IR 05000255/1991009

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Insp Rept 50-255/91-09 on 910406-0513.No Violations Noted. Major Areas Inspected:Plant Operations,Maint,Surveillance, Reportable Events & Region III & Headquarters Requests
ML18057A934
Person / Time
Site: Palisades Entergy icon.png
Issue date: 05/29/1991
From: Jorgensen B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18057A933 List:
References
50-255-91-09, 50-255-91-9, NUDOCS 9106040091
Download: ML18057A934 (13)


Text

U. S. NUCLEAR REGULATORY COMMISSION REGION II I Report No. 50-255/91009(DRP)

Docket No. 50-255 Licensee: Consumers Power Company 212 West Michigan Avenue Jackson, Ml 49201 Facility Name:

Palisades Nuclear Generating Plant Inspection At:

Palisades Site, Covert, MI Inspection Conducted:

April 6 through May 13, 1991 Inspectors: J. K. Heller, Senior Resident Inspector Approved By:

J. A. Isom, Senior Resident Inspector J. R. Roton, Resident Inspector R. L. B water, Reactor Engineer license No. DPR-20 DATE'.

I

Inspection Summary

Ins~ection on April 6 through May 13, 1991 (Report No. 50-255/91009 (DR ))

Areas Inspected: Routine unannounced inspection by the resident inspectors of plant operations, maintenance, surveillance, reportable events, and NRC Region III and Headquarters request No Safety Issues Management System (SIMS) items were reviewed. A routine management meeting was conducted on April 18, 199 Results: Of the five areas inspected, no violations or deviations were issue The strengths, weaknesses and open items are discussed in paragraph 9, 11Management Intervie In summary:

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Two strengths were noted pertaining to communications with the NRC and the licensee response to a fir Five weaknesses were noted pertaining to a personnel safety hazard, control of flammable liquids, control of vendor manuals, control of an outage related work activity, and use of a temporary repair versus temporary modificatio An open item pertaining to control of vendor manuals was identifie 'ii 106040091 PDR ADOCK G!

910529 05000255 F'DR

DETAILS Persons Contacted Consumers Power Company

  • D. P. Hoffman, Vice President, Nuclear Operations
  • D. W. Joos, Vice President, Energy Supply

+*G. B. Slade, Plant General Manager*

+ R. M. Rice, Plant Operations Manager

  • D. J. VandeWalle, Engineering Programs Manager
  • R. D. Orosz, Engineering & Construction Manager

+*P. M. Donnelly, Safety & Licensing Director

+ K. M. Haas, Radiological Services Manager J. L. Hanson, Operations Superintendent

  • R. B. Kasper, Maintenance Superintendent K. E. Osborne, System Engineering Superintendent

+ C. S. Kozup, Technical Engineer

+ W. L. Roberts, Senior Licensing Analyst R. W. Smedley, Staff Licensing Engineer K. A. Toner, Electrical/I&C/Computer Engineering Manager T. W. Bowes, Mechanical & Civil/Structural Engineering Manager T. A. Buczwinski, Reactor & Thermal-Hydraulic Engineering Manager T. J. Palmisano, Administrative & Planning Manager

+ M. G. Mlynarek, Plant Reactor Engineer Nuclear Regulatory Commission

  • A. B. Davis, Regional Administrator
  • H. J. Miller, Director, Division of Reactor Safety
  • M. P. Phillips, Chief, Operation Programs Section 2
  • Brent Clayton, Chief, Reactor Projects Branch 2

+*B. L._ Jorgensen, Chief, Projects Section 2A

+*J. K. Heller, Senior Resident Inspector

+ J. R. Roton, Resident Inspector

  • Denotes some of those present at the Management Meeting held in the Nuclear Regulatory Commission (NRC) Region III office on April 18, 199 +Denotes some of those present at the Exit Interview on May 13, 199 Other members of the plant staff, and several members of the contract security force, were *also contacted dlirin*g the inspection perio Operational Safety Verification (71707, 71710, 42700)

Routine facility operating activities were observed as conducted in the plant and from the main control roo The performance of Reactor Operators and Senior Reactor Operators, Shift Engineers, and Auxiliary Equipment Operators was observed and evaluate Included in the review were procedure use and adherence, records and logs, communications, shift/duty turnover, and the degree of professionalism of control room activities. Observations of the control room monitors, indicators, and recorders were made to verify the operability of emergency

systems, radiation monitoring systems, and nuclear reactor protection system Reviews of surveillance, equipment condition, and tagout logs were conducte General The plant began and ended the reporting period at essentially full powe Fire at P-47A, "Cooling Tower Chemical Addition Pump" On May 2, the licensee extinguished a small fire at the motor for P-47 The fire brigade response was appropriate. During the subsequent morning meeting, the fire was discussed and the need for a deviation report (internal corrective action document) was considered. It was concluded that this was a random failure of a 110 volt motor which did not require a deviation report. After the morning meeting, the inspector toured the site of the fire and determined by discussion with another NRC inspector that personnel had worked on the pump during the shift prior to the fir In addition, there was an outstanding work order indicating the need to repair an oil leak on the pum This was discussed with plant management and property protection personne Property protection personnel had separately learned of the outstanding work order and were requesting that a deviation report be written; Deviation Report 91-085 was written * Safety Injection Pump Recirculation Lines During reviews of the safety injection pump mini flow lines and shutdown heat exchanger recirculation lines to the Safety Injection and Refueling Water (SIRW) tank, the licensee determined that the leak tight integrity of the valve seats had never been verified. The tank is vented directly to the atmospher The licensee determined that minor leakage past the valve seats during LOCA conditions, with maximum core damage, would result in a significant unmonitored release path. It could.also result in habitability problems in the control room due to the location of the tank vent near the control room ventilation intake. Further, it could involve potential exposure problems at the site boundar The licensee discussed this problem with NRC Region III and Headquarters personnel during conference calls on May 9 and 1 Leak tight integrity testing of the isolation valves* was'not a regulatory requiremen Current plant configuration does not permit leak testing. Because of plant configuration, testing cannot be performed until the next cold shutdown - scheduled for 199 Evaluation of means to provide a filtered vent path continue The licensee has classified this as an unreviewed safety question because this plant configuration has not been reviewed by the NR This information was provided to the NRC Office of Nuclear Reactor Regulation (NRR) by separate correspondence *

  • Tours )

During a tour of the turbine building, the inspector found scaffolding that was not properly installed. The scaffolding, installed on the east side of the condenser adjacent to a main feed water pump, was missing the kick plate on one side. The inspector himself narrowly avoided a fall off this scaffol This was discussed with the safety officer and at the exit intervie The safety officer implemented corrective actio )

During a tour of the storage area, located on the mezzanine below the north end of the turbine deck, the inspector observed a number of items that raised questions of material accountability and flammable material contro The inspector found a large quantity of flammable material stored in a flammable storage locker. This amount may have been appropriate to support a large outage work force, however, the outage was over and the vendor was no longer on site. This was discussed with property protection personnel who agreed and had the materials remove The inspector verified the cabinet storage rating was not exceede While inspecting the general storage area, the inspector found two sealed weld rod canisters that did not have a Consumers Power receipt inspection numbe In addition, some of the liquid stored in the flammable storage cabinet did not appear to have markings indicating receipt inspection. This was discussed with system engineering who indicated that all material should be receipt inspected prior to us An attempt was made to determine if the material in question had been receipt inspecte However, clean up of the area had begun and the materials in question were discarde The licensee provided the inspector a copy of a work order associated with a turbine work activity. All items associated with this work order, including those provided by the vendor, had been receipt inspected. The inspector had no additional question Head/Pressurizer Vents During the post refuelin"g outage plant heatup, the indicated pressure on PIA-1066, 11Gaseous Vent Pressure Gauge, 11 increased as the primary coolant system was pressurize The pressure increase lagged the primary coolant system pressurization by approximately a shif The vent system is connected to both the head and pressurizer and relieves to either the pressurizer quench tank or directly to the containment atmospher The system configuration provides for dual isolation from either the head or the pressurizer to the containment atmospher PIA-1066 is installed on the common piping between the first and second isolation valves. The increase of pressure at PIA-1066 may indicate that one of the first isolation valves was

  • *

leakin The second isolation valve appeared to be holding, as evidenced by constant pressurizer quench tank readings and by stable containment atmospheric temperature/humidit Inspection Reports 50-255/90015(DRP) and 50-255/89012(DRP) document that this problem has occurred in the two previous operating cycle The only difference between the previous problem and the current problem is that the pressurization previously occurred a couple of months after the plant was on line and not while the plant was heating u Currently, there is no tag affixed to the vent system indicating that corrective action is required during the next cold shutdow The inspector discussed this with operations personnel, planning personnel, and system engineers. All were aware of the problem and were formulating corrective action The problem appears to be associated with the type of isolation valves used and the fact that the piping configuration ensures solid water in the line between the isolation valves. Operations personnel and system engineers all agree that additional testing is required to determine if a repair is require The inspector expressed concern that, since the problem was not captured by a formal mechanism, the potential exits that the opportunity for testing during the next outage may be misse Operations personnel entered this activity on the work order system to ensure testing is scheduled during the next cold shutdow No violations, deviations, unresolved, or open items were identified *

Maintenance (62703, 42700)

Maintenance activities in the plant were routinely inspected, including both corrective maintenance (repairs) and preventive maintenance. Mechanical, electrical, and instrument and control group maintenance activities were included as availabl The focus of the inspection was to ensure that the maintenance activities were conducted in accordance with approved procedures, regulatory guides, industry codes or standards, and were in conformance with Technical Specifications. The following items were considered during this review: Limiting Conditions for Operation were met while components or systems were removed from service, approvals were obtained prior to initiating the work, activities were accomplished using approved procedures, and post maintenance testing was performed as app 1 i cab l The following activities were inspected: Work Order 24102323, "F-138 continues to have high D/P Disassemble F-138 and clean filter element manually."

a permanently installed makeup system raw water supply manufactured by Hayward Manufacturing Company *

problem F-138 is strainer The inspector observed portions of the work activity and reviewed the work order packag The work order (WO) required review of the vendor manua The package contained a copy of the vendor

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manua The manual was not marked 11 controlled copy

, nor did the manual have any markings indicating the manual was reviewed and approved for us The inspector discussed this with mechanical maintenance department supervision who indicated that the strainer had recently been installed and the vendor manual was still being reviewed by system engineering. Since the vendor manual was required to support the maintenance activity, a copy of the manual was obtained from system engineering and attached to the work orde The planner had intended to mark-the copy "Information Only", however, the manual had not been so marke In addition, the inspector discussed this item with a work order planne The planner indicated that he knew vendor manuals were required to be controlled and how controlled copies were marke The planner showed the inspector a xerox copy of a vendor manual that the planner had obtained from the Document Control Cente The copy had the marks indicating the original was controlle The copy was marked 11 Information Only

  • The planner indicated that he had obtained the copy as an aid for work order plannin The inspector noted that use of an uncontrolled copy of a vendor manual while planning a work order could result in inadequate, inaccurate, or incomplete maintenanc This was discussed at the exit intervie The inspector reviewed Palisades Administrative Procedure AP 10.45, "Vendor Manuals 11 and found that AP 10.45 does not contain provisions for use of 11 Information Only 11 copies of vendor manual In addition, AP 10.45 does not permit use of uncontrolled vendor manual Failure to control vendor manuals as described above, is a violation of AP 10.4 A Notice of Violation was not issued for this because a Notice of Violation for an identical problem was issued in inspection report 255/91006(DRSS).

If this work activity had been observed at that time, this would have been an additional example for that Notice of Violation. Since this was an additional example of a violation for which insufficient time had elapsed to fully implement corrective action, a second Notice of Violation was not issue Until the corrective action is reviewed this item is an open ite (Open Item 255/91009-0l(DRP))

WO 2401854 air line to CV-0510, "Main Steam Isolation Valve, 11 leakin The repair was discussed in Paragraph 5.d, "Maintenance" of Inspec_tion Report 50-255/91005(DRP).

The-inspector performea additional reviews to determine if a temporary modification was performed without implementing the controls of Administrative Procedure AP.9.31,

"Temporary Modification Control

  • In this case, the system engineer classified the activity as a temporary repair which was controlled by Administrative Procedure AP 5.01, "Processing Work Requests/Work Orders". A temporary modification would require additional reviews-including a 10 CFR 50.59 review-prior to returning the component to servic The inspector has reviewed both Administrative Procedures and determined it was not clear if this was a temporary modification or temporary repai *
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The WO requir~d installation of a brace to hold two pieces of the air line togethe The brace will remain in place until a permanent repair is complete The brace adds weight to the air line which could change the stress calculations for the syste The added weight would be evaluated by the temporary modification process but was not evaluated by the temporary repair processes. The inspector discussed his concern with a design change supervisor, who agreed to evaluate and determine if the addition of weight was adequately controlled. Deviation Report D-PAL-91-090 was written to capture this questio An additional example of a previously cited Violation and one open item were identifie No deviations or unresolved items were identifie Surveillance (61702, 61708, 61710)

The inspector reviewed Technical Specifications required surveillance testing as described belo The review confirmed that testing was performed in accordance with adequate procedures, that test instrumentation was calibrated, and that the Limiting Conditions for Operation were me Additionally, removal and restoration of the affected components were properly accomplished, and test results conformed with Technical Specifications and procedure requirement The results were reviewed by personnel other than the individual directing the test, and deficiencies identified during the testing were properly reviewed and resolved by appropriate management personnel *

Special Test T-191, "Startup Physics Test Program" was inspecte The inspector reviewed the results of startup physics testing through 30 percent reactor power and discussed the results with the reactor engineer. Special Test T-191 was performed in March 1991, during restart from the refueling/steam generator replacement outag Measurements of hot zero power (HZP) critical boron concentration, HZP moderator temperature coefficient, and differential soluble boron worth all met procedure "review criteria".

"Review criteria" were more restrictive than any corresponding Technical Specification limits. Predicted values of physics parameters for each operating cycle were obtained

- from the licens*ee's fuel vendor, Advanced Nuclear Fuels* (ANF). -

Measurements of control rod worth for each rod group were all within review criteria limits with the exception of Group The worth of Group A was overpredicted by ANF by 0.158 percent delta rho, which exceeds the licensee's review criterion for individual rod group worth by 0.008 percent delta rh This deviation for an individual rod worth from the review criterion was considered small; the total sum of measured rod group worths satisfied its review criterio *

Core parameter measurements at less than 25 percent reactor power successfully met applicable review criteria. Core parameters at less than 30 percent reactor power failed to meet applicable review criteria. Predicted power of the two most in-board fuel assemblies on the major axis of the licensee's octant core model exceeded the actual power in these assemblies by greater than the 10 percent review criterion. The licensee noted that the computer model, used to predict fuel assembly power, was developed and bench marked against full power data.- The licensee subsequently obtained results of fuel assembly power predictions from AN The ANF model for predicting fuel assembly power contained a correction factor for power dependent albedo effects and showed reasonable agreement with the measured dat No violations, deviations, unresolved or open items were identifie.

Reportable Events (92700, 92720)

The inspector reviewed the following Licensee Event Reports (LERs) by means of direct observation, discussions with licensee personnel, and review of record The review addressed compliance to reporting requirements and, as applicable, that immediate corrective action and appropriate action to prevent recurrence had been accomplishe (CLOSED) LER 255/89006:

Component cooling water availability following a high energy line break. (CLOSED) LER 255/89022:

Radiological consequences of a safety injection refueling water tank ruptur {CLOSED) LER 255/89023: Discrepancies within actions completed and documentation provided for IE Bulletin 79-1 On October 10, 1989, engineering personnel identified that the U-bolt connection assembly for the main steam line support structure exceeded the stress allowable by FSAR by approximately 14 percen Enforcement action was considered and a Notice of Violation (255/89024-0l(DRS)) was issue The root cause and corrective action were addressed by Region III inspection specialists during evaluation of the license~

__ 's response_ to the violation~

(CLOSED) LER 255/90007:

Reanalysis of main steam line break identifies that containment pressure could exceed FSAR values due to inadequate desig On April 18, 1990, during a review of the main steam line break (MSLB) analysis being performed as part of the replacement steam generator effort, it was determined that the previous steam generator installation could result in containment pressures that exceed values referenced in the FSAR during MSLB scenarios where the break size is less than 100 percent of the steam line cross sectional are *

The cause of this condition was inadequate desig The methodology used by the Nuclear Steam Supply System supplier to assess the effects of MSLB transients on containment pressure incorrectly assumed that the large break constituted the most limiting design case for containment pressur *

A modification (FC-906) has been installed that provided a closure signal to the main feedwater regulator valves and main feedwater regulator bypass valves on high*containment pressure (setpoint approximately 3.7 psig). Closure of the feedwater regulator and regulator bypass valves on high containment pressure provides faster response than the previously used low steam generator pressure initiated main steam isolation signal (MSIS).

An analysis of the effects of variously sized MSLBs on containment pressure has been performed for the post-modification configuration. This indicates that the maximum containment pressure for the most limiting case is now within the containment pressure design basis referenced in the FSA The problem addressed by this LER was reviewed and documented in Inspection Reports 50-255/90014{DRP) - Paragraph 3.b(2),

1110 CFR 50. 72 report", 50-255/90015(DRP) - Paragraph 8, 11Design Changes

,

and 50-255/90018(DRP) - Paragraph 10, 11Design Changes

  • Enforcement action was considered and a Notice of Violation was issued (255/90018-04(DRP)). (CLOSED) LER 255/90011:

Unexpected reactor protection system actuation during turbine trip breaker testing due to incorrect test procedur On June 15, 1990, during performance of Operations Checklist CL 36, an unexpected, automatic actuation of the reactor protection system was initiated by the "loss of load 11 turbine trip feature due to an input to the 11 loss of load 11 trip logic which had not been adequately blocke The root cause of this event was the inadequacy of Operations checklist, CL 3 Changes to this checklist necessitated by implementation of facility change package FC 800 were not recognized by engineering, or by the operations personnel who were contacted regarding the checklist changes necessitated by implementation of Fc-so Failur~ fo p~op~rly revise ~rocedures affected by a design change is contrary to requirements of 10 CFR 50, Appendix B, Criterion III. This is addressed further belo To correct the deficiency, Operations Checklist, CL 36, has been revised to include appropriate position requirements in the turbine trip breaker testing sequence, and CL 36 has subsequently been performed without inciden In addition, a review of the Operations Checklist revision process and checklist controls had been performe *

The inspector concluded that the licensee had performed a prompt evaluation of the cause of this event with appropriate management attention. The corrective actions taken appeared adequate to prevent recurrence. Therefore, in accordance with 10 CFR 2 Appendix C, Section V.G, a Notice of Violation was not issued for the violation of Design Controls since it was licensee identified, classified as Severity Level IV or V, reported, not a willful violation, and corrected, including measures to prevent recurrence (Closed -

Violation (NV6) 255/91009-02(DRP) (CLOSED) LER 255/90014:

Inadvertent start of an auxiliary feedwater pum On August 28, 1990, an inadvertent start of the P-8C auxiliary feedwater (AFW) pump occurred while configuration control project personnel were performing electrical wiring diagram verification activities in the back of control panel C-187 This panel contains the AFW actuation channel for this pum The root cause of this event may have been the bumping of the AFW actuation channel, channel 118 11, logic module by configuration control project personnel during their wiring verification inside control panel C-187 No other root cause could be identifie The corrective actions taken for this event included discontinuing the balance of the AFW control panel work until the AFW system was placed out of service during the 1990 outag Additionally, during the aforementioned outage, I&C technicians attempted to duplicate the actuation. Negative results were achieved from those attempt Although the root cause of this event could not be absolutely attributed to the bumping of the AFW actuation logic module by the configuration control project personnel, the inspector concluded that the licensee had performed a prompt evaluation of the cause of this event with appropriate management attentio (CLOSED) LER 255/90019:

Inadvertent Right Channel Containment Isolatio On November 1, 1990, an inadvertent right channel containment isolation and a recirculation attuation occurred when

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configuration control project personnel, working in the EY-20 panel, caused a loss of the Y20 preferred bu With half of the right channel containment isolation circuits de-energized to support post installation modification checkouts, the required two out of four logic was satisfied when the bus was los The root cause of the event was personnel error. While verifying the wiring in panel EY-20, configuration control project personnel shorted the number two plant inverter when they placed a ruler with a metal edge across the terminal points of two heat sinks. This action tripped the inverter and resulted in the loss of the preferred bus Y2 *

A work order was issued and the Y20 inverter was repaired *

On November 2, 1990, a management review board was held to discuss the event with configuration control project personnel and their supervisor. Additionally, a Human Performance Enhancement System evaluation was conducted which led to additional follow-up corrective actions. These follow-up actions have been complete The inspector concluded that-the licensee had performed a prompt evaluation of the cause of this event with appropriate management attention. Corrective actions taken appeared reasonable to prevent recurrenc (CLOSED) LER 255/90020:

Loss of lC bus during startup breaker testin On November 10, 1990, bus lC was lost when the station safeguards power breaker opened due to the racking in of the startup breaker into the "test" positio The root cause of this event was inadequate instruction Administrative Procedure (AP) 4.02, "Control of Equipment Status", failed to caution against closing the 2400 volt incoming stored energy breaker while racked in the "test" position. Standard Operating Procedure 30, "Station Power",

Attachment 1, "System Testing" stated that testing of 4160 and 2400 volt incoming breakers may be done in the test position, but only when the plant is shutdown and the bus can be isolate This requirement was not discovered when the requirements for the breaker testing were reviewe Standard Operating Procedure 30 has been reviewed and revised to clarify the testing requirements of the 4160/2400 volt incoming breaker AP 4.02 has been reviewed and revised to clarify requirements for testing 4160/2400 volt stored energy breakers and 4160/2400 solenoid operated breaker Permanent Maintenance Procedure SPS-E-4, "Maintenance for 4160/2400 Volt Switchgear has been reviewed and revised to refer to Standard Operating Procedure 30 for testin The inspector concluded-that the license had performed a prompt evaluation for this event with appropriate management attentio The corrective actions taken appeared adequate to prevent recurrenc In accordance with 10 CFR 2 Appendix C, Section V.G., a Notice of Violation was not issued for the personnel error and inadequate procedure since it was licensee identified, classified as Severity Level IV or V, reported, not a willful violation, and was corrected, including measures to prevent recurrence, in a reasonable period of time (Closed - violation (NV6)255/91009-03(DRP)) *

Two licensee identified violations and two violations issued in previous inspection reports were identifie No deviations, unresolved or open items were identifie.

Inspection of Regional and Headquarters Requests (TI 2515/103 and 71707) (Closed) Temporary Instruction (TI) 2515/103 11Loss Of Decay Heat Removal" (Generic Letter 88-17) - TAC 6976 The resident inspector performed the inspection activities applicable to the Division of Reactor Projects (see Paragraph 12 of Inspection Report No. 50-255/90014(DRP)).

The inspection activities that remain are assigned to NRR, which are addressed by TAC #6976 Region III requested information pertaining to the Shift Technical Advisor (STA).

At Palisades, the Shift Engineer, who is a licensed (Senior Reactor Operator) member of the crew, would provide the STA function during an emergenc This information was provided to Region II Region III requested information pertaining to the seismic design and fuel storage capability of the Diesel Generator fuel oil syste The fuel oil system capacity was designed for seven days of operatio The portion of the fuel oil system from the underground storage tank to the day tank was not seismically qualifie The day tank to the diesel generator was seismically qualifie The day tank fuel oil capacity permits approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> of operatio In addition, the day tank can be filled directly from a fuel oil tanker. This information was provided to Region II No violations, deviations, unresolved or open items were identifie Management Meeting (30702)

On April 18, 1991, a management meeting was conducted in the NRC Region III offices {attendance was as indicated in Paragraph 1) to discuss licensee plans for changes in organizational structure and responsibilities. While these topics were discussed in various aspects, the main focus of the licensee's presentation on organizational changes was on the newly-created Nuclear Engineering and Construction grou Concerning assignments of responsibilities, special emphasis was directed to planned changes in the licensee's assessment of his own performance.- Specifically, the planned removal of the old Quality Assurance group from in-line review functions and the expanded use of "peer" inspection for in-process quality verification were discussed in some detail. Further staff-level exchanges and evaluations are anticipated in some of these area The licensee addressed a number of questions raised during the meeting and expressed a willingness to keep the NRC Region III management and staff informed regarding future.decisions which bear on the issues *

  • Open Item Open Items are matters that require further review and evaluation by the inspector, including an item pending specific action by the licensee and a previously identified violatio Open items are used to document, track, and ensure adequate followup by the inspecto An Open Item disclosed during the inspection is discussed in Paragraph.

Management Interview (71707)

The inspectors met with licensee representatives - denoted in Paragraph 1 - on May 13, 1991 to discuss the scope and findings of the inspectio In addition, the likely informational content of the inspection report with regard to documents or processes reviewed by the inspectors during the inspection was also discusse The licensee did not identify any such documents/processes as proprietar Highlights of the exit interview are discussed below: Strengths noted:

(1)

Fire brigade and property protection response to a May 2 motor fire (paragraph 2.b, "Operations").

(2)

Communication with the NRC pertaining to safety injection pump mini flow and shutdown cooling recirculation line potential unreviewed safety question (paragraph 2.c,

"Operations"). Weaknesses noted:

(1)

Potential safety hazard caused by incomplete scaffolding (paragraph 2.d(l), "Operations").

(2)

Control of flammable liquid In this case the letter of the requirements was met however the intent of the requirements may not have been (paragraph 2.d(2),

"Operations").

(3) Outage work activity not identified on the outage work schedule (paragraph 2.e, "Operations").

(4)

Vendor manual control and apparent lack of understanding of the controlling Administrative Procedure (paragraph 3.a, 11Maintenance")

(5)

Work activity that modified a system without a safety evaluation (paragraph 3.b, "Maintenance") The e-ight LERs (paragraph 5, "Reportable Ev-ent.5

) reviewed were discusse In summary, two were the subject of a previous violation and two were licensee identified violations for which a Notice of Violation was not issued, as provided for in 10CFR The remaining four were closed without commen The open item (paragraph 3.a, "Maintenance

) was discusse The inspector will review the licensee's corrective action in a subsequent inspection *

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