ML24135A177

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Integrated Inspection Report 05000282/2024001 and 05000306/2024001
ML24135A177
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 05/15/2024
From: Richard Skokowski
NRC/RGN-III/DORS/RPB3
To: Conboy T
Northern States Power Company, Minnesota
References
IR 2024001
Download: ML24135A177 (1)


See also: IR 05000282/2024001

Text

Thomas A. Conboy

Site Vice President

Prairie Island Nuclear Generating Plant

Northern States Power Company, Minnesota

1717 Wakonade Drive East

Welch, MN 55089-9642

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT - INTEGRATED

INSPECTION REPORT 05000282/2024001 AND 05000306/2024001

Dear Thomas Conboy:

On March 31, 2024, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Prairie Island Nuclear Generating Plant. On April 9, 2024, the NRC inspectors discussed the

results of this inspection with you and other members of your staff. The results of this inspection

are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. One of these

findings involved a violation of NRC requirements. We are treating this violation as a non-cited

violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector

at Prairie Island Nuclear Generating Plant.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a

regulatory requirement in this report, you should provide a response within 30 days of the date

of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the

Regional Administrator, Region III; and the NRC Resident Inspector at Prairie Island Nuclear

Generating Plant.

May 15, 2024

T. Conboy

2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Richard A. Skokowski, Chief

Reactor Projects Branch 3

Division of Operating Reactor Safety

Docket Nos. 05000282 and 05000306

License Nos. DPR-42 and DPR-60

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

Signed by Skokowski, Richard

on 05/15/24

ML24135A177

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE

RIII

EICS

RIII

NAME

RElliott:gmp

DBetancourt-Roldan

via email

RSkokowski

DATE

05/14/2024

05/15/2024

05/15/2024

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000282 and 05000306

License Numbers:

DPR-42 and DPR-60

Report Numbers:

05000282/2024001 and 05000306/2024001

Enterprise Identifier:

I-2024-001-0078

Licensee:

Northern States Power Company

Facility:

Prairie Island Nuclear Generating Plant

Location:

Welch, MN

Inspection Dates:

January 01, 2024 to April 10, 2024

Inspectors:

M. Abuhamdan, Reactor Inspector

T. Ospino, Resident Inspector

K. Pusateri, Resident Inspector

D. Tesar, Senior Resident Inspector

Approved By:

Richard A. Skokowski, Chief

Reactor Projects Branch 3

Division of Operating Reactor Safety

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Prairie Island Nuclear Generating Plant,

in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Adequately Implement the Requirements of 10 CFR 50, Appendix B, Criterion XVI

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000282,05000306/2024001-02

Open/Closed

[P.3] -

Resolution

71111.20

The inspectors identified a Green finding and associated non-cited violation of Title 10 of the

Code of Federal Regulations (10 CFR), Part 50, Appendix B, Criterion XVI, Corrective

Action, associated with the licensees failure to correct conditions adverse to quality (CAQ).

Specifically, the inspectors identified that the licensee failed to take adequate corrective

actions to correct a CAQ. Consequently, this failure would have allowed a CAQ associated

with safety related structures, systems, and components (SSC's) to remain uncorrected

absent inspector intervention.

Failure to Provide Adequate Oversight to Supplementary Personnel Resulting in a Reactor

Trip

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

FIN 05000282,05000306/2024001-03

Open/Closed

[H.2] - Field

Presence

71153

The inspectors identified a Green finding when the licensee failed to meet the standards of

procedure FP-MA-COM-02, "Oversight and Control of Supplementary Personnel."

Specifically, the licensee failed to provide supplemental workers with an appropriate level of

oversight and engagement to ensure performance was commensurate with station standards

and expectations, resulting in a loss of all non-safeguards busses and a Unit 1 turbine and

reactor trip.

Additional Tracking Items

Type

Issue Number

Title

Report Section

Status

URI

05000306/2024001-01

Unresolved Item Associated

with Modifications to

Motor-Operated Valve Limit

Switch

71111.18

Open

LER

05000282,05000306/20

23-001-01

LER 2023-001-01 for Prairie

Island Nuclear Generating

Plant, Units 1 and 2, Reactor

Trip, Auxiliary Feedwater

71153

Closed

3

and Emergency Service

Water System Actuation due

to Electrical Transient in DC

Control Power Cables

LER

05000282,05000306/20

23-001-00

LER 2023-001-00 for Prairie

Island Nuclear Generating

Plant, Units 1 and 2, Reactor

Trip, Auxiliary Feedwater

and Emergency Service

Water System Actuation due

to Electrical Transient in DC

Control Power Cables

71153

Closed

4

PLANT STATUS

Unit 1 entered the inspection period shut down in Mode 3 (hot standby). Unit 1 went critical on

January 24, 2024, entered Mode 1 (power operation) on January 27, 2024, and reached

full-rated thermal power on January 29, 2024. Unit 1 was then shut down to Mode 3 to facilitate

repairs on a main feed pump discharge line on February 8, 2024. Unit 1 returned to critical on

February 11, 2024, entered Mode 1 on February 12, 2024, and reached full-rated thermal power

on February 14, 2024. Unit 1 maintained at or near full-rated thermal power for the remainder of

the inspection period.

Unit 2 entered the inspection period shut down for refueling outage 2R33. Unit 2 went critical on

February 29, 2024, reached Mode 1 on March 1, 2024, and reached 50 percent power on

March 2, 2024. Unit 2 subsequently tripped from 50 percent power and entered Mode 3 on

March 3, 2024. Unit 2 returned to critical on March 7, 2024, Mode 1 on March 8, 2024, and

reached full-rated thermal power on March 18, 2024. Unit 2 remained at or near full-rated

thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to

the onset of a winter storm for the following systems:

AB-2 entry for winter storm warning on January 11, 2024

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

D6 emergency diesel generator on January 3, 2024

(2)

C1.1.38 common fuel system status on January 4, 2024

5

(3)

D1/D2 diesel generators on March 11, 2024

(4)

Unit 2 auxiliary feedwater system on March 13, 2024

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

door 43 fire impairment and fire areas 8 and 32 on February 20, 2024

(2)

fire zone 82, D1 diesel room on March 11, 2024

(3)

fire zone 35, battery rooms 21 and 22 on March 13, 2024

(4)

fire zone 2, auxiliary feed pump room, elevation 695' on March 13, 2024

(5)

fire zone 1, battery rooms 11 and 12 on March 13, 2024

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the onsite fire brigade training and performance during an

unannounced fire drill for crew 5 on March 19, 2024.

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated internal flooding mitigation protections following failure of

door 43 to close on February 28, 2024.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(7 Samples)

(1)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 1 reactor startup on January 24, 2024.

(2)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 1 reactor shutdown for a steam leak on February 8, 2024.

(3)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 1 reactor startup from a forced outage on February 11, 2024.

(4)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 2 reactor startup from a refueling outage with source range NI failure

on February 20, 2024.

(5)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 2 reactor startup from a refueling outage on February 29, 2024.

(6)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 2 trip response on March 3, 2024.

(7)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 2 reactor startup from a forced outage on March 7, 2024.

6

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed and evaluated licensed operator requalification training

as-found testing on March 18, 2024.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (6 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

21 cooling water pump replacement on January 17, 2024

(2)

multiple trips CB401 breaker on 28 inverter on January 17, 2024

(3)

Corrective Action Plan (CAP) 501000079768, "ISI [inservice inspection] Indication

Evaluation for SP2168.13," on January 17, 2024

(4)

MV-32019 21 turbine driven auxiliary feedwater (TDAFW) pump steam inlet isolation

valve on January 18, 2024

(5)

Work Order (WO) 700087060, "22 TDAFW Pump Maintenance," on

February 22, 2024

(6)

condensate demineralizer review following Unit 2 reactor trip on March 4, 2024

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

operational decision-making instruction (ODMI) for Unit 1 startup on January 8, 2024

(2)

risk evaluation for transition from shutdown risk to online risk on January 15, 2024

(3)

risk associated with emergent issues on Unit 1 circulating water and impact on Unit 1

startup on January 18, 2024

(4)

extended operation in lowered inventory risk evaluation on February 6, 2024

(5)

ODMI & adverse condition monitoring plan for Unit 2 startup with 22 reactor coolant

pump (RCP) second seal degraded on February 29, 2024

(6)

risk management following Unit 2 trip and subsequent startup on March 4, 2024

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (8 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

reactor coolant system evaluation for Technical Specification 3.4.3 on

October 25, 2023

(2)

source range nuclear instrument seismic qualification on December 5, 2023

(3)

CAP 501000080389, "D6 Fuel Oil Leak Getting Worse," on January 3, 2024

7

(4)

past operability review MV-32019 21 TDAWF pump on January 11, 2024

(5)

application of Technical Specification Limiting Condition for Operation (LCO) 3.0.4.b

for mode change on January 25, 2024

(6)

bus 25/26 and bus 27 circuit breaker sequencing on February 6, 2024

(7)

prompt operability determination for D1/D2 HELP question on February 29, 2024

(8)

CAP 501000082220, "POD 50000327699 Unit 1 HELB," on March 6, 2024

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated refueling outage activities from January 1, 2024, to

March 1, 2024.

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system

operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (8 Samples)

(1)

WO 700133040, "CV-31321 Diaphragm Leaking (PMT/LLRT [local leak rate test]),"

on January 11, 2024

(2)

22 reactor coolant pump seal replacement PMT on January 17, 2024

(3)

22 turbine driven auxiliary feedwater pump PMT on January 31, 2024

(4)

WO 700087060, "22 Turbine Driven AFW [auxiliary feedwater] Pump Quarterly

Test - PMT," on February 18, 2024

(5)

WO 700127367, "MV-32016," on March 13, 2024

(6)

WO 700135613, "SP 2406 MSIV [main steam isolation valve] In Service Test," on

March 21, 2024

(7)

SP 1073B, "Monthly Train B Shield Building Ventilation System Test," on

March 25, 2024

(8)

WO 700133173, "SP 1106B 22 DDCL [diesel-driven cooling water] Pump

Comprehensive Test," on March 25, 2024

Surveillance Testing (IP Section 03.01) (4 Samples)

(1)

WO 700044983, "SP 1070 Rx Coolant Sys Integrity Test," on January 11, 2024

(2)

SP 2750, "Containment Close-out," on January 29, 2024

(3)

SP 2750, "Containment Close-out," on February 16, 2024

(4)

WO 700125323, "SP 1155B 12 Component Cooling Water Quarterly Surveillance,"

on March 20, 2024

Inservice Testing (IST) (IP Section 03.01) (1 Sample)

(1)

WO 700125737, "SP 1106C 121 Cooling Water Pump Quarterly Test," on

February 22, 2024

8

Reactor Coolant System Leakage Detection Testing (IP Section 03.01) (2 Samples)

(1)

LLRT total leak rate for Unit 2 2R33 refueling outage on October 6, 2023

(2)

SP 2070, "RCS Integrity Test Unit 2," on January 1, 2024

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)

(1)

Unit 1 (January 1, 2023, through December 31, 2023)

(2)

Unit 2 (January 1, 2023, through December 31, 2023)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1)

Unit 1 (January 1, 2023, through December 31, 2023)

(2)

Unit 2 (January 1, 2023, through December 31, 2023)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1)

Unit 1 (January 1, 2023, through December 31, 2023)

(2)

Unit 2 (January 1, 2023, through December 31, 2023)

71153 - Follow Up of Events and Notices of Enforcement Discretion

Event Follow up (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated site response to the Unit 1 trip on January 25, 2024.

Event Report (IP Section 03.02) (2 Samples)

The inspectors evaluated the following licensee event reports (LERs):

(1)

LER 05000282, 05000306/2023-001-00 for Prairie Island Nuclear Generating Plant,

Units 1 and 2, "Reactor Trip, Auxiliary Feedwater and Emergency Service Water

System Actuation due to Electrical Transient in DC Control Power Cables"

(ADAMS Accession No. ML23338A277). The inspection conclusions associated with

this LER are documented in this report under Inspection Results Section 71153. This

LER is closed.

(2)

LER 05000282, 05000306/2023-001-01 for Prairie Island Nuclear Generating Plant,

Units 1 and 2, "Reactor Trip, Auxiliary Feedwater and Emergency Service Water

System Actuation due to Electrical Transient in DC Control Power Cables"

(ADAMS Accession No. ML24081A153). The inspectors reviewed the updated LER

submittal. The previous LER submittal was also reviewed in this inspection report

under Inspection Results Section 71153. This LER is closed.

9

INSPECTION RESULTS

Unresolved Item

(Open)

Unresolved Item Associated with Modifications to

Motor-Operated Valve Limit Switch

URI 05000306/2024001-01

71111.18

Description:

During the 2R33 refueling outage, modifications were made to the safety related limit switch

installed on motor-operated valve, MV-32019, 21 steam generator main steam supply to the

22 turbine driven auxiliary feedwater pump. Specifically, the gears inside the replacement

switch were stainless steel rather than bronze (not like for like), the intermittent shaft had an

additional hole drilled through it perpendicular to the manufacturer provided hole, and the

orientation of the rotor was changed from that provided by the vendor.

Planned Closure Actions: Review licensee evaluation of the changes in material and the

modifications made to the limit switch, their impact on seismic qualification, and the potential

impact to operability.

Licensee Actions: Evaluate the impact of the differences in material and the impact of the

modifications made as well as the resultant impact on seismic qualification and potential

operability impacts.

Corrective Action References: 501000079553, "Bkr 211J-13 Tripped During PMT/RTS"

501000079667, "Manually Operated MV-32019 per COO-17"

501000081027, "MOV Limit Switch Grease Related Failures"

501000081105, "MV-32019 Thermals Tripped D"

501000083170, "LEGACY: MV-32019 Limit Switch Material"

501000083626, "MV-32019 Limit Switch"

Failure to Adequately Implement the Requirements of 10 CFR 50, Appendix B, Criterion XVI

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000282,05000306/2024001-02

Open/Closed

[P.3] -

Resolution

71111.20

The inspectors identified a Green finding and associated non-cited violation of Title 10 of the

Code of Federal Regulations (10 CFR), Part 50, Appendix B, Criterion XVI, Corrective

Action, associated with the licensees failure to correct conditions adverse to quality (CAQ).

Specifically, the inspectors identified that the licensee failed to take adequate corrective

actions to correct a CAQ. Consequently, this failure would have allowed a CAQ associated

with safety related structures, systems, and components )SSC's) to remain uncorrected

absent inspector intervention.

Description:

During the Prairie Island Unit 2 refueling outage, inspectors identified an example where the

licensee failed to take corrective actions adequate to resolve the condition adverse to quality

absent inspector intervention:

Preventive maintenance (PM) procedure, "PM 3132-1-22: 22 TDAFWP [Turbine Driven

Auxiliary Feedwater Pump] Minor Insp [Inspection]" step 7.10.2 specifies to Measure and

10

Document "As-Found" data in the corresponding table. The step is followed by the following

note: "RCE 01132098 indicates that proper coupling alignment is critical in preventing turbine

bearing failure. Deviations from the values listed in the Reference table must be evaluated by

the system engineer. The most critical dimension is the vertical offset value due to predicted

thermal expansion which would occur during turbine operation." The "As-Found" data

recorded in the table was outside of the values listed in the Reference table in both the

horizontal and vertical directions. Despite the note indicating that the values must be

evaluated by the system engineer, no CAP was written, and the PM was documented as

having been completed satisfactorily. Inspectors determined that this was a condition adverse

to quality, and the requisite corrective action to perform an engineering evaluation was not

performed, as required by procedure PM 3132-1-22.

Corrective Actions: The licensee has entered the item into the corrective action program and

completed the required actions to address the condition adverse to quality.

Corrective Action References: 501000082185

Performance Assessment:

Performance Deficiency: The licensee's failure to identify and correct a condition adverse to

quality, such as nonconformances and deficiencies, in accordance with 10 CFR 50,

Appendix B, Criterion XVI was a performance deficiency. Specifically, the inspectors

identified that during preventive maintenance procedure PM 3132-1-22: 22 "TDAFWP Minor

Insp," maintenance personnel recorded data which did not meet acceptance criteria, a

condition adverse to quality, and the requisite corrective action to perform an engineering

evaluation was not performed. Inspectors determined that the failure of the licensee to

identify and correct this CAQ was within the ability of the licensee to foresee and correct and

was therefore a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

Systems cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Inspectors determined that the licensee's failure to identify and

correct a condition adverse to quality could have result in the failure of a safety related SSCs

to perform its intended safety function. Specifically, the deviation from acceptance criteria

associated with the TDAFWP had the potential to cause premature bearing failure as

specified in PM 3132-1-22 and Root Cause Evaluation (RCE) 1132098.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The

inspectors determined that the issue was of very low safety significance and screened to

Green by answering "No" to all of the questions in Exhibit 2 - Mitigating Systems Screening

Questions.

Cross-Cutting Aspect: P.3 - Resolution: The organization takes effective corrective actions to

address issues in a timely manner commensurate with their safety significance. The licensee

failed to ensure appropriate corrective actions for a condition adverse to quality were taken in

a manner commensurate with its safety significance.

11

Enforcement:

Violation: The requirements of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action,"

specifies in part that, "Measures shall be established to assure that conditions adverse to

quality, such as failures, malfunctions, deficiencies, deviations, defective material and

equipment, and nonconformances are promptly identified and corrected."

Contrary to the above, from December 5, 2023 thru January 28, 2024, the licensee failed to

establish measures to assure that conditions adverse to quality are promptly identified and

corrected. Specifically, the licensee failed to identify and correct deviations associated with

the as-found acceptance criteria requirements for the Turbine Driven Auxiliary Feedwater

Pump (TDAFWP). The as-found turbine bearing coupling alignment data were outside the

acceptance criteria values.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Failure to Provide Adequate Oversight to Supplementary Personnel Resulting in a Reactor

Trip

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

FIN 05000282,05000306/2024001-03

Open/Closed

[H.2] - Field

Presence

71153

The inspectors identified a Green finding when the licensee failed to meet the standards of

procedure FP-MA-COM-02, "Oversight and Control of Supplementary Personnel."

Specifically, the licensee failed to provide supplemental workers with an appropriate level of

oversight and engagement to ensure performance was commensurate with station standards

and expectations, resulting in a loss of all non-safeguards busses and a Unit 1 turbine and

reactor trip.

Description:

On October 19, 2023, horizontal directional drilling (HDD) activities were being performed at

the Prairie Island Nuclear Generating Plant (PINGP) in support of degraded cable

replacement as part of the Unit 2 refueling outage. The HDD was from the plant switchyard to

just inside the protected area fence and was being conducted by the Xcel Energy

Transmission & Distribution (T&D) group. At 11:10 a.m. on October 19, 2023, with Unit 1

operating at 100 percent power, multiple substation breakers unexpectedly opened and,

simultaneously, multiple grounds were detected on direct current (DC) control power cabling

from the plant to the substation control house. This resulted in a loss of all non-safety related

busses simultaneously with a Unit 1 turbine trip and reactor trip, and the actuation of auxiliary

feedwater and emergency service water. Operators responded to the event in accordance

with approved plant procedures and safely placed the plant in Mode 3, hot shutdown. NRC

inspectors responded to the site to provide oversight of licensee response. Unit 1 was

subsequently cooled down to Mode 5, cold shutdown.

The site determined that the HDD in progress at the site damaged DC control cables resulting

in the identified plant response. The licensee root cause evaluation determined the root

causes were weakness in the excavation permit approval process as well as inadequate

oversight of the personnel performing the work. The T&D workers were Xcel Energy

12

employees with authorized access to the respective areas, and little oversight was provided

based upon this. However, this was not in compliance with licensee procedure

FP-MA-COM-02 "Oversight and Control of Supplementary Personnel," which specifies that

oversight be provided to supplemental personnel "anytime work is to be accomplished at

NSPM nuclear facilities by personnel other than permanent nuclear business unit

employees." The procedure further specifies that it is the responsibility of the department

manager/functional area manager or designee to "provide in-field oversight, observations,

and coaching to supplemental workers."

This finding is NRC-identified because the inspectors had identified a previous weakness in

the licensee's oversight of work from the same workgroup (Transmission and

Distribution - T&D), both in the quality of work and the oversight of the supplemental workers.

This issue was reviewed using Inspection Procedure 71153, "Follow up of Events and

Notices of Enforcement Discretion," and was reported in Licensee Event Reports (LERs)

05000282, 05000306/2023-001-00 and 05000282, 05000306/2023-001-01 for Prairie Island

Nuclear Generating Plant, Units 1 and 2, "Reactor Trip, Auxiliary Feedwater and Emergency

Service Water System Actuation due to Electrical Transient in DC Control Power Cables"

(ADAMS Accession Nos. ML23338A277 and ML24081A153).

Corrective Actions: The licensee replaced and tested all damaged cables. In addition, they

implemented procedure changes to strengthen the requirements for excavation onsite as well

as incorporating duties and responsibilities of individuals responsible for oversight of

supplemental personnel.

Corrective Action References: CAP 501000077958

Performance Assessment:

Performance Deficiency: Licensee procedure FP-MA-COM-02 "Oversight and Control of

Supplemental Personnel," requires that oversight be provided to supplemental personnel

"anytime work is to be accomplished at NSPM nuclear facilities by personnel other than

permanent nuclear business unit employees." The procedure further specifies that it is the

responsibility of the department manager/functional area manager or designee to "provide

in-field oversight, observations, and coaching to supplemental workers."

Contrary to the above, at 11:10 a.m. on October 19, 2023, the licensee failed to provide

adequate oversight to the T&D group performing HDD onsite at the Prairie Island Nuclear

Generating Plant, resulting in the drill head damaging DC control power cables, tripping the

turbine generator output breakers, the turbine, and the reactor.

Inspectors determined that the licensee's failure to provide adequate oversight to

supplementary workers was within the ability of the licensee to foresee and correct and was

therefore a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Human Performance attribute of the Initiating Events

cornerstone and adversely affected the cornerstone objective to limit the likelihood of events

that upset plant stability and challenge critical safety functions during shutdown as well as

power operations. Specifically, the horizontal directional drilling led to damage to the DC

control power cables, resulting in a loss of all non-safeguards busses, an automatic turbine

and reactor trip. The loss of all non-safeguards busses coincident with the turbine and reactor

13

trip resulted in a "SCRAM with Complications" in accordance with NEI 99-02, revision 7,

"Regulatory Assessment Performance Indicator Guideline."

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The

inspectors assessed the significance of the finding using Inspection Manual Chapter (IMC) 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power.

The inspectors used IMC 0609.04, Initial Characterization of Findings, and IMC 0609,

Appendix A, Exhibit 1, Initiating Events Screening Questions. The finding was determined to

be of very low safety significance (Green) because there was no loss of mitigating equipment

relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-Cutting Aspect: H.2 - Field Presence: Leaders are commonly seen in the work areas of

the plant observing, coaching, and reinforcing standards and expectations. Deviations from

standards and expectations are corrected promptly. Senior managers ensure supervisory and

management oversight of work activities, including contractors and supplemental personnel.

Specifically, the licensee did not have nuclear business unit personnel in the field providing

oversight of supplemental workers as required.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 9, 2024, the inspectors presented the integrated inspection results to

Thomas Conboy and other members of the licensee staff.

14

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2C1.2-M1

Unit 2 Startup to Mode 1

14

2C1.2-M2

Unit 2 Startup to Mode 2

10

C1B

Appendix - Reactor Startup

25

71111.11Q

Procedures

Fig C1A-3

Estimated Critical Boron Concentration Based on

BEACON-TSM

13

Prairie Island

Maintenance Rule

Basis Document

Various Functions

Various

Dates

Miscellaneous

SP 2168.13 2R33

CE Boric Acid Indications

71111.12

Procedures

PM 3122-3

Shield Bldg, Category 1 Vent Zone, Fire and Security Door

Inspection

43

71111.13

Miscellaneous

Extended Operation in Lowered Inventory Operational Fous

Protection Plan

0

501000080988

Past Operability Review (POR)

02/06/2024

501000081254

Unit 1 Use of LCO 3.0.4

01/24/2024

501000081294

IST Review Mode Change and SP 1155 A/B

01/25/2024

501000081411

SP 2155A Not Complete w/in Periodicity

01/28/2024

501000081422

IST Requirements for Pumps vs 3.0.4

01/29/2024

Corrective Action

Documents

501000081503

AOC - Tech Spec Surveillance SP/ASME/IST

01/30/2024

Engineering

Changes

QF2702, Design

Equivalent

Change,

602000023965

EC 601000004330, Rev. 0, U1 NIS Drawer Replacement

1R34

12/27/2023

Engineering

Evaluations

608000001132

Evaluation of RCS for Continued Operation per Tech. Spec.

3.4.3

0

LTR-EQ-23-35

Dynamic Similarity Evaluation of NIS Source Range Drawer

Assemblies

12/14/2023

Miscellaneous

LTR-NIS-23-020

Functional Similarity Evaluation of NIS Source Range

Drawer Assemblies

12/14/2023

71111.15

Procedures

MP D27.35

MSIV Closure for Maintenance or Testing

2

71111.18

Miscellaneous

Limitorque

Technical Update

Material Color Change

03/05/2001

15

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

01-01

501000077983

11 DC Panel Ground

01/10/2024

Corrective Action

Documents

501000078005

12 DC Panel Ground

01/10/2024

EM 4.3.1-C-6

Connectors

4

EM 4.3.1-C.7

Electrical Construction Standards Cables

6

EQ H8-E.1.7.DG

EEQ - SPLICES RAYCHEM INLINE - CRIMP CONN

PLANNERS INSTRUCTIONS

6

H8-E.1.53.DG

EEQ - Splices EGS Compact Splice Planners Instructions

1

H8-E.1.8.DG

EEQ - Splices Raychem Inline-Crimp Conn Installers

Instructions

6

71111.20

Procedures

SP 2072

Local Leakage Rate Test of Containment Penetrations

27

2M-AF-3132-1-22

Isolation, Restoration and Testing of 22 Aux Feed Pump

21

D70.12

Motor-Operated Valve Steam Lubrication

6

MP D65

Auxiliary Feedwater Overspeed TTOD Test

6

SP 1070

Reactor Coolant System Integrity Test

57

SP 1073B

Monthly Train B Shield Building Ventilation System Test

21

SP 1080.2

12 Shield Building Ventilation Filter Removal Efficiency Test

28

SP 1106B

22 Diesel Cooling Water Pump Monthly Test

109

SP 2070

Reactor Coolant System Integrity Test

53

SP 2070

Reactor Coolant System Integrity Test

53

Procedures

SP 2406

Main Steam Isolation Valve Inservice Test

6

WO 700044935

SP 1070 Rx Coolant System Integrity Test

WO 700078684

Troubleshoot Bkr 211J-13 and MV-32019

WO 700087060

PM 3132-1-22: 22 TDAFWP MINOR INSP

09/27/2023

WO 700100220

SP 2070 - Rx Coolant SYS Integrity TST

WO 700100220

SP 2070 - RX Coolant SYS Integrity TST

01/28/2024

WO 700119857

CV-31419 Water Leak By

WO 700125323

SP 1155B - CC SYS QTR TEST TRN B

WO 700127367

MV-32016 LP A MS to 11 TDAFWP Lube

WO 700133040

Perform As-Found LLRT

WO 700133173

SP 1106B-22 DD CL PMP (245-392) 1 M Test

WO 700133246

Test SI NOT READY Light

71111.24

Work Orders

WO 700135613

SP 2406 - MSIV Inservice TST up from CSD

03/06/2024

16

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Engineering

Evaluations

602000031728

Reactor Trip Report - Unit 2

03/03/2024

QF0431, Rev. 21,

602000031268

Cause Evaluation Template, CAP ID# 501000077958, Unit 1

Reactor Trip

10/19/2023

QF0565, Revision

17

Maintenance Rule Functional and MSPI Failure Evaluation,

QA# 501000081105

12/01/2023

Miscellaneous

QF1146, Revision

5, Past

Operability

Review

CAP 501000079553

12/01/2023

2C49.5

Placing Unit 2 Condensate Filter Demineralizers On Line

12

2E-0

Reactor Trip or Safety Injection

41

C58800

Remote Alarm Response Procedure

6

OP 2C28.1 AOP4

Restarting Unit 2 AFWP After Low Suction/Discharge

Pressure Trip

7

71153

Procedures

OP 2C28.2

Unit 2 Feedwater System

46