IR 05000352/2011005
ML12020A071 | |
Person / Time | |
---|---|
Site: | Limerick |
Issue date: | 01/20/2012 |
From: | Paul Krohn Reactor Projects Region 1 Branch 4 |
To: | Pacilio M Exelon Nuclear, Exelon Generation Co |
Krohn P | |
References | |
IR-11-005 | |
Download: ML12020A071 (39) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION
REGION I
475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406*1415 January 20, 2012 Mr. Michael Senior Vice President, Exelon Generation Company, LLC President and Chief Nuclear Officer, Exelon Nuclear 4300 Winfield Rd.
Warrenville,IL 60555 SUB~IECT: LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000352/2011005 AND 05000353/2011005
Dear Mr. Pacilio:
On December 31,2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Limerick Generating Station, Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on January 13, 2012, with Mr. W.
Maguire, Site Vice President, and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, obs!rved activities, and interviewed personnel.
This report documents one NRC-identified finding of very low safety significance (Green). This finding was determined to involve a violation of NRC requirements. However, because of the very low safety significance, and because it is entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV). consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest the NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Limerick Generating Station. In addition, if you disagree with the cross-cutting aspect assigned to the finding in this report, you should provide i3 response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Limerick Generating Station.
In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).
Sincerely, f:ztv! -/f;! ~rLL Paul G. Krohn. Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos.: 50-352,50-353 License Nos.: NPF-39, NPF-85
Enclosure:
Inspection Report 05000352/2011005 and 05000353/2011005 w/Attachment: Supplemental Information
REGION I==
Docket Nos.: 50~352, 50-353 License Nos.: NPF-39, NPF-85 Report No.: 05000352/2011005 and 05000353/2011005 Licensee: Exelon Generation Company, LLC Facility: Limerick Generating Station, Units 1 & 2 Location: Sanatoga, PA 19464 Dates: October 1, 2011 through December 31, 2011 Inspectors: E. DiPaolo, Senior Resident Inspector N. Sieller, Resident Inspector J. Ambrosini, Acting Senior Resident Inspector J. Richmond, Senior Reactor Inspector J. Tomlinson, Operations Engineer S. Ibarrola, Project Engineer J. Lilliendahl, Reactor Inspector T. Moslak, Health Physicist Miller, Project Engineer Approved By: Paul G. Krohn, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000352/2011005, 05000353/2011005; 10/01/2011-12/31/2011; Limerick Generating
Station, Units 1 and 2; Post Maintenance Testing.
This report covered a three-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. The inspectors identified one finding of very low safety significance (Green), which was determined to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SOP). The cross-cutting aspects for the findings were determined using IMe 0310, "Components Within Cross-Cutting Areas." Findings for which the SOP does not apply may be Green, or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a Green NCVof 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for failure to implement adequate corrective actions for a previous NRC-identified finding. The previous finding involved a failure to perform adequate preventive maintenance (PM) on an emergency diesel generator (EDG) due to site engineers not being fully aware of new PM requirements developed by Exelon corporate.
The lack of proper PM led to a failure of an EDG in May 2010. In response to the previous finding, Limerick performed an apparent cause evaluation (ACE) and developed actions to address the causes and extent of condition. However, the inspectors identified that the actions were not properly implemented, and, as a result, the deficiency identified by the inspectors was not fully resolved. Exelon entered the issue in the Corrective Action Program (CAP) for resolution.
The inspectors determined that the failure to implement adequate corrective actions for a previous NRC-identified finding was a performance deficiency. The issue is more than minor because, if left uncorrected, it could become a more significant safety concern.
Specifically, the issues identified by the inspectors impacted Limerick's ability to establish and implement appropriate PM for equipment relied on for safe operation of the plant. Until the issues are fully resolved, Limerick continues to be vulnerable to gaps in their PM program. This issue affects all sites in the Exelon fleet. The finding was determined to be of very low safety significance (Green) using Attachment 4 to IMC 0609, "Significance Determination Process," because the incomplete corrective actions did not result in an actual loss of safety function.
This finding has a cross-cutting aspect in the area of Problem Identification and Resolution,
Corrective Action Program, because Exelon failed to implement appropriate corrective actions for a previous NRC-identified finding in timely manner. P.1(d) (Section 1R19)
Other Findings
None.
REPORT DETAILS
Summary of Plant Status
Unit 1 began the inspection period at 100 percent power. On October 15, operators reduced power to approximately 90 percent for a control rod pattern adjustment. The plant was returned to 100 percent power on October 16. On November 12, operators again reduced power to 90 percent for a rod pattern adjustment. The unit was returned to 100 percent power on November 13. On December 10, operators reduced power to approximately 80 percent to facilitate main turbine valve testing, control rod channel distortion testing, and to perform a control rod pattern adjustment. Operators returned the unit to full power on December 12.
Operators commenced a planned shutdown on December 17 for Maintenance Outage 1 M47 to replace the '0' safety/relief valve which exhibited degrading first stage pilot valve leakage.
Operational Condition (OPCON) 4 (Cold Shutdown) was achieved on December 18. On December 20, the 'B' recirculation pump motor-generator motor faulted during startup of the 'B' recirculation pump in preparations for a reactor startup. Following replacement of the motor, a reactor startup was commenced on December 26. The unit returned to 100 percent power on December 31. Unit 1 remained at or near 100 percent power for the remainder of the inspection period.
Unit 2 began the inspection period at 100 percent power. On December 23, operators reduced power to approximately 92 percent to facilitate main turbine valve testing, secondary plant planned maintenance, and control rod hydraulic control unit maintenance. Operators returned the unit to 100 percent power on December 24, and the unit remained at or near 100 percent power for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, ,and Barrier Integrity
1R01 Adverse Weather Protection
Readiness for Seasonal Extreme Weather Conditions
a. Inspection Scope
The inspectors performed a review of Exelon's readiness for the onset of seasonal cold weather. The review focused on the emergency service water (ESW) system, the residual heat removal service water (RHRSW) system, and other equipment located in the site's Spray Pond Pump House. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR). technical specifications, contml room logs, and the corrective action program to determine what temperatures or other seasonal weather could challenge these systems. and to ensure Exelon personnel had adequately prepared for these challenges. The inspectors reviewed station procedures, including Exelon's seasonal weather preparation procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during cold weather conditions. Documents reviewed for each section of this inspection report are listed in the Attachment.
b. Findings
No findings were identified.
1R04 Equipment Alignment
.1 Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial walkdowns of the following systems:
- Emergency Diesel Generator (EDG) D24 on October '19 during the overhaul of EDG D21
- Unit 2 reactor core isolation cooling (RCIC) system when the high pressure coolant injection (HPCI) system was out-of-service on December 21
- Offsite Power Source and 4 Kilo-Volt Safeguard alignment during EDG D14 testing on December 29 The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, technical specifications, work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of theif intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Exelon staff had properly identified equipment issues and entered them into the corrective action program for resolution with the appropriate significance chara cterization.
b. Findings
No findings were identified .
.2 Full System Walkdown (71111 .04S - 1 sample)
a. Inspection Scope
On October 24 and 25, 2011, the inspectors performed a complete system walkdown of accessible portions of the common unit ESW system to verify the existing equipment lineup was correct. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, technical specifications, work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment. The inspectors performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. Additionally, the inspectors reviewed a sample of related issue reports (IRs) and work orders to ensure Exelon appropriately evaluated and resolved any deficiencies.
b. Findings
No findings were identified.
1R05 Fire Protection
Resident Inspector Quarterly Walkdowns (71111.05Q - 3 samples)
a. Inspection Scope
The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that Exelon controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The! inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.
- Fire Area 5, F-A-360, Unit 2 Class 1E Battery Room
- Fire Area 30, F-R-400, Unit 1 Drywell
- Fire Area 85, F-D-315B, D22 Diesel Generator Room
b. Findings
No findings were identified.
1R07 Heat Sink Performance (711111.07 A - 1 sample)
a. Inspection Scope
The inspectors reviewed the Unit 1 'F' Residual Heat Removal (RHR) room unit cooler to determine its readiness and availability to perform its safety function. The inspectors reviewed the design basis for the component and verified Exelon's commitments to NRC Generic Letter 89-13. The inspectors reviewed the results of inspections and tests of the unit cooler, and verified that Exelon initiated appropriate corrective actions for identified deficiencies. The inspectors also verified that the number of tubes plugged within the heat exchanger did not exceed the maximum amount allowed.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification
.1 Quarterly Review of Licensed Operator Requalification Testing and Training (71111.11 Q
-1 sample)
a. Inspection Scope
The inspectors observed licensed operator simulator training scenarios on November 22 which included inadvertent containment isolations, equipment failures requiring a rapid plant shutdown, failure of the reactor protection system, and failures of emergency core cooling systems. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the technical specification action statements entered. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.
b. Findings
No findings were identified .
.2 Annual Operator Requalification Program Review
a. Inspection Scope
On November 14, one NRC region-based inspector conducted an in-office review of results of licensee-administered annual operating tests and comprehensive written exams for 2011. The inspection assessed whether pass rates were consistent with the guidance of NRC Manual Chapter 0609, Appendix I, "Operator Requalification Human Performance SDP." The inspectors verified that:
- Crew pass rates were greater than 80 percent (Pass rate was 100 percent)
- Individual pass rates on the written exam were greater than 80 percent (Pass rate was 92 percent)
- Individual pass rates on the job performance measures of the operating exam were greater than 80 percent (Pass rate was 100 percent)
- More than 75 percent of the individuals passed all portions of the exam (92 percent of the individuals passed all portions of the examination)
- Individual pass rates on the dynamic simulator test were greater than 80 percent (Pass rate was 100 percent)
- Overall pass rate among individuals for all portions of the exam was greater than or equal to 75 percent (Overall pass rate was 92 percent)
b. Findings
No findings were identified .
.3 Annual Limited Operator Requalification Program Review
a. Inspection Scope
On December 21, one NRC region-based inspector conducted an in-office review of results of licensee-administered annual operating tests and comprehensive written exams for Limerick and Peach Bottom Limited Senior Reactor Operators for 2011. The inspection assessed whether pass rates were consistent with the guidance of NRC Manual Chapter 0609, Appendix I, "Operator Requalification Human Performance SOP."
The inspector verified that:
- Individual pass rates on the written exam were greater than 80 percent (Pass rate was 100 percent)
- Individual pass rates on the job performance measures of the operating exam were greater than 80 percent (Pass rate was 91 percent)
- More than 75 percent of the individuals passed all portions of the exam (i00 percent of the individuals passed all portions of the examination) .
- Overall pass rate among individuals for all portions of the exam was greater than or equal to 75 percent (Overall pass rate was 91 percent)
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structures, systems, and components (SSCs) performance and reliability. The inspectors reviewed system health reports, corrective action program documents, maintenance work orders, and maintenance rule basis documents to ensure that Exelon was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 Code of Federal Regulations (CFR) 50.65 and verified that the (a)(2) performance criteria established by Exelon staff was reasonable. As applicable, for SSCs classified as (a)(1),the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2). Additionally, the inspectors ensured that Exelon staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.
- IR 1191498, Unit 1 Main turbine stop valve #3 failed to close from main control room during testing
- IR 1231487, Unit 1 HPCI control valve failure
- IR 1275643, Standby gas treatment system relay surveillance test failure
b. Findings
No findings were identified.
1R 13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 5 samples)
a. Inspection Scope
The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that Exelon performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that Exelon personnel performed risk assessments as required by 10 CFR 60.65(a)(4) and that the assessments were accurate and complete. When Exelon performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk.
The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the station's probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
- Yellow risk on Unit 1 due to 'A' reactor enclosure recirculation system and standby gas treatment system surveillance testing with both Unit 1 HPCI room coolers out-of service for ESW valve work on October 11
- Green risk on Unit 1 while both '0' core spray pump unit coolers were out-of-service on October 12
- Yellow risk on Unit 1 while the HPCI system was out-of-service for governor tuning and the 'A' standby gas treatment system was out**of-service during an extended system outage window on October 24 fd
- Emergent maintenance on the 3 offsite power source on November 8 due to a switch yard bushing failure
- Yellow risk on Unit 2 while HPCI was out-of-servicE! for planned maintenance and Unit 1 was operating shutdown cooling in a maintenance outage on December 21
b. Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments
a. Inspection Scope
The inspectors reviewed operability determinations and functionality assessments for the following degraded or non-conforming conditions:
- IR 1140215, Unexpected shift in '8' loop ESW flow
- IR 1280748, EDG 024 frequency oscillations during load reject testing
- IR 1282425, Unit 2 feedwater leading edge flow meter indicated less flow than other plant parameters during surveillance testing
- IR 1292570, Reduced RHRSW and ESW flow discovered during ESW flow balance testing
- IR 1294806, Motor-driven fire pump automatic start due to suspected fire system leak The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and UFSAR to Exelon's evaluations to determine whether the components or systems were operable.
Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by Exelon. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.
b. Findings
No findings were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions.
- C0238106, Standby gas treatment system charcoal filter outlet isolation valve (HV 076-012A-OP) Oil Change and Pressure Switch Calibration
- C0239796, Replace Unit 1 main steam safety/relief valve PSV-041-1 F0130
- C0240449, Replace 022 EOG LSA relay
- C0240530, Replace battery cells 36 and 45 for 20 battery
- IR 1275643, Unexpected results during standby gas treatment system ST-2-072 107-0
- R 0859511, Replace Unit 2 'A' reactor enclosure recirculation system damper (HV 076-252-0P) solenoid valve
- R 1144306, 021 EDG 24-month overhaul
- R 1150960, Clean and examine residual heat removal unit cooler 1F-V210
- R 1170641, InspecURework '0' core spray pump room unit cooler supply valve
- R 1187754, Rebuild control rod drive hydraulic control unit waterside components for control rod 02-23
b. Findings
Introduction.
The inspectors identified a Green NCVof 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for failure to implement adequate corrective actions for a previous NRC-identified finding. The previous finding involved a failure to perform adequate PM on an EDG due to site engineers not being fully aware of new PM requirements developed by Exelon corporate engineers. The lack of proper PM led to a failure of an EOG in May 2010. In response to the previous finding, Limerick performed an ACE and developed actions to address the causes and extent of condition. However, the inspectors identified that the actions were not properly implemented by Exelon, and, as a result, the deficiency identified by the inspectors was not fully resolved.
Description.
In November 2010, the NRC issued NCV 05000352, 353/2010004-03 to Limerick following a catastrophic failure of the 023 EDG. Limerick's investigation had attributed the diesel failure to degraded operation of the lube oil Filter bypass valves, and had identified that the station was not conducting thorough inspections of the valves as required by Exelon's Performance Centered Maintenance (PCM) template for the diesel.
The NRC inspectors followed-up by questioning why the inspections were not being performed, and discovered that the site engineers had never been informed of the inspection requirement when it was added to the template. Exelon corporate engineers had added the detailed inspection guidance to the basis section of the PCM template, but relied on an internet tool to communicate the change to the site engineers. The internet tool compared new template revisions to former ones, and highlighted any PM tasks that had changed. The inspectors identified that the tool only highlighted tasks whose titles or frequencies had been revised; it did not highlight tasks if only the basis had changed. The inspectors determined that Exelon's flawed internet tool had resulted in Limerick site engineers not being fully informed of the new inspection guidance added to the basis of the PCM template. As a result, they did not implement new PM guidance for the lube oil bypass valve inspection, and did not prevent the 023 EOG failure in May 2010. The inspectors documented a Green NRC-identified NCV for Exelon's failure to provide an adequate procedure for PM of the Limerick EDG lube oil filter bypass valves.
In response to the NRC finding, Limerick wrote IR 1114118 and performed an ACE to determine why the PCM template revision had not been fully implemented at Limerick.
The ACE confirmed the inspectors' observations, concluding that "the tool used by site engineering to identify changes in a new revision of a PCM template did not highlight changes to the basis for a PM task." The ACE also identified that the tool did not highlight changes made to the notes section or the comments section of a PCM template. Because the issue affected all sites in the fleet, Exelon corporate engineering generated IR 1126485 to evaluate the PCM template process and establish appropriate corrective actions.
The inspectors' review of IRs 1114118 and 1126485 determined that Exelon did not implement adequate corrective actions to address PCM template process weaknesses.
Specifically, two of the six actions listed in the ACE were not implemented as intended:
1. Corrective Action 1126485-02 was to revise MA-AA-716-210, "Performance Centered Maintenance Process," to explicitly require that changes to a PCM template be summarized in a revision summary note so that the changes are clearly communicated. When Exelon corporate implemented this action, they added the following step to the procedure: "4.14.8. PROVIDE a summary of all changes to the Task, Frequency and Basis associated with the revision." The inspectors noted that this step did not require the summary to include changes to the notes or comments section of the PCM template, although Limerick's ACE identified that the notes and comments sections were also not being highlighted by the online tool.
2. Assignment 1126485-03 was for Exelon corporate to review the changes made
since the implementation of each PCM template and identify any changes that may require further evaluation by the sites to verify they were properly implemented. (The review was intended to focus on changes made to the basis, notes, and comments sections, and to address thE! other potential vulnerabilities.)
This assignment was closed on September 2, 2011, without the required review being conducted. Exelon reviewed only the templates that were recently revised and in the process of implementation, although they were tasked with looking back at all PCM templates.
On October 31, 2011, during performance of a surveillance test (ST), the D22 EDG failed to swap from isochronous to droop mode. The licensee determined that contacts on the relay that controls this function (LSA) had failed to reposition, which meant that control of the engine could not be transferred to the main control room. D22 was declared inoperable, and a prompt investigation was performed. The investigation stated that the LSA relay had been installed since 1995, despite a note in the PCM template indicating the LSA relay should be replaced every 10 years at Limerick. The inspectors discovered that the note was not included in the original version of the PCM template, but was added in July 2006. The inspectors observed that this issue appeared very similar to the D23 EDG finding from May 2010. If Exelon had conducted a thorough extent of condition review under assignment 1126485-03, the fact that there was no 10 year replacement PM in place for the relay should have been identified.
Limerick wrote a new IR (lR 1312492) to document the inspectors' concerns. Exelon plans to implement a new internet tool for PCM templates, which will allow engineers to do a more thorough comparison of new template revisions to former ones. The new tool will capture changes to all fields, including the basis, notes, and comments. Exelon also plans to perform a thorough extent of condition review to identify all instances of technical information contained in basis, note, or comment fields, and ensure the information has been properly evaluated and implemented.
Analysis.
The inspectors determined that Exelon's failure to take adequate corrective actions for a previous NRC-identified NCV was a performance deficiency. The finding was more than minor because, if left uncorrected, it could become a more significant safety concern. Specifically, the issues identified by the :inspectors impacted Limerick's ability to establish and implement appropriate PM for equipment relied on for safe operation of the plant. Until the issues are fully resolved, Limerick continues to be vulnerable to gaps in their PM program. This issue affects all sites in the Exelon fleet, since the PCM template process is common to all plants. This finding affected the Mitigating Systems cornerstone and was evaluated using Phase 1, "Initial Screening and Characterization" worksheet in Attachment 4 to IMC 0609, "Significance Determination Process." The inspectors determined this finding was of very low safety significance (Green) because the incomplete corrective actions from the ACE under IR 1114118 did not result in an actual loss of safety function of a component, train, or system, and was not potentially risk-significant due to a seismic, fire, flooding, or severe weather initiating event.
This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because Exelon failed to implement appropriate corrective actions for a previous NRC-identified finding in timely manner. P.1(d)
Enforcement.
10 CFR Part 50, Appendix B, Criterion XVI., "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to the above, Exelon failed to take adequate actions in response to a previous NRC-identified finding. Specifically, in November 2010, Exelon received a Green, NRC-identified NCV for failing to provide an adequate procedure for PM of the Limerick EDG lube oil filter bypass valves. (NCV 05000352,353/2010004-03). Exelon performed an ACE under IR 1114118 and developed several actions to address the causes and extent of condition. The inspectors identified that two of the actions were not completed as intended, which resulted in the deficiency identified by the inspectors not being fully resolved and failure of the D22 EDG during a surveillance test on October 31, 2011. Because the issue is of very low safety significance (Green), and Exelon entered this issue into their CAP as IR 1312492, this finding is being treated as an NCV consistent with the NRC Enforcement Policy. (NCV 05000352,353/2011005-01, Inadequate Corrective Actions for a Previous NRC Finding for Programmatic Deficiencies in the Preventive Maintenance Program)
1R20 Refueling and Other Outage Activities
a. Inspection Scope
The inspectors reviewed the station's work schedule and outage risk plan for the Unit 1 maintenance outage (1 M47) which was conducted December 18, 2011 through December 27,2011. The main purpose for the planned outage was to replace the '0' safety/relief valve which exhibited degrading first stage pilot valve leakage. In addition, the 'B' recirculation pump motor-generator motor was replaced due to an emergent failure. The inspectors reviewed Exelon's development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cool down processes and monitored controls associated with the following outage activities:
- Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable technical specifications wtlen taking equipment out of service
- Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing
- Configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting
- Status and configuration of electrical systems and switch yard activities to ensure that technical specifications were met
- Monitoring of decay heat removal operations
- Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss
- Activities that could affect reactivity
- Maintenance of secondary containment as required by technical specifications
- Fatigue management
- Identification and resolution of problems related to outage activities
b. Findings
No findings were identified.
1R22 Surveillance Testing (71111.22 6 samples)
a. Inspection Scope
The inspectors observed performance of surveillance tests (STs) and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied technical specifications, the UFSAR, and Exelon procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstratEld operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:
- RT-2-011-2S2-0, ESW Loop'S' Flow Salance
- RT-3-047-640-1, Fuel Channel Distortion Monitoring
- RT-6-051-702-1, Unit 1 'S' Residual Heat Removal Loop Contaminated Piping Inspection .
- ST-6-092-316-2, D22 Diesel Generator Fast Start Operability Test Run
- ST-6-0S1-235-1, Unit 1 'S' Residual Heat Removal Pump Comprehensive Test (1ST)
- RT-6-041-490-1, Suppression Pool Gross Input Leak Rate Determination (reactor coolant system (RCS) leak rate surveillance)
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstones: Occupational and Public Radiation Safety
2RS5 Radiation Monitoring Instrumentation
a. Inspection Scope
During the period of December 12 -16, the inspectors conducted the following activities to evaluate the operability and accuracy of radiation monitoring instrumentation used to ensure a safe work environment, and to detect and quantify radioactive process streams and effluent releases. Implementation of these programs was reviewed against the criteria contained in 10 CFR Part 20, applicable industry standards, and Exelon's procedures.
Walkdown of Process and Effluent Monitoring Systems The inspectors walked down selected portions of the liquid and gaseous monitoring systems installed in Unit 1 and Unit 2 to assess material condition and the status of system upgrades. The walkdown included the Unit 1 and Unit 2 South Stack gaseous effluent monitors and the site liquid radwaste monitor.
Calibration of Portable Survey Instruments, Contamination Monitors, Electronic Dosimeters, and Air Samplers The inspectors reviewed the operating procedure, calibration reports and current source activities/dose rate characterizations for the Shepherd Model 89 box calibrators (Nos.
8271 and 8268), and the dosimeter calibrator (Model 423) used for calibrating survey instruments and electronic dosimeters, respectively.
The inspectors reviewed the operating procedures and calibration records for selected survey meters, electronic dosimeters, and contamination monitors including small article monitors (9), personal contamination monitors (ARGOS SA/B & PM-7), airborne contamination monitors (AMS-4), and portable instruments (RO-2, RO-2A, RSO-SOE, Telepole, ASP-1/NRD). For these instruments, the inspectors observed technicians perform daily operational source checks. The inspectors confirmed that procedural requirements were met and that the instruments had the required accuracy.
During walkdowns in various plant areas, the inspectors confirmed that available monitoring instruments were calibrated, that daily source checks had been performed, and that the instruments were operational. Instruments checked included handheld survey instruments, electronic dosimeters, air monitors, and contamination monitors.
The inspectors reviewed contamination sampling results (10 CFR Part 61 radionuclide analyses) used to characterize difficult-to-measure radioisotopes, to determine if the calibration sources were representative of the radioisotopes found in the plant's source term. Whole body counting system records and contamination monitor setpoints were reviewed to determine if source term data was incorporated in system setup to ensure that relevant radioisotopes were accounted for when making measurements.
Laboratory instrumentation The inspectors reviewed the calibration records, daily source checks and maintenance records for selected gamma spectroscopy systems (Detectors Nos. 1, 2, 3, and 4) and a beta scintillation counter (Packard TriCarb 2900TR ) to verify that the instruments were calibrated and properly maintained. The inspectors confirmed that the check sources used aligned with the plant's isotopic mix and the instruments met the operability acceptance criteria.
Whole Body Counters The inspectors reviewed the calibration and operating procedure for the FastScan and AccuScan whole body counting systems. The inspectors determined that appropriate radioactive source phantoms were used in making calibrations and that calibration sources were representative of radioisotopes found in the plants' source term.
Plant Process and Post-Accident Monitoring Instrumentation The inspectors reviewed the calibration/functional test records for various areas, liquid and gaseous effluent instruments installed in Unit 1 and Unit 2. Records reviewed included the drywell high range radiation monitors, liquid radwaste discharge monitor, plant vent wide range monitors, north and south stack effluent monitors, and hot maintenance shop exhaust radiation monitors. The inspectors reviewed electronic and radiation source calibrations to determine whether they were appropriately conducted and that the alert and high alarm set points were properly established.
Problem Identification and Resolution The inspectors reviewed selected IRs, system health reports, self~assessments, and various Nuclear Oversight reports to evaluate Exelon's threshold for identifying, evaluating, and resolving problems for the radiation monitoring instrumentation.
Included in this review were IRs related to radiation worker and radiation protection technician errors to determine if an observable pattern traceable in the maintenance or use of radiation instruments was evident.
b. Findings
No findings were identified.
Cornerstone: Public Radiation Safety
2PS1 Radioactive Gaseous and Liquid Effluent Treatment (71124.06 ~ 1 sample)
a. Inspection Scope
During the period of November 14 - 17, the inspectors conducted the following activities to verify Exelon was properly maintaining the gaseous and liquid effluent processing systems to ensure that radiological releases were properly mitigated, monitored, and evaluated with respect to public exposure. Implementation of these controls was reviewed against the criteria contained in 10 CFR Parts 20 and 50, the licensee's Offsite Dose Calculation Manual (ODCM), and Exelon's procedures.
Effluent Reports, ODCM and UFSAR Reviews The inspectors reviewed the 2009 and 2010 Annual Radiological Effluent Release Reports (Nos. 35 and 36) to verify that the results of the effluents program were reported as required by the ODCM.
The inspectors reviewed the changes made to the ODCM, Revision 25, in 2010 to determine if the changes were technically justified and affected Exelon's ability to maintain effluent releases as low as is reasonably achievable.
The inspectors reviewed the current revision of the site UFSAR to determine if effluent treatment and monitoring systems had been reconfigured or modified.
Walkdown and Observations The inspectors examined portions of the Unit 1 and Unit 2 gaseous and liquid release monitoring systems to evaluate equipment material condition and system configurations.
The inspectors reviewed the most current system health reports for the process radiation monitoring systems and discussed the system status with the cognizant system engineer. The inspectors also reviewed the completed ST procedures associated with selected monitors that demonstrated instrument functionality. STs reviewed included:
Unit 1:
ST-2-026-400-1, South Stack Radiation Monitor, Unit 1 A ST-2-026-401-1, South Stack Radiation Monitor, Unit 1 B ST -2-026-442-1, South Stack Flow Rate Monitor Gal/Functional Test Unit 2:
ST-1-026-400-2, South Stack Radiation Monitor, Unit 2 A ST-2-026-401-2, South Stack Radiation Monitor, Unit 2 B ST-2-026-442-2, South Stack Flow Rate Monitor Gal/Functional Test Unit 1 & 2:
ST-2-026-414/415-0, North Stack Radiation Monitor Gal/Functional Test AlB ST-2-026-440-0, North Stack Flow Rate Monitor Gal/Functional Test ST-2-026-438-0, Wide Range North Stack Monitor Gal/Functional Test ST-2-063-400-0, Liquid Effluent Radiation Monitor Gal Functional Test ST-2-063-600-0, Liquid Effluent Radiation Monitor Quarterly Functional Test ST-2-063-601-0, Liquid Effluent Radiation Monitor Gal/Functional Test ST-2-063-602-0, Liquid Effluent Flow Rate Monitor Gal/Functional Test The inspectors reviewed the most current liquid and gaseous effluent monitor functional test results and calibration records to verify that the associated isolation functions and alarms were operable. The inspectors evaluated the effluent radiation monitor set pOints for agreement with the aDGM requirements.
Sampling and Analysis The inspectors reviewed the relevant ST procedures (S1-5-076-815-0/1/2) and associated sampling procedure (GY-LG-170-202) and observed a technician collecting weekly air particulate filter and iodine cartridge samples from the Hot Maintenance Shop, the North Stack monitors, the South Stack monitors, and the Wide Range Gas Monitor.
The inspectors reviewed the quality control records for laboratory counting instrumentation (Gamma Detectors Nos. 1, 2, 3, and 4) used to characterize and quantify effluent samples to determine jf the instruments met the required operating parameters.
The inspectors reviewed the ground water sampling procedure and observed a contractor technician obtain the quarterly sample taken from an on-site monitoring well (MW-9).
The inspectors reviewed the results of Exelon's inter-laboratory (cross check)comparison program to verify the accuracy of effluent sample analyses.
Air Gleaning System The inspectors reviewed the air cleaning system ST results for the high efficiency particulate air (HEPA) and charcoal filtration systems installed in Unit 1 and Unit 2.
Systems reviewed included the A & B Standby Gas Treatment Systems, Radwaste Enclosure Compartment Exhaust, A & B Turbine Enclosure Equipment Compartment Exhaust, and the A & B Reactor Enclosure Equipment Exhaust. The inspectors confirmed that the air flow rates were consistent with the UFSAR values ..
Dose Calculations The inspectors reviewed liquid and gaseous effluent monthly, quarterly, and annual dose calculations for calendar years 2009 and 2010, to ensure that the licensee properly calculated the offsite dose from effluent releases, in accordance with the ODCM, and to determine if any performance indicator (criteria contained in Appendix I of 10 CFR Part 50) was exceeded.
The inspectors reviewed three
- (3) liquid waste and three
- (3) gaseous waste discharge permits to verify that the projected doses were properly calculated using representative samples from the associated waste stream.
The inspectors reviewed and discussed with the licensee the validation and verification results for the effluent software (OpenEMS) to ensure the software in use provides accurate dose calculations.
Problem Identification and Resolution The inspectors reviewed relevant IRs and an Effluents Control Program self-assessment (LS-AA-126-1 001) to evaluate the licensee's effectiveness in identifying, evaluating, and resolving effluent control issues. This review was conducted against the criteria contained in 10 CFR Part 20, technical specifications, and the Exelon's procedures.
b. Findings
No findings were identified.
OTHER ACTIVITIES
40A1 Performance Indicator Verification (71151)
.1 Mitigating Systems Performance Index (2 samples)
a. Inspection Scope
The inspectors reviewed Exelon's submittal of the Mitigating Systems Performance Index for the Units 1 and 2 Cooling Water System (I\IIS1 0) for the period of October 1, 2010 through September 30,2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute (NEJ) Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors also reviewed Exelon's operator narrative logs, IRs, mitigatin~l systems performance index derivation reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.
b. Findings
No findings were identified .
.2 RCS Specific Activity and RCS Leak Rate (4 samples)
a. Inspection Scope
The inspectors reviewed Exelon's submittal for the RCS specific activity (8101) and RCS leak rate (8102) performance indicators for both Unit 1 and Unit 2 for the period of October 1, 2010 through September 30, 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors also reviewed RCS sample analysis and control room logs of daily measurements for RCS leakage, and compared that information to the data reported by the performance indicator.
b. Inspection Findings No findings were identified .
.3 Occupational Exposure Control Effectiveness (1 sample)
a. Inspection Scope
The inspectors reviewed implementation of the licensee's Occupational Exposure Control Effectiveness Performance Indicator (OR01) Program for the period of January 2011 through December 14, 2011. Specifically, the inspectors reviewed dosimetry alarm reports, IRs, and associated documents, for occurrences involving locked high radiation .
areas, very high radiation areas, and unplanned exposures against the criteria specified in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, to verify that all occurrences that met the NEI criteria were identified and reported.
b. Findings
No findings were identified.
40A2 Problem Identification and Resolution (71152 - 4 samples: 1 semi-annual trend review, 1 operator workaround annual sample, and 2 in depth review samples)
.1 Routine Review of Problem Identification and Resolution Activities
a. Inspection Scope
As required by Inspection Procedure 71152, "Problem Identification and Resolution," the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that Exelon entered issues into the corrective action program at an appropriate threshold. gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the corrective action program and periodically attended IR screening meetings.
b. Findings
No findings were identified .
.2 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a semi-annual review of site issues, as required by Inspection Procedure 71152, "Problem Identification and Resolution," to identify trends that might indicate the existence of more significant safety issues. In this review, the inspectors included repetitive or closely-related issues that may have been documented by Exelon outside of the corrective action program, such as trend reports, performance indicators, major equipment problem lists, maintenance rule assessments, and maintenance or corrective action program backlogs. The inspectors also reviewed Limerick's corrective action program database for the third and fourth quarters of 2011 to assess IRs written in various subject areas (equipment problems, human performance issues, etc.), as well as individual issues identified during the NRCs daily IR review (Section 40A2.1). The inspectors reviewed the Limerick's quarterly PerformanCE! Improvement Integrated Matrix report for the third quarter of 2011, conducted under PI-AA-1001, "Performance Improvement Integrated Matrix, Revision 1," to verify that Limerick personnel were appropriately evaluating and trending adverse conditions in accordance with applicable procedures.
b. Findings and Observations
No findings were identified.
The review did not reveal any trends that could indicate a more significant safety issue.
The inspectors assessed that Exelon was identifying issues at a low threshold and entering the issues into the CAP for resolution.
The inspectors performed a review of Exelon's actions in response to a negative trend identified in NRC Inspection Report 05000352, 353/2011003, dated August 4, 2011.
The negative trend was associated with not entering plant issues and events into the CAP in a timely manner. The issues involved were isolated to the Operations and Maintenance departments.
Exelon entered the NRC-identified trend as well as other similar issues into the CAP as IR 1237270 and performed a common cause analysis. Exelon identified that there was a mindset that issues encountered during the performance of a work document (IR or work order) or during the performance of a procedure would be addressed as part of the initial work order document closeout or procedure changls process document. Exelon detenmined that the established mindset represented an opportunity for improvement in the generation of IRs. Maintenance, Operations, and Engineering supervision conducted briefings with department personnel to reinforce timely IR generation and to reemphasize the threshold for IR generation. The inspectors determined that Exelon's actions were reasonable and were apparently effective based on no significant occurrences during the review period where plant issues or events were not entered into the CAP .
.3 Annual Sample: Review of the Operator Workaround Program
a. Inspection Scope
The inspectors reviewed the cumulative effects of the existing operator workarounds, operator burdens, existing operator aids and disabled alarms, and open main control room deficiencies to identify any effect on emergency operating procedure operator actions, and any impact on possible initiating events and mitigating systems. The inspectors evaluated whether station personnel had identified, assessed, and reviewed operator workarounds as specified in Exelon procedure OP-AA-1 02-1 03, "Operator Work-Around Program," Revision 3.
The inspectors reviewed Exelon's process to identify, prioritize and resolve main control room distractions to minimize operator burdens. The inspectors reviewed the system used to track these operator workarounds and recent Exelon self assessments of the program. The inspectors also toured the control room and discussed the current operator workarounds with the operators to ensure the items were being addressed on a schedule consistent with their relative safety significance.
b. Findings and Observations
No findings were identified.
The inspectors determined that the issues reviewed did not adversely affect the capability of the operators to implement abnormal or emergency operating procedures.
The inspectors also verified that Exelon entered operator workarounds and burdens into the CAP at an appropriate threshold and planned or implemented corrective actions commensurate with their safety significance .
.4 Annual Sample: Reactor Recirculation Motor Generator (RRMG) Set Issues
a. Inspection Scope
The inspectors performed an in-depth review of Exelon's evaluations and corrective actions associated with RRMG issues. Specifically, sincE~ 2009, the RRMGs have tripped or changed speed without operator demand on sEweral occasions.
A RRMG provides a variable frequency power supply to a reactor recirculation pump (RRP) motor. The RRMG consists ofa constant speed motor coupled to an alternating current (AC) generator through a fluid coupler. The recirculation flow control system positions a scoop tube in the fluid coupler which changes the speed of the AC generator.
This in turn changes the speed of the reactor recirculation pump (RRP). The RRPs are used to change power level in the reactor by adjusting the flow of water through the reactor core.
The inspectors assessed Exelon's problem identification threshold, cause analyses, extent of condition reviews, compensatory actions, and the prioritization and timeliness of Exelon's corrective actions to determine whether Exelon was appropriately identifying, characterizing, and correcting problems associated with this issue and whether the planned and completed corrective actions were appropriate. The inspectors compared the actions taken to the requirements of Exelon's corrective action program. In addition, the inspectors performed field walkdowns and interviewed engineering personnel to assess the effectiveness of the implemented corrective actions.
b. Findings and Observations
No findings were identified.
In response to several events where RRMGs changed speed without operator demand (undemanded speed changes), Exelon preformed a common cause analysis in June 2009. Corrective actions included; determining the age criterion for replacement of circuit components, and determining a strategy for old and obsolete circuit cards.
Exelon also performed an effectiveness review as part of their common cause analysis and appropriately determined that the corrective actions had not been effective and subsequent evaluation was necessary.
The 2A RRMG tripped twice in late 2010, which prompted Exelon to perform a root cause evaluation (I Rs 1129709 and 1148152). The root cause for the 2A RRMG trips was attributed to the voltage regulator card. After replacement of the voltage regulator card, the specific problem has not reoccurred.
Based on several other undemanded speed changes, an apparent cause evaluation was completed in March 2011 (IR 1184004). The apparent cause was associated with the amplifier cards. Based on minor undemanded speed changes, the 1A, 2A, and 2B RRMGs were assigned adverse condition monitoring plans to provide guidance for monitoring the RRMGs' performance and to provide actions to address any abnormal behavior. The 2B RRMG experienced several undemanded speed changes while under the adverse condition monitoring plan, so the scoop tube for the 2B RRMG was locked.
While locked it can be operated manually and all undemanded speed changes are prevented.
In 2005, as a long term corrective action, Exelon began the process for replacing the current RRMGs with adjustable speed drives. The modification will replace all components of the existing systems. The modifications were given high priority and are scheduled to be complete by 2012 on Unit 1 and 2013 on Unit 2.
The inspectors reviewed the troubleshooting methodologies, cause evaluations, and modification for RRMG replacement and did not identify any additional issues. The inspectors determined Exelon's overall response to the issues were commensurate with the safety significance, were timely. and included appropriate compensatory actions.
The inspectors determined that the actions taken were masonable to resolve the RRMG issues .
.5 Annual Sample: 13kV Cable Failures
a. Inspection Scope
The inspectors performed an in~depth review of Exelon's evaluations and corrective actions associated with IR 1051496, 1083732, and 1144472 for 13kV cable failures.
Specifically, in 2010, Limerick experienced three separate cable failures on non-safety related 13kV power cables.
The inspectors assessed Exelon's problem identification threshold, problem analysis, extent of condition reviews, compensatory actions, and the prioritization and timeliness of Exelon's corrective actions to determine whether Exelol1 was appropriately identifying, characterizing, and correcting problems associated with this issue and whether the planned or completed corrective actions were appropriate. The inspectors compared the actions taken to the requirements of Exelon's CAP and Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B. The inspectors performed field walkdowns, and interviewed engineering and maintenance personnel to assess the effectiveness of the implemented corrective actions, the reasonableness of the planned corrective actions, and to evaluate the extent of anyon-going cable degradation problems. In addition, the inspectors reviewed Exelon's cable monitoring program, routine cable preventive maintenance testing, selected cable test results, and cable test and replacement schedules. Specific documents reviewed an3 listed in the attachment to this report.
In addition, the inspectors observed replacement activities for the 2D-P501 circulating water pump motor feeder cable, which had been previously identified as degraded by tan-delta testing in January 2011. Specifically, the inspectors observed a new 15kV rated cable being pulled from the switchgear to the pump motor, and reviewed the post installation tan-delta test results.
b. Findings and Observations
No findings of significance were identified.
Exelon determined that the most probable cause of the cable failures was manufacturing defects of the Anaconda ethylene propylene rubber UniShield 15kV rated cable.
Specifically, Exelon stated that an examination of a failed Anaconda cable by the Electric Power Research Institute identified water tree damage and distributed deterioration due to voids and contamination of the cable's insulating material which occurred during the manufacturing process. Exelon's corrective actions included routine cable tan-delta testing, very low frequency withstand testing, replacement of selected cables based on test results, and installation of a cable manhole water detection system to facilitate maintaining underground cables in a dry environment.
The inspectors reviewed selected IRs and cable test results for Anaconda 15kV rated cables and did not identify any additional issues. The inspectors determined Exelon's overall response to the issue was commensurate with the safety significance and included appropriate compensatory actions. The inspectors determined that the actions taken or planned were reasonable to resolve the identified cable issues.
Notwithstanding, the inspectors did identify a weakness in Exelon's cable monitoring program. Exelon had not established or implemented written procedures or instructions to perform cable tests, such as a tan-delta or very low fre,quency withstand test, and had not established approved acceptance criteria. The inspectors determined this was a minor issue because maintenance personnel responsible for the testing were knowledgeable of the test methods and industry standards used for evaluation of the test results; plant engineering personnel reviewed test results; and test results indicative of cable degradation were routinely entered into the CAP for further evaluation. Exelon entered the inspector's observations into their CAP (IR 1284994).
In addition, the inspectors also identified a weakness in Exelon's cable installation program. As part of the modification process to replace a non-safety related medium voltage cable, Exelon engineering calculated the expected cable pulling tension and compared it to the maximum allowable tension specified by the cable manufacturer to ensure that no cable mechanical damage would occur during installation. The maximum tension at the end of the pull was calculated to be approximately 2,973 pounds, as compared to the manufacturer's limit of 10,000 pounds. Based on the large margin between the calculated value and the limit, Exelon engineering authorized a deviation from normal plant procedures and allowed installation without monitoring the actual pulling force with a dynamometer or tension-meter. In addition, Exelon engineering did not evaluate or specify the pulling method, such as by basket grip on the cable jacket or by pulling eye attached directly to the cable conductor. The inspectors observed that a cable tugger, rated at 8,000 pounds force maximum, was attached to the cable with a basket grip. The inspectors noted that the cable manufacturer specified that the maximum pulling force should not exceed 1,000 pounds if a basket grip were used. In addition, E-1412, "Wire and Cable Notes and Details," sp(~cified that the maximum pulling force with a basket grip was limited to 1,500 pounds. The inspector determined this was a minor issue because Exelon subsequently determined that the installation method was acceptable, based on additional information from the cable manufacturer for the pulling forces used. Exelon entered the inspectors' observations into their CAP (IR 1282881).
40A5 Other Activities
.1 Followup on Traditional Enforcement Actions Including Violations, Deviations,
Confirmatorv Action Letters, Confirmatorv Orders, and Alternate Dispute Resolution Confirmatorv Orders (IP 92702 - 1 sample)
a. Inspection Scope
On December 23,2010, the NRC issued a Severity Level IV NCVof 10 CFR 50.71 (e),
"Maintenance of Records, Making of Reports," when Exelon failed, on mUltiple occasions, to revise the UFSAR with information consistent with plant conditions.
Specifically, Exelon personnel failed to incorporate four previously identified UFSAR inconsistencies into the September 2010 UFSAR update as required. This issue was identified as NCV 05000352, 353/2010007~01, "Failure to Update UFSAR Consistent with Plant Conditions as Required."
The objective of the inspection was to determine whether adequate corrective actions have been implemented for traditional enforcement actions including violations. To assess and document Exelon's corrective actions regarding the issued violation, the region elected to conduct IP 92702 and formally informed Exelon of the NRC's intent to conduct this inspection via the NRC Mid-Cycle letter dated September 1, 2011 (ML112411354).
The inspectors reviewed Exelon's ACE, related IRs, self-assessment and audit reports, procedures and relevant references. The inspectors confirmed that the outstanding changes identified in the NCV and others identified during an extent of condition review were properly processed and incorporated into the next UFSAR revision submittal. The inspectors conducted interviews with a member of the Station Ownership Committee and staff from the Engineering, Regulatory Assurance, Nuclear Oversight, Chemistry and Radiation Protection departments. The inspectors conducted an extent of condition evaluation to assess the U FSAR update program. The program was evaluated for adequacy of identification and change processing timeliness of required UFSAR changes.
b. Findings and Observations
No findings of significance were identified.
The inspectors observed that while initial corrective actions were implemented to address the NCV, subsequent internal self-assessment and follow-up activities performed by the station's Nuclear Oversight organization identified that a lack of knowledge and ownership of the UFSAR change process still existed at the station.
Additional corrective actions generated from those observations included performance of an ACE, creation of a read and sign to reinforce management expectations, and further procedure enhancements. The inspectors determined that Exelon's corrective actions were appropriate to ensure required changes were incorporated into UFSAR revision submittals to the NRC .
.2 NRC Review of Exelon's Response to Non-Cited Violation EA-11-128 (IP 92702-1
sample)
a. Inspection Scope
On September 12, 2011, the NRC transmitted an NCV and a Green finding to Exelon related to a change Exelon made to the emergency action level (EAL) basis for EAL HU6, which introduced a decrease in effectiveness to Limerick's Emergency Plan and resulted in a violation of the requirements stipulated in 10 CFR 50.54(q). Specifically, the licensee modified the EAL Basis in EAL HU6, Revision 13, which extended the start of the 15-minute emergency classification clock beyond a credible notification that a fire is occurring or indication of a valid fire detection system alarm. This change decreased the effectiveness of the Emergency Plan by reducing the capability to perform a risk significant planning function in a timely manner. The NCV and finding were described in detail in NRC Inspection Report Nos. 05000352/2011503 and 05000353/2011503.
In response to the NCV and finding, Exelon entered the issue into their corrective action program as IR 01184333 and subsequently implemented Revision 20 of the Limerick Emergency Plan, which restored the EAL HU6 Basis to the Revision 12 guidance, thereby removing the decrease in effectiveness. The inspectors reviewed IR 01184333 and the revised version of the HU6 Basis, and discussed the corrective actions with the Limerick Emergency Preparedness staff.
b. Findings and Observations
No findings were identified. The inspectors determined that Exelon's response and corrective actions were reasonable and appropriate to address the NCV and finding, and their underlying performance deficiency. The NRC considers the issue to be closed.
40A6 lVIeetings, Including Exit On January 13, 2012, the inspectors presented the inspection results to Mr. William Maguire, Site Vice President, Limerick Generating Station, and other members of the Exelon staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.
ATTACHMENT:
SUPPLEMENTARY INFORMATION
KEY POINTS OF CONTACT
LIcensee Personnel
- W. Maguire, Site Vice President
- P. Gardner, Plant Manager
- C. Rich, Director of Operations
- D. Doran, Director of Engineering
- R. Kreider, Director of Maintenance
- P. Colgan, Director of Work Management
- C. Gerdes, Security Manager
- R. Dickinson, Director of Training
- K. Kemper, Manager Nuclear Oversight
- D. Merchant, Radiation Protection Manager
- J. Hunter, Manager, Regulatory Assurance
- C. Cooney, Chemistry/Radwaste Manager
- M. Gillin, Sr. Manager Engineering Systems
- R. Harding, Regulatory Assurance Engineer
- R. Rhode, LIcensed Operator Requalification Training Supervisor
- R. Higgins, Environmental Engineer
- R. Ruffe, Operations Training Manager
- J. Bendyk, Site Engineer, Ventilation
- L. Konen, Chemistry Technician
- B. Lance, Chemistry Manager
- M. Strawn, Nuclear Oversight
- A. Varghese, Site Engineer, Radiation Monitoring
- M. Ajmera, Nuclear Oversight
- P. Dunston, Regulatory Assurance Engineer
- D. Hocker, Work Management Cycle Manager
- A. Lambert, Design Engineer
- L. Parlatore, Radiation Protection Technician
- A. Rocco, System Engineer
- D. Ryan, Senior Chemist
- J. Duskin, Supervisor, Radiation Protection Instrumentation
- M. Gift, Plant Engineer
- R. Goskins, Instrument Technician
- P. Imm, Radiological Engineering Supervisor
- J. Ristetler, Supervisor - Radiation Protection
- S. Sweisford, Instrument Technician
- D. Cheung, Recirculation System Engineer
Other:
- M. Murphy, Inspector, Commonwealth of Pennsylvania
LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED
Opened/Closed
- 05000352, 353/2011005-01 NCV Inadequate Corrective Actions for a Previous NRC Finding for Programmatic Deficiencies in the Preventive Maintenance Program (Section 1R19)
Opened
None
Closed
- 05000352, 353/2011503-01 NCV (Traditional Enforcement) Changes to EAL Basis Decreased the Effectiveness of the Plan without Prior NRC Approval (40A5.2)
- 05000352, 353/2011503-02 FIN Changes to EAL Basis Decreased the Effectiveness of the Plan without Prior NRC Approval (40A5.2)
Discussed
- 05000352,353/2010007-01 NCV Failure to Update UFSAR Consistent with Plant Conditions as Required (Section 40A5.1)