IR 05000280/1987001

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Insp Repts 50-280/87-01 & 50-281/87-01 on 870112-15.No Violations or Deviations Noted.Major Areas Inspected:Fire Protection Sys Interaction Events Associated w/861209 Feedwater Pipe Rupture
ML20210V217
Person / Time
Site: Surry  Dominion icon.png
Issue date: 02/04/1987
From: Conlon T, Madden P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20210V181 List:
References
50-280-87-01, 50-280-87-1, 50-281-87-01, 50-281-87-1, NUDOCS 8702180718
Download: ML20210V217 (7)


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-Report Nos.: 50-280/67- and 50-281/87-01 Licensee: -Virginia Electric and Power Company Richmond, VA 23261 Docket Nos.: 50-280 and 50-281 License Nos.: DPR-32 and DPR-37 Facility Name: Surry 1 and 2 Inspection ConductedHanuary J2-15,1987 Inspecto P. MgMadden T? f' [ /

2'- B -8 7 Date Signed Approved by: f / M[ z, , /m 72 4) -f' T T. E. Cdrilbn,Sectidn Chief / Date Signed Plant Systems Section

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Division of Reactor Safety SUMMARY Scope: This special, announced inspection was conducted in the areas of Fire Protection System interaction events associated with the December 9,1986, feedwater pipe rupture and followup on previously identified inspection item Results: No violations or deviations'were identified.

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REPORT DETAILS Persons Contacted Licensee Employees

  • Benthall, Nuclear Safety and Licensing Staff
  • T. Carlisle, Staff Engineer Corporate Loss Prevention
  • Craft,-Licensing Coordinator
  • L. Farinholt, Site Loss Prevention Supervisor Other licensee employees contacted included construction craftsmen, engineers, technicians, operators, mechanics, security force members, and office personne NRC Resident Inspector
  • B. Holland
  • Attended exit interview Exit Interview The inspection scope and findings were summarized on January 15, 1987, with those persons indicated in paragraph 1 above. The inspector described the areas inspected and discussed in detail the inspection finding No dissenting comments were received from the license The licensee did not identify as proprietary any of the materials provided to or reviewed by the inspector during this inspectio . Licensee Action on Previous Enforcement Matters This subject was not addressed in the inspectio . Unresolved Items '

Unresolved items were not identified during this inspectio . Fire Protection System Spurious Activations and Main Control Room Habit-ability On December 9,1986, at approximately 14:20 hours the Surry Nuclear Power Station experienced a feedwater pipe failure in the Unit 2 Turbine Buildin Within minutes of the feedwater pipe rupture event in the Unit 2 Turbine Building, portions of the Unit 2 turbine building sprinkler system actuate Sixty-two sprinkler heads opened in the immediate area of the feedwater pipe

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rupture due to the high heat levels associated with the even These sprinkler heads as they opened began immediately discharging water to cool the turbine building atmospher As a result of the sprinkler water and feedwater discharge due to the event the carbon dioxide (C0 2) and the Halon Fire Suppression System Control panels were affected. The CO 2 fire suppression system control panels for both the Units 1 and 2 cable tray rooms are located near the Unit 2 cable tray room access door along the column line 9 wall on elevation 45'-0". The sprinkler water discharge from the sprinkler heads directly over and adjacent to these panels intruded into the C02 fire suppression system control panels through multiple open conduits ends which extend from the panels to the cable tray raceway above. Therefore, the water intrusion into these panels caused the time limit switches to short in the closed positio Upon closure of these switches, the C02 fire suppression systems, at approximately 14:32 hours (12 minutes into the event) the Robert Shaw fire protection panel / printer in the main control room recorded the discharge of CO2 into the Unit 2 cable tray rooms. In addition, at approximately 14:34 ,

hours (14 minutes into the event) the Robert Shaw panel recorded the second discharge of CO2 into the Unit 2 cable tray room. It should be noted that the bulk of CO2 discharge, which was noticed by the licensee's loss prevention staff who conducted the perst inel search and initiated the venting of C0 2 from the cable tray rooms, was in the Unit 1 cable tray room. The Robert Shaw fire protection panel / printer did not register a Unit 1 discharge throughout the duration of the pipe rupture event. Thus, as a result of the water affecting the time limit switches in the CO2 control panels, the discharge timers did not function as designed. This allowed a total of 17 tons of CO 2to be discharged into the cable tray room In addition, the Halon Fire Suppression System protecting Units 1 and 2 emergency switchgear rooms on elevation 9' 6" actuated at approximately 15:02 hours (42 minutes into the event as documented by the Robert Shaw panel printer). The Halon system actuation was caused by sprinkler water discharge and feedwater runoff which flowed under the elevation 27'-0" fire door (30) installed in the column line 9 wall. The water runoff cascaded down the column line 9 wall, which separates the Units 1 and 2 turbine buildings, on the Unit 1 side, entered a Halon system conduit through a conduit fitting which had the fitting cover plate removed at the time of the event. The specific conduit fitting is located directly below the open grating floor on the Unit 1 side of the elevation 27'-0" column line 9 wall fire door (30). The runoff water which entered in the subject conduit flowed through the conduit and intruded Halon control panel 1-FPH-CP-1 located on the Unit 1 side of the column line 9 wall on elevation 9'-6".

The water intrusion caused the time limit, battery charger and the dual zone modules to short. Therefore, upon shorting the dual zone modules, which are associated with the manual remote actuation circuit located in the control room, the system actuated discharging 7 to 10% Halon concentration into the emergency switchgear room . - ---

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Since Halon extinguishing agent is heavier than air, the Halon discharge into the emergency switchgear rooms on elevation 9' 6" had basically no effect on the habitability of the main control room. Upon the initial discharge of the emergency switchgear Halon fire suppression system some in leakage of Halon into the main control room through floor penetrations in the Unit 1 computer room and through the control room emergency air bottle discharge piping was noticed. However, it should be noted that the concen-trations of Halon as a result of the emergency switchgear room discharge would not have created a life hazard to personnel in the control roo Upon verification of C0I system discharge by the main control room, two members of the licensee s loss prevention staff responded to the cable tray rooms with self-contained breathing apparatus to conduct a personnel search of these rooms. As a part of this search, measures were taken to vent the C0 2 from the cable tray rooms by opening the doors to Units 1 and 2 mechanical equipment rooms and the respective cable tray room access doors located on elevation 45'-0" of Units 1 and 2 turbine buildings. In addition, at the time the C0 2was being vented from the cable tray rooms the main control room annex door in the turbine building / control room complex wall and the main control room door separating the annex from the main control room were blocked open. Thus, C02 being heavier than air flowed down from elevation 45'-0" to the 27'-0" elevation and into the main control room annex and the main control room through the open door. In addition, during the time the C02 was being vented from the cable tray rooms, the main control room exhaust fan (1-VS-r-15) was operating. The operation of this fan created a negative pressure in the main control room and the main control room annex thus, causing the vented CO 2 to be drawn into the control room comple Presence of CO 2 in the control room can also be attributed to the fact that at the time of the event control room ventilation unit 1-VS-AC4 was out of service for design modifications and that a temporary unit which obtained its makeup air from mechanical equipment room 1 was in service. Therefore, upon venting the C02 from the respective cable tray room into the mechanical equipment room, this allowed the temporary control room HVAC fan unit to draw C0 2 into the control room ventilation syste Control room personnel in the main control room annex and near the main control room door experienced shortness of breath, dizziness and nause It should be .noted that once it was recognized that CO2 was present in the control room, the control room operators took the appropriate corrective actions and initiated control room emergency air supply fans 1-VSF-41 and 2-VSF-4 The starting of these fans placed the main control room at a higher pressure than the turbine building. This action assisted in diluting and exhausting the existing CO2 levels and precluded any additional CO2 from infiltrating into the main control roo _ . ._ . .. _ '

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The licensee, as a result of the spurious fire protection system actuations associated with the feedwater pipe break event, has proposed the following C02 /Halon fire protection system modifications: Seal the open ends of all conduits leading to the CO2 system control panels throughout the plan . Replace all components within both Units 1 and 2 Cable Tray Room CO 2 control panels that show visible signs of corrosio . Fully test both systems to confirm proper system operatio . Seal the Unit 1 control panel. A li"s hole and a 1" hole exist in the right side wall near the bottom of the pane . Replace missing 2" conduit cover under the elevation 27'-0" turbine building column line 9 wall platform and walk down all other conduits to ensure that covers to conduit, pull boxes, and junction boxes are in place and properly seale . Repair door seal on the Halon control panel and relocate identification sig . Replace all existing Halon panel modules and upgrade modules to CP35 Serie . Perform functional tests of the Halon System for both Units 1 and 2 emergency switchgear rooms to ensure proper operatio . Replace Halon System check valves in discharge lines or replace rubber seal . Have Halon cylinder heads replaced or reworked to ensure bottles will not leak and that seals are in good conditio . Have Halon bottles filled and placed in discharge heade . Have Halon pressure switch and solenoid covers removed and inspect for corrosion or water damag Based on our review of the above modifications, it appears that upon their completion the probabilities of spurious cable tray room CO2 and emergency switchgear room fire suppression system actuations due to water / steam intrusion will be greatly reduced. However, it is our recommendation that the licensee in addition to implementing the above proposed modifications, consider the following with respect to ensuring control room habitability and personnel safety:

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5 The installation of a wintergreen odorized on Units 1 and 2 cable tray room CO 2 system,

~ The installation of a permanent 0 2 analyzer with a control room audible alarm in the main control room annex, The development of a procedure which will require the control room operators to pressurize the control room in the event of a gaseous fire suppression system actuation in either the cable tray rooms or the emergency switchgear rooms, and The installation of predischarge visual and audible warning devices near Units 1 and 2 cable tray room doors and inside the cable tray rooms which will activate to alert personnel prior to a CO 2 system discharg The licensee's proposed fire protection system modifications and their evaluation and implementation of the above recommendations will be reviewed during a subsequent NRC inspectio . Inspector Followup Items (IFI) (OPEN) IFI (280 and 281/85-37-01), Firefighting preplans lack brigade guidance in smoke control, fire damage control and fire suppression water runoff contro Currently, the preplans are being revised by the license Currently the licensee's site loss prevention staff anticipates issuing the

. revised preplans by April 1, 198 (CLOSED) IFI (280 and 281/85-37-02), Annual Fire Pump Test not being conducted following the guidance of NFPA-20. The licensee has revised perodic test (PT) procedure 24.12, fire pump flow rate test to reflect the intent of the fire pump flow test guidance of NFPA-2 (CLOSED) IFI (280 and 281/85-37-03), Review of Appendix R Fire Barrier Upgrade Progra The licensee has revised surveillance procedure PT-24.11, Fire Barriers, to incorporate the required Appendix R Fire Barrier into the Surveillance Program, (CLOSED) IFI (280 and 281/85-37-04), Review of Fire Protection Valve Cycle Test Program to verify all testable valves are being tested. The licensee has completed their valve review and has incorporated the dry pipe hose station and sprinkler system valves for Units 1 and 2 cable tunnels into surveillance procedure PT-24.1A, Fire Protection System -

Testable Valves.

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! (CLOSED) IFI (280 and 281/85-37-05), Failure to Review FPSER Commitment

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Regarding Replacement of Form Cart by Fire Truck. The fire truck's fighting equipment exceeds the equipment which was carried by the foam car The site loss prevention staff had advised their corporate staff by memorandum dated December 26, 1985, to request the NRC to revise their Safety Evaluation Report commitment with respect to the foam cart replacement.

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