Technical Specifications. The team inspected the EDG during a walkdown to assess material condition, verify equipment configuration, and to identify conditions that could affect the reliable operation of the generator operating and diesel starting control components.

b. Findings

No findings were identified.

.2.1.1 5 Unit 1, Automatic Depressurization System (ADS) Permissive Logic Circuit

a. Inspection Scope

The team inspected the calibration test results for the controls for ADS valve solenoids (level, pressure, pump status, timer) for adequacy, issues identified, and corrective actions. The team reviewed a modification for the ADS solenoid valve circuit for adequacy and implementation of design basis requirements. The team reviewed surveillance test results on the ADS controls for conformance with technical specifications. The team reviewed the PM template for the ADS solenoids and the PMs performed for adequacy, issues identified, and the effectiveness of corrective actions. The team reviewed the corrective maintenance and CR history for the ADS solenoids and control components to identify recurring issues affecting reliability and to evaluate whether plant staff adequately identified and corrected adverse conditions. The team reviewed ADS solenoid molded case circuit breaker (MCCB) preventive maintenance to assure reliable containment penetration conductor overcurrent protection.

b. Findings

No findings were identified.

.2.1.1 6 Unit 2, 'A' Recirculation Pump Trip Breakers 3A and 3B (2A-20501 and 2A-20502)

a. Inspection Scope

The team inspected the adequacy of the trip breaker rating for design basis load conditions. The team also inspected the adequacy of breaker overcurrent trip relay settings for the adequacy of penetration conductor protection. The breaker overcurrent relay calibration test results were reviewed for adequacy, issues identified, and corrective actions. The team reviewed a modification that replaced the trip breakers for adequacy and implementation of design basis requirements. The team reviewed the PM template for the breakers, PMs performed, and the calibration test results for the overcurrent relays to assess maintenance adequacy, issues identified, and corrective actions. The team performed an in-plant walkdown of trip breakers 3A and 4A to assess the observable material condition, operating environment, and configuration control and to identify conditions that could affect the reliable operation of the breakers. The team reviewed the corrective maintenance and CR history on the above components for recurring issues affecting reliability and to evaluate whether problems were properly identified, characterized, and corrected.

b. Findings

No findings were identified.

.2.1.1 7 Unit 2, 'A' 4kV Emergency Safety System Electrical Bus (2A-202)

a. Inspection Scope

The team reviewed design specifications, one-line diagrams, calculations, design basis descriptions, the UFSAR, vendor manuals, drawings, and the loading requirements to evaluate the capability of the 4 kilovolt (kV) bus to supply the design bases voltage and current requirements to one train of emergency safety system (ESS) loads. The team reviewed calculations of short circuit, voltage drop, and bus and feeder protective relay trip settings to verify the bus ratings were not exceeded and the bus and feeder relays were appropriately coordinated for normal and sequenced accident loading conditions. Specifically, the team evaluated whether the bus was capable of transferring supplied power to downstream loads during a design bases accident. The team also reviewed switchgear protective device settings and breaker ratings to ensure that selective coordination was adequate for the protection of connected equipment during short-circuit conditions.

The team reviewed the results of completed 4160 VAC Bus 2A-202 preventive maintenance to verify the test results were within acceptable limits. The loss of voltage and degraded voltage relay settings were also reviewed to verify they satisfied the requirements of TS 3.8.1. The team performed walkdowns of the 4KV ESS Bus 2A-202 to verify equipment alignment was consistent with design drawings and to assess observable material conditions and potential vulnerability to hazards. The team reviewed equipment room operating temperatures to confirm equipment capabilities to operate reliably within ambient conditions present in the space.

The team reviewed high impedance grounding features of this power distribution system to verify available ground fault alarm indications and the arrangement of the feeder transformer windings (delta-wye) to rule out any possibility of higher voltage scenarios that may affect loads connected to this distribution bus. Finally, the team reviewed corrective action documents and system health reports to evaluate whether there were adverse operating trends and to assess Talen's ability to identify, evaluate, and correct problems.

b. Findings

No findings were identified.

.2.1.1 8 Unit 2, 'B' 125 Volt Battery (2D-620)

a. Inspection Scope

The team inspected 125VDC station battery 2D620, feeding into Unit 2 Load Center 2D622 and emergency safety system distribution panels (2D624 and 2D625) to evaluate whether it was capable of meeting its design basis requirements. The team reviewed vendor manuals, surveillance documentation, one-line diagrams, calculations, component manuals, maintenance procedures, testing reports and procedures, and design basis documents. The team reviewed calculations and drawings including voltage drop calculations, short circuit analyses, and load study profiles to evaluate the adequacy and appropriateness of testing procedures and design assumptions. The team also reviewed the direct current (DC) overcurrent protective coordination studies to evaluate whether there was adequate protection for postulated faults in the DC system. Additionally, the team reviewed maintenance procedures and schedules for the 125Vdc panel and associated circuit breakers to determine whether the equipment was being maintained in accordance with vendor recommendations. The team interviewed system and design engineers and walked down the 125Vdc distribution panels to independently assess its material condition and to determine whether the system alignment and operating environment was consistent with design basis assumptions. Finally, the team reviewed corrective action documents and system health reports to determine whether there were adverse operating trends and to assess Talen's ability to identify, evaluate, and correct problems.

b. Findings

No findings were identified.

.2.1.1 9 Unit 2, 'D' 125 Volt Battery Charger (2D-623)

a. Inspection Scope

The team inspected the battery charger to verify its sizing would satisfy the requirements of the risk significant DC loads and that the minimum voltage was taken into account. Specifically, the evaluation focused on verifying that the battery charger was adequate to supply the design duty cycle of the 125 VDC system for the LOCA/LOOP and SBO loading scenarios, and that adequate voltage would remain available for the individual load devices required to operate during a four-hour SBO coping duration. The team reviewed vendor manuals, surveillance documentation, one-line diagrams, calculations, component manuals, maintenance procedures, capacitor replacement procedures, testing reports and procedures, and design basis documents.

The team also reviewed short circuit fault duty, verified breaker trip setting calculations, and verified protection coordination. In addition, a walkdown was performed to visually inspect the physical condition of the battery and battery chargers, verify the charger was properly aligned, and verify the charger panel indicated acceptable voltage and current. The team reviewed the maintenance history, including capacitor replacement, to verify applicable industry operating experience had been incorporated into the battery charger maintenance program. The team interviewed design and system engineers to determine design aspects and operating history for the battery charger. The team reviewed battery charger surveillance test results to verify that applicable test acceptance criteria and test frequency requirements specified for the battery were met. Finally, the team reviewed corrective action documents and system health reports to determine whether there were any adverse operating trends and to assess Talen's ability to identify, evaluate, and correct problems.

b. Findings

No findings were identified.

.2.2 Review of Industry Operating Experience (OE) and Generic Issues (3 samples)

The team reviewed selected OE issues for applicability at Susquehanna. The team performed a detailed review of the OE issues listed below to verify Talen staff had appropriately assessed potential applicability to site equipment and initiated corrective actions when necessary.

.2.2.1 NRC Information Notice (IN) 2010-23, Malfunctions of Emergency Diesel Generator Speed Switch Circuits

a. Inspection Scope

The team assessed Talen's applicability review and the disposition of corrective actions identified during the OE review performed for NRC Information Notice (IN) 2010-23. The NRC issued this generic communication to inform licensees about OE involving conditions that caused malfunctions of diesel speed switch circuits, due to electrical noise on the DC power supply to the speed switch, which rendered EDGs inoperable. The team assessed Talen's evaluation of the IN to confirm that an adequate review and assessment of the issue was performed. The team interviewed electrical design and system engineering personnel responsible for the implementation of preventive maintenance for power supplies that could cause electrical noise on the speed switch circuits to evaluate and confirm the effectiveness of corrective actions.

b. Findings

No findings were identified.

.2.2.2 NRC Information Notice 2013-17, Significant Plant Transient Induced by Safety-Related Direct Current Bus Maintenance at Power

a. Inspection Scope

The team assessed Talen's applicability review and disposition of NRC Information Notice 2013-17 to evaluate whether Talen's review adequately addressed the industry operating experiences discussed in the information notice. Specifically, the team reviewed Talen's evaluation to ensure the review addressed proper overcurrent device coordination under short-circuit conditions, proper precautions during live bus maintenance, and adequate evaluation of the risks associated with this type of work for plant safety. Additionally, the team reviewed maintenance program procedures and interviewed plant staff regarding controls for energized bus maintenance to evaluate and confirm the effectiveness of corrective actions.

b. Findings

No findings were identified.

.2.2.3 NRC Information Notice 2012-16, Preconditioning of Pressure Switches Before Surveillance Testing

a. Inspection Scope

The team assessed Talen's applicability review and disposition of NRC IN 2012-16. This generic communication discussed nuclear industry issues involving technical specification-required surveillance testing using procedures that unacceptably preconditioned pressure switches associated with various safety related functions. The team reviewed CR-1616182 which evaluated Susquehanna's applicability to this condition, the UFSAR, the TSs, and the associated instrument calibration sheets for selected pressure switches that were identified by Talen staff as potentially affected by this IN. The team performed field walkdowns to assess the condition of the selected instruments and associated tubing. The team verified that Talen had appropriately evaluated the operational experience, performed engineering evaluations, and implemented corrective actions including procedural changes to ensure that no unacceptable preconditioning of pressure switches occurred.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems (IP 71152)

a. Inspection Scope

The team reviewed a sample of problems that Talen had previously identified and entered into the corrective action program (CAP). The team reviewed these issues to verify an appropriate threshold for identifying issues and to evaluate the effectiveness of corrective actions. In addition, the team reviewed CRs written on issues identified during the inspection to verify adequate problem identification and incorporation of the problem into the CAP.

The specific corrective action documents that the team sampled and reviewed are listed in the Attachment.

b. Findings

No findings were identified.

4OA6 Meetings, including Exit

On October 21, 2016, the team presented the inspection results to Mr.Timothy Rausch, President and Chief Nuclear Officer, and other members of the Susquehanna staff. The team verified that no proprietary information was retained by the team or documented in the report.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by Talen personnel and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for being dispositioned as a non-cited violation. Title 10 of the Code of Federal Regulations (10 CFR), Part 50, Appendix B, Criterion XVI, "Corrective Actions," requires measures to be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to 10 CFR 50, Appendix B, Criterion XVI, station personnel did not promptly correct a condition adverse to quality. Specifically, from August 1, 2013 to February 26, 2016, Talen did not implement corrective actions to establish a PM program for molded case circuit breakers (MCCBs) found in distribution control panels that protect containment penetration conductors. The need for a MCCB PM program was originally identified during the 2013 NRC CDBI and documented as NCV 05000387 (05000388)/2013010-01, Failure to Verify Operation of Safety-Related 125Vdc Molded Case Circuit Breakers (CR 1732454).

Talen identified this untimely implementation of corrective action during a self-assessment in preparation for the 2016 NRC CDBI. Plant staff entered the issue into the corrective action program (CRs 2016-04833; 23373; 23971 and 24015) and established a MCCB PM program. The team evaluated this finding using IMC 0609.04, "Initial Characterization of Findings," and IMC 0609, Appendix A, Exhibit 3, "Barrier Integrity Screening Questions." The team determined that the finding was of very low safety significance (Green) because the finding did not represent an actual open pathway in the physical integrity of reactor containment (valves, airlocks, etc.), containment isolation system (logic and instrumentation), and heat removal components, and did not involve an actual reduction in function of hydrogen igniters in the reactor containment.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Susquehanna Personnel

T. Rausch, Chief Nuclear Officer
R. Franssen, Plant General Manager
D. Ambrose, Manager, Design Engineering
K. Anderson, Senior Design Engineer
C. Angione, Senior Design Engineer
D. Bockstanz, Senior Engineer
A. Corrado, Senior Electrical Engineer
M. Eckert, System Engineer
N. Giusto, System Engineer
J. Hartzell, PRA Engineer
N. Hyduk, Motor Operated Valve Program Engineer
J. Jennings, Manager, Nuclear Regulatory Assurance
D. Kostelnik, Manager, Mechanical Design Engineering
M. Krick, Senior Licensing Engineer
G. Lubinsky, Manager, Electrical Design Engineering
J. McDonald, System Engineer
J. Oswald, Electrical Engineer
D. Przyjemski, Component Engineer
B. Reppa General Manager, Engineering
A. Schrad, Senior Electrical Engineer
R. Vazquies, Senior Design Engineer
R. Weitzel, Design Engineer
R. Williams, System Engineer
M. Yackoski, Senior Engineer

NRC personnel

T. Daun, Resident Inspector
A. Foli, NRC Susquehanna Project Manager
J. Grieves, Senior Resident Inspector
C. Hobbs, Reactor Engineer

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED Open and Closed NCV

05000387(388)/2016-07-01 NCV Failure to Specify and Maintain Safety-Related Quality Standards and Materials Essential for Reactor Core Isolation Cooling (Section 1R21.2.1.1)

LIST OF DOCUMENTS REVIEWED

Audits and Self-Assessments

DI-2015-01256, 2016 NRC Component Design Bases Inspection Focused Area Self-Assessment, dated 3/04/16

Calculations

EC-002-0501, 125 VDC System 2D630 Master Battery Calculation, Revision 25
EC-002-0504, 125 VDC System 2D620 Master Battery Calculation, Revision 38
EC-002-0505, 125 VDC System 2D640 Master Battery Calculation, Revision 23
EC-002-0508, 125 VDC Utilization Voltage and Load Profile Calculation for Circuits 2D634-31, Revision 9
EC-002-0588, 125 VDC Utilization Voltage and Load Profile for Ckt 1D63437, Revision 0
EC-002-0638, 125 VDC Utilization Voltage and Load Profile Calculation for Circuits 1D634-05 and 2D634-05, Revision 4
EC-002-1031, Unit 1 and Unit 2 125VDC Battery Load Profile for Performance Surveillance Test and Modified Performance per ITS Surveillance Test, Revision 14
EC-004-0007, Control Circuit Voltage Drop, Revision 0
EC-004-0221-1, Plant AC Short Circuit Analysis, Revision 0
EC-004-0501, Attachment 7 - Breaker Coordination Data 125 VDC Panels, Revision 0
EC-004-0501, Attachment 7A - Breaker Coordination Plots 125 VDC Panels, Revision 0
EC-004-0503, Degraded Grid Scheme Tolerance Calculation, EC1, Revision 0
EC-004-0521, Over Current Protection for 4 KV Penetrations
ECI-ESS Buses, Cables, etc., Revision 0
EC-004-0537, Design Basis for 4.16 KV Degraded Grid Protection, Revision 1
EC-004-1031, Plant AC Load flow Analysis, Revision 4
EC-004-1033, Degraded Grid Relay Setpoint, Revision 1
EC-004-1036, Plant AC Short Circuit Analysis, Revision 0
EC-013-0561, Appendix R - HVAC Study, Revision 11
EC-013-1860, Handling of Transient Combustibles in the Wraparound Zones and Restricted Areas (Red Zones), Revision 5
EC-016-1027, Required Operating Torque and Weak Link Analysis HV11210A, Revision 0
EC-024-008, Design Temperature of Air Starting Skid Piping-DG, Revision 0
EC-024-0503, Diesel Generator Load Calculation, Revision 27
EC-024-0506, Air Start Receiver Pressurization Time, Revision 0
EC-024-0556, Design ESW Flow Rate Requirements to the Diesel Generator A-E Heat Exchanger, Revision 5
EC-024-0629, SSES FSAR 8.3 Diesel Generator Loading Tables Update, Revision 17
EC-024-1004, Required Diesel Generator Lube Oil Volume for Technical Specifications, Revision 0
EC-028-0505, Diesel Generator Building Heating and Ventilation System, Revision 0
EC-028-0551, ESSW Pump House Temperature Transients Caused by Ventilation Fan Failure, Revision 2
EC-030-0506, Generate Performance Curves for the Control Structure Chillers, Revision 0
EC-030-1012, Additional Control Structure Post-LOCA Heat Load for
SE-030-014AandB, Revision 0
EC-034-0551, Secondary Containment Thermal Response to an Appendix R Fire, Revision 5
EC-049-0001, Pressure Drop in RHR System, Revision 10
EC-050-1010, Max Thrust and Seismic Analysis HV149F013, Revision 2
EC-052-0002, HPCI Pressure Drop Calculations, Revision 3
EC-052-0522, Maximum HPCI Pump Discharge Pressure, Revision 1
EC-052-1061, Establish Tube Plugging Limits for HPCI Lube Oil Cooler, Revision 0
EC-059-1036, Basis for ECCS and RCIC FSAR NPSHA Calculations, Revision 6
EC-060-0523, Power Uprate Impact on Drywell Cooling, Revision 3
EC-088-0504, 250V DC Class 1E Breaker and Overload Calculation, Revision 14
EC-Flood-001, Internal Flooding Evaluations for Moderate Energy Pipe Cracks and Sprinkler System Actuation, Revision 3
EC-PIPE-1032, PSTR, PSUP, MELB Moderate Energy Pipe Crack Evaluation, Revision 4
EC-PUPC-20309, EPU Task Report T0309 - RCIC System, Revision 0
EC-PUPC-20900, EPU Task Report T0900 - Transient Analysis, Revision 0
EC-SOPC-0510, Design Base Calculation - General Setting Criteria for Electrical Protective Devices, Revision 1
EC-SOPC-0514, Relay Setting for TR101 Circuit Breaker Degraded Grid Protection at Buses 1A, 1D, 2A + 2D, 1A, 1D, 2A + 2D; 1B, 1C, 2B + 2C, Revision 0
EC-SOPC-0520, Relay Setting Calculation for Electrical Protective Devices Criteria for the Protection of 13.8kV, 4.16kV, and 480V 3 phase, Revision 0
EC-SOPC-0580, Relay Setting Calculation for Batter Charger 2D663 CB at LC 2D662 and Battery Charger 2D653B and 2D653A CBS at LC 2D652, Revision 0
EC-SOPC-0598, Relay Setting Calculation for Diesel Gen A (B, C, D, E) V Restr. TOC at Buses 1A and 2A (1B and 2B, 1C and 2C, 1D and 2D), Revision 4
EC-SOPC-0617, Relay Setting Calculation for Control Structure Chiller 0K112A/4kV Bus 1E and 0K112B/4kV Bus 1E, Revision 0 EC-
SOPC-0738, Relay Setting Calculations for TR101, 111, 201, 211 and CB OC at Buses 1A, 1D, 2A, and 2D (1B, 1C, 2B, and 2C), Revision 2
EC-SOPC-0751, Relay Setting Calculation for Bus 1A (1B, 1C, 1D, 2A, 2B, 2C, 2D) Loss of Voltage, Revision 0
EC-SQRT-0728, Dynamic Qualification of Q-Passive Devises Located in the Diesel Generator A-D, Revision 1
EC-SQRT-0792, Qualification of Level Gauges
LG-03403E,
LG-03452E, and
LG-03476E, Revision 0
EC-VALV-1041, Generic Letter 95-07 Applicability, Revision 5
EC-VALV-1072, DC Motor Operated Gate Valve, dated 4/5/16
EC-VALV-1075, Appendix I, MOV Calculation Results for HV11210A, printed 08/23/16 EWR M24044, CS Chilled Water Design Flow to ESRC, dated 5/16/1993 M-30, Dynamic Qualification-Fuel Oil Tank, date 5/16/84 M-PUP-010, Diesel Generator Buildings A, B, C, D and E Heat Gain, dated 1/17/1992
OT-183-001, MSRV Remote Actuation Following Maintenance, Revision 4
Completed Surveillance, Performance, and Functional Tests RTSV
14233937, Diesel Generator 0G501C Integrated Surveillance Test, performed 10/9/13 RTSV
1456899, 24 Month Channel B 2D620-125 VDC Battery Discharge Performance Test and Battery Charger Capability Test, performed 5/2/13 RTSV
1576711, Unit 1 Division 1 DG LOCA/LOOP Test per
SE-124-107, performed 4/23/14 RTSV
1687667, 48 Month Channel B 2D620-125 VDC Battery Discharge Performance Test and Battery Charger Capability Test, performed 4/24/15 RTSV
1701406, 2 YR 4KV Bus 2A202 UV CH Cal. ACT# Z1374-01, performed 4/24/15 RTSV
1704644, 4KV Bus 2B (2A202) Offsite Supply Transfer per
SE-204-201, performed 4/21/15 RTSV
1705026, Unit 2 Division II LOCA LOOP Test per
SE-224-207, performed 4/20/15 RTSV
1712389, 2YR LSFT Unit 2 LOCA Initiation Scheme to the Unit 1 4KV ESS Auxiliary Buses 93% Degraded Grid Voltage Timer Reselect Schemes (SE-204-105), performed 5/8/15 RTSV
1715252, 2YR ESS Auxiliary Bus 2B (2A202) 93% Degraded Grid Voltage Timer Reselect Test, performed 6/4/15 RTSV
1762534, Diesel Generator 0G501C Integrated Surveillance Test, performed 6/9/15 RTSV
1805887, Unit 1 Division 1 DG LOCA/LOOP Test per
SE-124-107, performed 4/2/16
RTSV
1808413,
SO-183-002 24 mo ADS Valve Manual Actuation, performed 4/8/16 RTSV
1950030,
SM-202-001 - 31DY-2D610/620/630/640 125V STN BATT Bank checks, performed 12/23/15 RTSV
1956350,
SM-202-001 - 31DY 125V STN BATT Bank checks, performed 1/27/16 RTSV
1964841,
SM-202-001 - 31DY 125V STN BATT Bank checks, performed 2/24/16 RTSV
1975419, 92 Day 125VDC Station Battery Bank Check, performed 6/3/16 RTSV
1977435,
SI-183-329 Quarterly Calibration of Automatic Depressurization System (ADS) Drywell Pressure Bypass Timers B21C-K114A, B, C, and D, performed 6/24/16 RTSV
1977439,
SI-183-208 Quarterly Functional Test of Reactor Vessel Water Level (Low Low) Level 3 (ADS Permissive) Channels
LIS-B21-1N042AandB, performed 6/21/16 RTSV
1977444,
SI-183-322 Quarterly Calibration - Automatic Depressurization System Initiation Timers, performed 6/24/16 RTSV
1993820, Monthly DG "C" Operability Test, performed 5/19/16 RTSV
1996146, Monthly DG "C" Operability Test, performed 6/5/16
RTSV
1997361, 31 Day 125VDC Station Battery Bank Check, performed 6/22/16 RTSV
1999502, FERC Related Z0001-51,
SM-202-001 92DY 125V Station Battery Bank Checks, performed 9/3/16 RTSV
1999881, Monthly DG "C" Operability Test, performed 7/5/16 RTSV
2002034, 31 Day 4KV Degraded Volt Channel Function, performed 7/14/16 RTSV
2003266, Weekly Electrical Distribution Verification, performed 6/24/16
SC-023-005, 31 Day Particulate Analysis and Water Check on 'C' EDG Fuel Oil Storage Tank, performed 4/2/16
SE-013-009, 24 Month Inspection of Fire Windows/Fire Dampers and Associated Hardware, performed 03/03/15
SE-024-C01, Diesel Generator 0G501C Integrated Surveillance Test, completed 10/9/13
SE-030-014A, 'A' Control Room Floor Cooling Performance Test, performed 12/15/15
SE-183-006, Main Steam Safety Relief Valve Inservice Testing, Revision 7
SO-024-001A, Monthly Diesel Generator 'A' Operability Test, performed 1/12/16
SO-024-001C, Monthly Diesel Generator 'C' Operability Test, performed 1/12/16
SO-024-001C, Monthly Diesel Generator 'C' Operability Test, performed 7/5/16
SO-030-A03, Quarterly Control Structure Chilled Water Flow Verification Loop A, performed 07/05/16
SO-100-021, ESW RHRSW Functional Test at 1C201B, performed 04/11/16
SO-116-015A, Division I Two Year RHRSW System RPI Checks (Unit 1 Reactor Building Valves), performed 04/07/16
SO-116-A01, Monthly RHR Service Water System Alignment Check Division I, performed 08/03/16
SO-116-A02, Quarterly RHRSW Valve Exercising Division I, performed 07/01/16
SO-183-002, U-1 24 Months ADS Valve Manual Actuation, performed 4/8/16
SO-183-002, U-1 24 Months ADS Valve Manual Actuation, performed 5/12/16
SO-183-016, ADS 2YR-Logic System Functional Division 1, performed 4/7/16
TP-05-076, ESW Flow Balance, performed 10/11/13
TP-134-056, Unit 1 ESGR Standby Fan Testing, performed 06/02/16
Completed Preventive Maintenance, Calibrations, and Inspections As-found Visual Inspection of 'A' Control Structure Chiller, dated 01/07/13 As-found Visual Inspection of 'A' Control Structure Chiller, dated 12/14/10 Control Structure Chilled Water Circ Pump 0P162A Infrared Survey, dated 08/31/16 Control Structure Chilled Water Circ Pump 0P162A Vibration Trend Data, dated 07/05/16 Control Structure Chiller 0K112A Infrared Survey, dated 08/31/16 Control Structure Chiller 0K112A Vibration Trend Data, dated 01/09/16 Control Structure Chiller Condenser Water Pump 0P171A Infrared Survey, dated 07/05/16 Control Structure Chiller Condenser Water Pump 0P171A Vibration Trend Data, dated 07/05/16
Eddy Current Testing Report for 'A' Control Structure Chiller, dated 12/15/10 ESGR 1V222A Fan Flow Rate Testing Data Sh., dated 01/29/14 ESGR 1V222A Fan Vibration Trend Data, dated 05/17/16 ESGR 1V222A Infrared Survey of Breaker, dated 02/04/16 Instrument Calibration Sh. for Emergency Condensate Loop Temperature
TE-08612A, dated 10/08/14 Instrument Calibration Sh. for ESGR Temp Switch High/Low
TSHL-17631B, dated 02/11/09 Instrument Calibration Sh. for ESGR Temp Switch High/Low
TSHL-17631B, dated 08/20/13 RTSV
1692380, 2 yr Test and Cal 50D Relay 2A20501, performed 4/11/15 RTSV
1451147, 2 yr Test and Cal 50D OC Relay 2A20501, performed 4/13/13 RTSV
1692381, 2 yr Test and Cal 50D Relay 2A20502, performed 4/11/15 RTSV
1492381, 2 yr Test and Cal 50D OC Relay 2A20502, performed 4/13/13 RTSV
1687661, 4 yr - RC Pmp Bkrs 2A20501 and 2 Arc T, performed 5/20/15 RTSV
1068335, 4 yr - RC Pmp Bkrs 2A20501 and 2 Arc T, performed 5/12/11
Corrective Action Condition Reports (CRs)
217087
851024
851719
871022
871023
871024
1005793
1058196
1058916
1156877
1217911
1235872
1359171
1389608
1428156
1461457
1486036
1500216
1501556
1501778
1504737
1504785
1505231
1505265
1506105
1508022
1515111
1515309
1530332
1532616
1538448
1572932
1616182
1643085
1647412
1649562
1660445
1669596
1693368
1712564
1732454
1747808
1753834 2014-11378 2015-01256 2015-21681 2016-04833 2016-06873
2016-12748 2016-14215 2016-17738 2016-20090* 2016-20625 2016-21100 2016-21168 2016-21510 2016-21546* 2016-21548* 2016-21550* 2016-21551* 2016-21552* 2016-21580* 2016-21584* 2016-21588* 2016-21643* 2016-21644* 2016-21830* 2016-21854* 2016-21948* 2016-21949* 2016-21950 2016-22058* 2016-22599* 2016-22692* 2016-22747* 2016-22789* 2016-22792* 2016-22817* 2016-22822*
2016-22886* 2016-22893* 2016-22900* 2016-23043* 2016-23373* 2016-23398*
2016-23477* 2016-23555* 2016-23615* 2016-23619* 2016-23624* 2016-23678*
2016-23706* 2016-23708* 2016-23712* 2016-23877* 2016-23912* 2016-23971*
2016-23983* 2016-24015* *CR written as a result of this inspection
Design and Licensing Bases DBD002, Control Structure HVAC and Chilled Water Systems, Revision 2
DBD007, Reactor Building HVAC, Chilled Water and SGTS, Revision 3 DBD009, ESW, RHRSW, and Ultimate Heat Sink, Revision 3 DBD014, Residual Heat Removal System, Revision 4 DBD016, Design Basis Document for Main Steam System and Automatic Depressurization System, Revision 4 DBD044, Design Basis Document for Reactor Recirculation System, Revision 4 C1027, Specification-Design and Installation of Penetration Seals, Revision 10
DCP 95-9071, U-2 Elimination of HPCI Valve (HV255-F006) Susceptibility to Pressure Locking, Revision 0
EQAR-029, Environmental Qualification Assessment Report-ITT Cannon Circular Connectors, Model
CE-9446-98, Revision 5
EQAR-081, Environmental Qualification Assessment Report-Crosby Pilot Solenoid Valve, Model
IMF-2RA, Revision 9
MFP-QA-2241, Electrical Discipline Calculations, Revision 5
MFI-2241, Administration and Control of 120VAC, 125VDC, and 250VDC Voltage Drop Calculations Using VOLTCALC, Revision 0 Specification 8856-M-156, Containment Instrument Gas Accumulators, Revision 8 Susquehanna Unit 1 and Unit 2 Technical Specifications 3.8, Electrical Power Systems, Revision 4 Susquehanna Unit 1 and Unit 2 UFSAR Table 8.3-1, Assignment of ESF and Selected Non-ESF Loads to Diesel Generators and ESS Buses, Revision 59

Drawings

93-13709, 14"-900 Weld Ends Pressure Seal, Flex Wedge, Carbon Steel, Gate Valve with
SB-3-150 Limitorque Operator, Revision G C-75-136, 12" Diam. x 21" LG Gas Accumulator Tank Susquehanna Stations Units 1 and 2, Revision 5 E-1 Sh. 1, Unit 1 and 2 Single Line Diagram Station, Revision 37 E-1 Sh. 1A, Unit 1 and 2 Single Line Diagram Station, Revision 9 E-1 Sh. 2, Units 1 and 2 Single Line Diagram 13.8KV thru 480V Station Auxiliary Bus Arrangement, Revision 21 E-4, Units 1 and 2 Single Line Meter and Relay Diagram 13.8KV Start-up Auxiliary Power System, Revision 38 E-4 Sh. 3, Unit 2 Single Line Meter and Relay Diagram 13.8 KV Unit Auxiliary Power System, Revision 18 E-5, Unit 2 Single Line Meter and Relay Diagram 4.16KV ENG. Safeguards Power System, Revision 32 E-5 Sh. 4, Single Line Meter and Relay Diagram 4.16 KV Diesel Generator Common, Revision 17 E-11 Sh. 11, Unit Common One Line Diagram Diesel Generator "E", Revision 18 E-11 Sh. 2, Unit 2 Single Line Meter and Relay Diagram 125 and 250 VDC System, Revision 28 E-26, Unit 2 Schematic Meter and Relay Diagram 125VDC System, Revision 10 E-57, Sh. A, Unit 1 and Common Power Cable Ampacity Tables, Revision 12
E-49, Sheet 20, Units 1 and 2, C E106321, Sheet 5B, Common Penetrations Diesel Generator Building Area 44-Plan of Elevation 677'-0", Revision 26 E-105 Sh. 11, Schematic Diagram 4.16 KV Bus 2C Diesel Generator Circuit Breaker Control, Revision 29 E-105 Sh. 11A, Schematic Diagram 4.16 KV Bus 2C Diesel Generator Circuit Breaker Control, Revision 11 E-150, Sh. 10, Unit 1 Schematic Diagram RHR Heat Exchanger Inlet Valve, Revision 9 E-151 Sh. 36, Schematic Diagram Reactor Recirc RPT Breaker 3A, Revision 16 E-151 Sh. 37, Schematic Diagram Reactor Recirc RPT Breaker 4A, Revision 19 E-151 Sh. 41, Schematic Diagram Reactor Recirc RPT Breakers Unit 2, Revision 2 E-152, Sh. 27, Unit 2 Schematic Diagram HPCI Pump Discharge Valve, Revision 17 E-154, Sh. 7, Schematic Diagram RCIC Injection Shutoff Valve Unit 1, Revision 20 E-180 Sh. 2, Block Diagram ADS and Safety Relief Valves, Revision 9 E-185, Sh. 31, Schematic Diagram Motor Overload Bypass System Unit 1, Revision 3 E-185, Sheet 7, Schematic Diagram Bypass Indication System U-1, Revision 9 E-185, Sheet 15, Schematic Diagram Bypass Indication System U-2, Revision 8 E-214, Sh. 11, Schematic Diagram HVAC Control Structure Chilled Water Sys Mixing Valves Common, Revision 16 E-259 Sh. 1B, Unit Common Schematic Diagram Diesel Engine Control, Revision 7 E-259 Sh. 9B, Common Schematic Diagram Diesel Generator Excitation Control, Revision 11 E-328, Susquehanna Unit 2 Schematic Diagram Annunciator Alarm Re-flasher 125 VDC System 2D610, 2D620, 2D630, 2D640, Revision 10
E-612, Sh. 2, Unit 1 480V Motor Control Center Break and Overload Setpoint List 1B237, Revision 9 E-618, Sheet 5, U-2 Safety Related 250V DC Motor Control Center Breaker and Overload Setpoint List, Revision 3
FF61742, Sh. 1, 20" 815L-11-22HBUA Mod B Wafer Sphere Valve ANSI Cl 150 Nuclear Class 3, Revision 0
HCC-132-4, Isometric-Reactor Building Nuclear Boiler Unit1, Revision 2
HCC-133-3, Isometric-Reactor Building Nuclear Boiler, Revision 1 J-451, Sheet 1, Remote Shutdown Panel, 1C201A RCIC Section, Revision 23 J-451, Sheet 2, Remote Shutdown Panel, 1C201B RHR, Revision 20 J-451, Sheet 3, Remote Shutdown Panel, 1C201 RHR Section, Revision 18
LA-2L620-001, 125 VDC Panel 2L620, Revision 8
M1-B21-129 Sh. 1, Elementary Diagram Auto Depressurization System, Revision 18 M1-B21-129 Sh. 2, Elementary Diagram Auto Depressurization System, Revision 11 M1-B21-129 Sh. 3, Elementary Diagram Auto Depressurization System, Revision 14 M1-B21-129 Sh. 4, Elementary Diagram Auto Depressurization System, Revision 7 M1-B21-129 Sh. 5, Elementary Diagram Auto Depressurization System, Revision 6 M1-B21-129 Sh. 6, Elementary Diagram Auto Depressurization System, Revision 7 M1-B21-129 Sh. 7, Elementary Diagram Auto Depressurization System, Revision 5 M1-B21-129 Sh. 8, Elementary Diagram Auto Depressurization System, Revision 11 M1-B31-178 Sh. 18, Reactor Recirc Pump and MG Set, Revision 14 M1-C72-2 Sh. 4, Common Instrument Engineering Diagram Reactor Protection System, Revision 7 M1-C72-5 Sh. 17, Elementary Diag Reactor Protection System, Revision 5 M30-124 Sh. 1B, Common DG Control Schematic Starting Sequence Control Panel 0C521C, Revision 4
M30-124 Sh. 2B, Common DG Control Schematic Starting Sequence Control Panel 0C521C, Revision 10 M30-124 Sh. 4B, Common DG Control Schematic Starting Sequence Control Panel 0C521C, Revision 1 M30-124 Sh. 13B, Common DG Control Schematic Starting Sequence Control Panel 0C521C, Revision 6 M30-124 Sh. 14B, Common DG Control Schematic Starting Sequence Control Panel 0C521C, Revision 4 M30-204 Sh. 2B, Control Schematic Static Excitation Voltage Regulator and Voltage Controls for Diesel Generator 0C519C, Revision 5 M30-204 Sh. 4B, Control Schematics Static Excitation Voltage Regulator Interwiring for Diesel Generators 0G501C and 0C519C, Revision 5 M-111, Sh. 2, PandID Emergency Service Water System 'A' Loop, Revision 53 M-112, Sh. 1, PandID RHR Service Water System, Revision 53 M-141 Sh. 1 of 2, PandID Nuclear Boiler, Revision 54 M-141, Sh. 2, Unit 1 PandID - Nuclear Boiler, Revision 20 M-142 Sh. 2, PandID Nuclear Boiler Vessel Instrumentation, Revision 17 M-149, Unit 1 PandID - RCIC, Revision 53 M-176, Sh. 1, Unit 1 PandID Air Flow Diagram Zone 1 Reactor Building, Revision 31 M-177, Unit 1 PandID - Drywell Air Flow Diagram, Revision 14 M-178, Sh. 1, PandID Control Structure Air Flow Diagram, Revision 35 M-182, Sh. 1, PandID Diesel Gen and ESSW Pumphouse Air Flow Diagram, Revision 9
M-186, Sh. 1, PandID Control Structure Chilled Water System 'A', Revision 43 M-186, Sh. 2, PandID Control Structure Chilled Water System 'B', Revision 15 M-186, Sh. 3, PandID Control Structure Chilled Water Chiller 0K112A, Revision 11 M-2101, Sh. 1, Unit 2 PandID - Main Steam, Revision 42 M-2101, Sh. 3, Unit 2 PandID - Main Steam, Revision 14 M-2151, Unit 2 PandID - RHR, Revision 62 M-2155, Unit 2 PandID - HPCI, Revision 45 M-2156, Sh. 1, Unit 2 PandID - HPCI Turbine-Pump, Revision 31 M-2176, Sh. 1, Unit 2 PandID Reactor Building Air Flow Diagram Zone II, Revision 24
SP-HCC-132-4, From Line
HCB-110 to MS Relief Valve to Accumulator Tanks 1T-402 M, G, and J, Revision 13
SP-HCC-132-10, From Accumulator
IT-402A to Main Steam Relief Valve 1F013G, Revision 6 X-33-1, Sheet 2, U-2 Penetrations Reactor Building Area 33-Plan Elevation 645'-0", Revision 28 X-44-1, Sheet 2, Common Penetrations Diesel Generator Building Area 44-Plan of Elevation 660'-0", Revision 25 X-44-2, Sheet 4C, Common Penetrations Diesel Generator Building Area 44-Plan of Elevation 660'-0", Revision 1 X-44-2, Sheet 5B, Common Penetrations Diesel Generator Building Area 44-Plan of Elevation 677'-0", Revision 26 X-44-3, Sheet 6, Common Penetrations Diesel Generator Building Area 44-Plan of Elevation 710'-9", Revision 14 X-44-3, Sheet 6A, Common Penetrations Diesel Generator Building Area 44-Plan of Elevation 710'-9", Revision 0 X-44-4, Sheet 8, Common Penetrations Diesel Generator Building Area 44-Plan of Elevation 723'-0", Revision 8 X-101, Sheet 1, Piping and Mechanical Sleeves and Seal Details Penetrations and Blockouts, Revision 13 V-486, Sh. 3, Diagram Control Structure Chilled Water System Emerg Condenser Water Temp, Revision 9
Engineering Evaluations 85-0115, Replacement Item Equivalency Evaluation-Emergency Diesel Generator High Pressure Lube Oil Hose, Revision 0
91-0136, Replacement Item Evaluation-Diesel Generator Fuel Injector Drain Hoses, Revision 1 RHR LPCI Injection Flow, Effects of EDG Voltage and Frequency Tolerances on RHR LPCI Injection Flow Under Accident Conditions, dated 9/15/14
Maintenance Work Orders
E3280-02 M0999-01 M0999-02 M1340-07 55627
184857
355728
441602
490734
490735
611313
890715
986922
1110931
1119868
1162828
1162829
1170790
1176734
1225726
1257887
1330052
1364839
1402494
1456889
1458490
1540504
1560353
1682664
1697321
1709614
1724914
1723029
1738011
1739375
1740383
1740830
1745843
1754233
1754501
1775604
1845078
1852797
1868450
1966442
1977435
1977444
1975419
1978957
1984180
2002830
2008517

Miscellaneous

0G501C, Diesel Engine Diagnostic Report, performed 8/21/16 8856-M-423, Specification for Determining the Operability of Piping Systems for Susquehanna Units 1 and 2, Revision 0 97061, Industry Events Review Program Assignment Form-Preconditioning of Plant SSG's Before ASME Code IST or TS Surveillance Testing, dated 5/28/97 Carrier Performance Data Sh. for Emergency Switchgear Cooler 1V/2V222A, Revision 0
CH-024-003, Emergency Diesel Lube Oil, performed 9/11/03
DCP# 22635, Multiple Hi Impedance Faults in Fire Area
CS-9 Re-power Backup Control for Div 1 ADS Valves from PNL 2D614 Breaker 03 to Breaker 18, dated 7/6/00 EC/BTT, Increase Drywell Fan Temperature Setpoint, dated 9/16/11 EC#
375683, Bus 2A205/2A206 4kV Breaker Replacement, dated 9/5/02 EDG Fuel Oil Sample Report
2016006646, performed 7/27/16
EDS-06, Design Standard for Motor Operated Valve Voltage Drop Considerations, Revision 5
EDV-SVX-0012, Dedication Criteria for ASCO Catalog No. 212-631-1F Solenoid Valve, Revision 3 EPRI PM Template, Medium Voltage 1KV to 7KV Switchgear, Revision 0
Equipment Apparent Cause Evaluation for A Control Structure Chiller 0K112A, dated 04/12/16 LDCN 4612, Plant Process Computer Replacement, dated 10/8/08 List of PM Activities for System 204 - Frequency: 31 Days, Annual, 2 Year, 18, 4 Year, 36, 6 Year, 54, 10 Year, 7, 12 Year, 7, 30 Year, 32 Year, 35 Year, 36 Year, 40 Year, 47 Year, and On-demand, dated 8/24/16
PA-B-NA-041, Appendix E, PRA Time Sensitive Operator Actions, Revision 5 Underground Piping and Tanks Program Asset Management Plan, Revision 0
Normal and Special (Abnormal) Operations Procedures
AOP-024-001, Diesel Generator Abnormal Operating Procedure, Revision 0
AOP-030-001, Control Structure HVAC Abnormal Operating Procedure, Revision 0
AR-015-001, 13.8/4 KV Switchgear Distribution and Diesel Generators A, B, C 0C653, Revision 47
AR-029-001, Control Structure, SGTS, DG and ESW PH Ventilation Div 1 0C681, Revision 34
AR-109-001, F01, RHR SW A HI Radiation, Revision 36
AR-127-001, Drywell, Reactor Building and Various HVAC Div 1 1C681, Revision 19
EO-000-031, Station Power Restoration, Revision 27
EO-100-030, Unit 1 Response to Station Blackout, Revision 35
EO-200-030, Unit 2 Response to Station Blackout, Revision 32
ON-4KV-101, Loss of 4KV Bus, Revision 2
ON-CSHVAC-001, Loss of Control Structure HVAC, Revision 0
ON-RBCW-101, Loss of Reactor Building Chilled Water, Revision 0
OP-024-001, Diesel Generators, Revision 82
OP-030-001, Control Structure Chilled Water System, Revision 47
OP-037-003, Transferring Inventory from Refueling Water Storage Tank to CST A (B) or CST A(B) to RWST Using Intertie, Revision 30
OP-102-001, 125V DC System, Revision 25
OP-116-001, RHR Service Water, Revision 53
OP-128-001, Emergency Safeguard Service Water (ESSW) Pumphouse HVAC, Revision 15
OP-134-002, Reactor Building HVAC Zones 1 and 3, Revision 72
OP-150-001, RCIC System, Revision 46
OP-160-001, Drywell Ventilation System, Revision 15
OP-202-001, 125V DC System, Revision 23
OP-249-001, RHR System, Revision 44
OP-249-004, RHR Containment Cooling, Revision 30
OP-252-001, HPCI System, Revision 61
OP-293-001, Main Turbine Operation, Revision 67
OP-AD-300, Administration of Operations, Revision 17
Operating Experience
NRC Information Notice 2010-23, Malfunctions of Emergency Diesel Generator Speed Switch Circuits NRC Information Notice 2012-016, Preconditioning of Pressure Switches before Surveillance Testing NRC Information Notice 2013-17, Significant Plant Transient Induced by Safety - Related Bus Maintenance at Power
Operator Training
TM-OP-034, Operator Training Manual for Secondary Containment System, Revision 1
TM-OP-052, High Pressure Coolant Injection (Comprehensive), Revision 2
TM-OP-300-ST, Operator Training Manual for Chillers and Chilled Water System, Revision 6
TM-OP-073-ST, Primary Containment Atmosphere Control, Revision 4

Procedures

E-113-008, 6 Month Inspection of Unit 1 Fire Doors, Revision 8
EDS-07, Design Standard - Loads or Other Electrical Changes to the 125 VDC Distribution System, Revision 8
LA-0521-003, Diesel Generator C 0C521C, Revision 19
MI-AD-043, Maintenance Standard (Work Document: 1975419), Revision 42
MI-PD-002, Thermography Program, Revision 5
MT-GE-005, Circuit Breaker and Switchgear Inspection and Maintenance 5 and 15 KV, Revision 20
MT-GE-036, DC MCC Inspection and Maintenance - GE Cubicles, Revision 14
NDAP-QA-0343, Time Critical and Time Sensitive Operator Actions, Revision 1
NDAP-QA-0401, Emergency Diesel Generator Reliability Monitoring Program, Revision 5
NDAP-QA-0440, Control of Transient Combustible/Hazardous Materials, Revision 19
NDAP-QA-0485, Thermography Training, Qualification, and Certification Program, Revision 0
SE-124-107, Unit 1 Division 1 DG LOCA LOOP Test, Revision 25
SI-183-208, Quarterly Functional Test of Reactor Vessel Water Level (Low Low
SE-204-105, 24 Month Logic Functional Test of the Unit2 LOCA Initiation Scheme to the Unit 1 4KV ESS Auxiliary Buses 93% Degraded Voltage Timer Reselect Schemes, Revision 5
SE-204-201, 24 Month 4.16KV Class 1E Bus 2B (2A202) Offsite Supply Transfer Check, Revision 11
SE-204-203, 24 Month ESS Auxiliary Bus 2B (2A202) 93% Degraded Grid Voltage Timer Reselect Test, Revision 5
SE-224-207, Unit 2 Division II Diesel Generator LOCA LOOP Test Special, Infrequent or Complex Test/Evolution, Revision 23
SE-293-001, 24 Month System Functional and Turbine Bypass System Response, Revision 9
SI-83-312, Instrument Calibration Sheet 183H-MSIV Leakage Control System, Revision 0
SI-83-320, Instrument Calibration Sheet 183H-MSIV Leakage Control System, Revision 2
SI-183-208, Quarterly Functional Test of Reactor Vessel Water Level (Low Low) Level 3 (ADSPermissive) Channels
LIS-B21-1N042AandB, R18
SI-183-322 Quarterly Calibration - Automatic Depressurization System Initiation Timers, Revision 15
SI-183-329, Quarterly Calibration of Automatic Depressurization System (ADS) Drywell Pressure Bypass Timers B21C-K114A, B, C, and D, Revision 9
SM-106-000, Functional Testing, Inspection and PM of Primary Containment Penetration Conductor Overcurrent Protective Devices, Revision 18
SM-202-001, 92 Day FERC Related Z0001-51, 125V DC Station Battery Bank Checks Weekly, Monthly, and Quarterly Electrical Parameter Checks Unit 2, Revision 19
SM-202-B03, 24 Month Channel B 2D620 125 VDC Battery Service Discharge Test and 2D623 Battery Charger Capability Test, Revision 26
SM-202-B04, 48 Month Channel B 2D620 125 VDC Battery Discharge Modified Test and Battery Charger Capability Test, Revision 20
SM-204-002, 4KV Bus 2A202 24 Month Undervoltage Channel Calibration, Revision 6
SO-000-005, Weekly Electrical Distribution Verification, Revision 4
SO-150-004, Quarterly RCIC Valve Exercising, Revision 34
SO-183-002, 24 mo ADS Valve Manual Actuation, Revision 18
SO-183-016, 24 mo Division 1 ADS Logic System Functional Test, Revision 0
SO-183-017, 24 month Division 2 ADS Logic System Functional Test, Revision 0
SO-200-006, Shiftly Surveillance Operating Log, Revision 81
SO-204-001, Monthly 4KV Bus 2A201, 2A202, 2A203, and 2A204 Degraded Voltage Channel Functional Test, Revision 19
SO-249-A02, Quarterly RHR System Flow Verification, Div I, Revision 23
SO-252-002, Quarterly HPCI Flow Verification, Revision 70
SO-252-004, Quarterly HPCI Valve Exercising, Revision 31
SO-252-005, 24 Month HPCI Flow Verification, Revision 26
SO-252-006, HPCI Comprehensive Flow Verification, Revision 21
SO-282-001, Monthly Turbine Bypass Valve Cycling, Revision 26
SP-00-111, Electrical Safe Work Practice, Revision 23
SUS-ISTPLN-100.0, Unit 1 Inservice Testing Program, Revision 8
SUS-ISTPLN-200.0, Unit 2 Inservice Testing Program, Revision 10
NDAP-QA-0017, MOV Program, Revision 15
Risk and Margin Management 016-N-N-VENT-O, Operator Fails to Open ESSW Pumphouse for RHRSW Ventilation, dated 02/07/12
EC-RISK-1158, EDG and AC System Notebook, Revision 0
OC-PSA-000, Susquehanna Nuclear Generating Station Documentation Roadmap, Revision 1
PA-B-NA-041, SSES PSA Notebook, Attachment E-PRA Time Sensitive Operator Actions, Revision 5 Plant Risk Information e-Book for Susquehanna Nuclear Generating Station, dated 6/21/12 Risk-Informed Inspection Notebook for Susquehanna Nuclear Generating Station, Revision 2.01a
System Health Reports, System Walkdowns, and Trending 024, Emergency Diesel Generators System Health Scorecard 2016-1Q 282/293, Bypass Steam/ Main Turbine Health Report, 2016-1Q 150, Unit 1 RCIC, 2016-1Q 252, Unit 2 HPCI, 2016-1Q 149, Unit 1 Residual Heat Removal, 2016-1Q
Vendor Technical Manuals and Specifications 8856-E-109, Technical Specification for Medium-Voltage Metal-Clad Switchgear (Safeguards) for the Susquehanna Steam, Revision 3 8856-E-119, Technical Specification for Batteries and Battery Chargers, Revision 12
GEK-73602B, Susquehanna 1 Operation and Maintenance Instructions Automatic Depressurization System, dated 6/84
IOM 168, Hermetic Centrifugal Liquid Chillers Installation, Maintenance, and Operating Manual, dated 01/13/1976
IOM 211, Installation, Operation and Maintenance of 5 KV Type
DHP-VR Vacuum Replacement Circuit Breakers for DHP Switchgear, Revision 26
IOM 224, Jamesbury Wafer-Sphere Butterfly Valve Installation, Maintenance, and Operating Manual, Revision 10
IOM 231, Batteries CandD, dated 11/8/1995
IOM 276, Cooler and Fan Installation, Maintenance, and Operating Manual, dated 01/03/1977 Portec Inc. Instruction Manual, Model 72 10400 100

LIST OF ACRONYMS

ADAMS Agency-Wide Documents Access and Management System
ADS Automatic Depressurization System
CAP Corrective Action Program
CDBI Component Design Bases Inspection
CFR Code of Federal Regulations
CR Condition Report
CST Condensate Storage Tank
DBD Design Basis Document
DC Direct Current
DRS Division of Reactor Safety
EDG Emergency Diesel Generator
ESS Emergency Safety System
ESSW Emergency Safeguard Service Water
ESW Emergency Service Water °F Degrees Fahrenheit
HPCI High Pressure Coolant Injection
IMC Inspection Manual Chapter
IN Information Notice
IP Inspection Procedure
IST In-Service Test kV Kilovolts
LERF Large Early Release Frequency
LOCA Loss-of-Coolant Accident
LOOP Loss-of-Offsite Power
MCC Motor Control Center
MCCB Molded Case Circuit Breaker
MOV Motor-Operated Valve
NCV Non-Cited Violation
NRC Nuclear Regulatory Commission
OE Operating Experience
PM Preventive Maintenance
PRA Probabilistic Risk Assessment
PRIB Plant Risk Information e-Book
RAW Risk Achievement Worth
RCIC Reactor Core Isolation Cooling
RHR Residual Heat Removal
RRW Risk Reduction Worth
RWST Refueling Water Storage Tank
SBO Station Blackout
SDP Significance Determination Process
SPAR Standardized Plant Analysis Risk
SRV Safety Relief Valve
SSC Structures, Systems, and Components Talen Talen Energy Company
TS Technical Specification
UFSAR Updated Final Safety Analysis Report
VAC Volts Alternating Current