IR 05000254/2019002

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Integrated Inspection Report 05000254/2019002 and 05000265/2019002
ML19214A115
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 07/31/2019
From: Kenneth Riemer
NRC/RGN-III/DRP/B1
To: Bryan Hanson
Exelon Generation Co
References
IR 2019002
Download: ML19214A115 (22)


Text

July 31, 2019

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2INTEGRATED INSPECTION REPORT 05000254/2019002 AND 05000265/2019002

Dear Mr. Hanson:

On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Quad Cities Nuclear Power Station, Units 1 and 2. On July 11, 2019, the NRC inspectors discussed the results of this inspection with Mr. Ken Ohr and other members of your staff. The results of this inspection are documented in the enclosed report.

No NRC-identified or self-revealing findings were identified during this inspection.

The inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects

Docket Nos. 05000254 and 05000265 License Nos. DPR-29 and DPR-30

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000254 and 05000265

License Numbers:

DPR-29 and DPR-30

Report Numbers:

05000254/2019002 and 05000265/2019002

Enterprise Identifier: I-2019-002-0063

Licensee:

Exelon Generation Company, LLC

Facility:

Quad Cities Nuclear Power Station, Units 1 and 2

Location:

Cordova, IL

Inspection Dates:

April 01, 2019 to June 30, 2019

Inspectors:

J. Cassidy, Senior Health Physicist

G. Edwards, Health Physicist

R. Murray, Senior Resident Inspector

J. Park, Reactor Inspector

C. Phillips, Project Engineer

D. Tesar, Resident Inspector

Approved By:

Kenneth R. Riemer, Chief

Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Quad Cities Nuclear Power Station,

Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

Licensee-identified non-cited violations are documented in report sections: 71111.05Q.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000254,05000265/

2017-002-01 LER 2017-002-01 for Quad Cities Nuclear Power Station,

Unit 1, Four Main Steam Isolation Valves (MSIVs)

Closure Times Exceeded 71153 Closed LER 05000254,05000265/

2018-001-01 LER 2018-001-01 for Quad Cities Nuclear Power Station,

Unit 2, Two Main Steam Isolation Valves (MSIVs)

Closure Times Exceeded 71153 Closed LER 05000254,05000265/

2019-001-00 LER 2019-001-00 for Quad Cities, Unit 1, HPCI System Inoperable Due to Blown Fuse in the Motor Speed Changer Circuit 71153 Closed

PLANT STATUS

Unit 1

The unit began the inspection period shut down for refueling outage Q1R25. Startup on Unit 1 was commenced on April 6, 2019, and the unit was synchronized to the grid on April 7, 2019.

The unit reached full rated thermal power on April 9, 2019, where it remained for the entire inspection period with the exception of planned power reductions for turbine testing, control rod pattern adjustments, and other short-term power reductions as requested by the transmission system operator.

Unit 2

The unit began the inspection period at full rated thermal power, where it remained for the entire inspection period, with the exception of short-term power reductions as requested by the transmission system operator.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated readiness to cope with external flooding for the following areas:
  • Units 1 and 2 turbine building during rising Mississippi River levels on April 1, 2019

Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather (summer/ hot weather) conditions prior to the onset of extreme temperatures for the following systems:
  • transformer cooling, adjustable speed drive cooling, offsite power systems

Summer Readiness Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated summer readiness of offsite and alternate alternating current (AC) power systems on May 10, 2019

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1B core spray during refueling outage Q1R25 on April 1, 2019
(2) Units 2A and 2B core spray during Unit 2 high pressure coolant injection system maintenance on April 30, 2019
(3) Unit 1/2 emergency diesel generator during unavailable Unit 1 emergency diesel generator on May 9, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (3 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire zone 1.2.1; Unit 1 reactor building, elevation 544-0/666-6, drywell and drywell expansion gap on April 3, 2019
(2) Fire zone 11.1.1 A, B, C; Unit 1 turbine building, elevation 547-0, residual heat removal service water pumps on May 27, 2019
(3) Fire zone 8.2.8.E; Units 1 and 2 turbine building, elevation 639-0, main turbine floor (outside shield wall) on June 25, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the following areas:

(1) Units 1 and 2 residual heat removal service water vaults on April 29, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated the Unit 1 start-up from refueling outage Q1R25 on April 6, 2019

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated training scenarios in the simulator on June 24, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1)345 kV system (2)4kV switchgear

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Q1R25 outage shutdown safety and Unit 2 online risk the week of April 1, 2019 (2)repair instrument air leak on containment vent valve on April 16, 2019
(3) Unit 1B adjustable speed drive (ASD) speed hold and severe weather during week of April 23, 2019
(4) Work week risk for weeks of May 27 and June 3, 2019
(5) Emergent work and operational risk activity for repairs on the Unit 1B ASD cooling water leak the week of June 24, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (4 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Issue Report 4238910, RV 1-1402-28A Set-Point Test Exceeded 10-Year Test Frequency, on April 15, 2019
(2) Issue Report 4242536, Unexpected Speed Hold on [1] B ASD, on April 23, 2019
(3) Issue Report 4236078, EDG [emergency diesel generator] to ESS [essential service system] BUS Ducts in EQ [environmental qualification] Harsh Zones, on May 8, 2019
(4) Issue Report 4258635, B CREVS [control room emergency ventilation system]

Rough Pre-Filters Installed Backwards, on June 20, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change 402298, U1 Core Spray Pipe Repairs In-Vessel, which performs structural replacement of the P4D weld at the core spray piping downcomer-to-shroud elbow on April 1, 2019
(2) QOA 4700-06, Loss of Instrument Air, procedure number 28 on June 16, 2019

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance tests:

(1) Residual heat removal pump/loop operability test following outage on April 1, 2019
(2) QCOS 0201-08, Reactor Vessel Class 1 and Associated Class 2 System Leak Test, following refueling outage Q1R25 on April 3, 2019
(3) QCOS 0250-12, MSIV (main steam isolation valve) Stroke Test, and QCOS 0250-04, MSIV Closure Timing Following Q1R25 Maintenance, on April 5, 2019
(4) Scram Time Testing of Control Rods Following Outage work on April 5, 2019
(5) Work Order 4877341 (QCOS 5750-04), Quarterly Testing of Control Room HVAC (heating, ventilation, and air conditioning) System Valves and Dampers, following B Train Control Room Emergency Ventilation Maintenance on April 12, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The Inspectors Evaluated Unit 1 Refueling Outage Q1R25 Activities that Continued into the Second Quarter (began on March 18, 2019) and Completed on April 6, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1) QCOS 1200-01, RWCU (reactor water cleanup) Power Operated Valve Testing, on April 1, 2019

RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) Core Flow Calibration on April 9, 2019

Surveillance Tests (other) (IP Section 03.01) (2 Samples)

(1) Division II Emergency Core Cooling System Simulated Auto Initiation With Diesel Auto Start and load on April 3, 2019
(2) Surveillance Test Interval Change Request QC-18-008: Revised TS [Technical Specification] SR (Surveillance Requirement) for the HPCI (high pressure coolant injection]/RCIC (Reactor Core Isolation Cooling] Low Pressure Flow Rate and RCIC Automatic Initiation Testing from 24-Months to 48-Months, on May 29, 2019

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) Emergency preparedness drill on May 21,

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)

The inspectors reviewed the following gaseous and liquid effluent monitor instrument calibrations and tests:

(1)

  • Unit 1 Reactor Building Vent Monitor
  • Main Chimney Special Particulate Iodine Noble Gas Monitor
  • Radioactive Waste Liquid Effluent Monitor

Dose Calculations (IP Section 02.05) (1 Sample)

The inspectors reviewed the following to assess public dose:

(1) The inspectors reviewed the following liquid and gaseous discharge permits to evaluate public dose calculations:
  • Liquid Discharge, Permit Number 2018004
  • Liquid Discharge, Permit Number 2018005
  • Gaseous Discharge, Permit Number 2019199
  • Gaseous Discharge, Permit Number 2019201
  • Gaseous Discharge, Permit Number 2019203

The inspectors reviewed the following annual radiological effluent release reports:

  • 2017 Radioactive Effluent Release Report
  • 2018 Radioactive Effluent Release Report

The inspectors also reviewed the following abnormal gaseous or liquid tank discharges:

  • none were available for review during this inspection

Instrumentation and Equipment (IP Section 02.04) (1 Sample)

The inspectors reviewed the following radioactive effluent discharge system surveillance test results:

(1)

  • Stand-By Gas Treatment System
  • Control Room Ventilation System

Sampling and Analysis (IP Section 02.03) (1 Sample)

The inspectors reviewed the following:

(1)

  • Main Chimney
  • Unit 1 Reactor Building Vent
  • Unit 2 Reactor Building Vent

Effluent discharges with inoperable monitors

  • none were available for review during this inspection

Walk Downs and Observations (IP Section 02.01) (1 Sample)

The inspectors walked down the following gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design:

(1)

  • Main Chimney Monitoring System
  • Unit 1 Reactor Building Vent Monitoring System
  • Unit 2 Reactor Building Vent Monitoring System

71124.07 - Radiological Environmental Monitoring Program

Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)

(1) The inspectors examined the remediation efforts associated with the 2018 Radwaste Piping Vault Leak and other historical leaks at the facility.

Site Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the radiological environmental monitoring program implementation.

(1) Walkdowns, Calibrations, and Maintenance Record Review
  • Air Sampling Station Q-01
  • Air Sampling Station Q-02
  • Air Sampling Station Q-04
  • Optically Stimulated Luminescent Dosimeter (OSLD) Monitoring Station Q-01
  • OSLD Monitoring Station Q-02
  • OSLD Monitoring Station Q-04

Environmental Sample Collections and Preparation Observation

  • Water Sample Q-33
  • Water Sample Q-34

Licensee Actions in Response to Missed Sample, Inoperable Sampler, Lost TLD or Anomalous Measurement

  • Q-01 (AI) (Air Sample); 01/04/2019; No Sample, Power Outage
  • Q-36 (WW) (Well Water); 01/10/2019; Sample leaked during transportation.

New Sample Completed 01/14/2019.

  • Q-33 (SW) (Surface Water); 01/05/2019; No Sample, Water Frozen

Sampling Program for the Potential of Licensed Material Entering Groundwater

  • Monitoring Well QC-GP-18
  • Remediation Well RW-1
  • Radwaste Piping Vault

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI02: RCS Leak Rate Sample (IP Section 02.11)===

(1) Unit 1 (04/01/2018-03/31/2019)
(2) Unit 2 (04/01/2018-03/31/2019)

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1)10/01/2018 - 03/31/2019

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in drywell radiation monitor failures that might be indicative of a more significant safety issue on June 21, 2019.

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 265/2018-001-01 Two Main Steam Isolation Valves (MSIVs) Closure Times Exceeded (ADAMS Accession: ML19115A142). The inspectors reviewed the updated LER submittal. The previous LER submittal was reviewed in Inspection Report 05000254/ 2018002; 05000265/ 2018002.
(2) LER 254/2017-002-01, Four Main Steam Isolation Valves (MSIVs) Closure Times Exceeded (ADAMS Accession: ML19115A136). The inspectors reviewed the updated LER submittal. The previous LER submittal was reviewed in Inspection Report 05000254/2017002; 05000265/2017002.
(3) LER 254/2019-001-00, HPCI System Inoperable Due to Blown Fuse in the Motor Speed Changer Circuit (ADAMS Accession: ML19095A380). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71111.05Q This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Quad Cities Units 1 and 2 license condition 3.F requires the licensee to implement and maintain, in effect, all provisions of the approved fire protection program as described in the Final Safety Analysis Report and as approved through Safety Evaluation Reports dated July 27, 1979, with supplements dated November 5, 1980, and February 12, 1981; December 30, 1982; December 1, 1987 with supplement dated April 20, 1988; December 11, 1987 with supplement dated July 21, 1988; and February 25, 1991.

The Updated Final Safety Analysis Report Section 9.5.1, Fire Protection System, states Quad Cities Administrative Procedures (QCAP) define the fire protection program by assigning responsibilities, defining the organization, and providing information and procedures pertinent to fire protection. These procedures provide the Administrative Technical Requirements for fire protection and safe shutdown equipment and specify surveillance requirements for the applicable systems and equipment.

QCAP 1500-01, Administrative Requirements for Fire Protection, 39, outlines the administrative requirements for the fire protection system.

QCAP 1500-01, Procedure - Fire Detection System, section D.1.a.(d), states in part:

IF supervisory device listed in Attachment A is inoperable, THEN perform one of the following:

-Test detection system at a frequency of once per month OR

-declare system inoperable

Contrary to the above, from March 23, 2019 to May 16, 2019, the licensee failed to maintain in effect all provisions of the approved fire protection program. Specifically, on March 23, 2019, the licensee documented in Issue Report 4232291 that fire alarm system (FAS) device 32-24 was in alarm and initiated an impairment for the device. Fire alarm system device 32-24 was a supervisory device for the Unit 1 residual heat removal service water vaults and was an emergency fire protection system listed in Attachment A of QCAP 1500-01. From March 23, 2019, to May 16, 2019, the licensee failed to either declare supervisory device 32-24 inoperable or test the detection system at a frequency of once per month.

Significance: Green. The inspectors determined the issue was more than minor because the performance deficiency was associated with the Mitigating Systems cornerstone attribute of Protection Against External Factors (fire) and it adversely affect the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).

The inspectors determined the significance of the finding could be determined using Inspection Manual Chapter (IMC) 0609, Appendix F, Fire Protection Significance Determination Process, dated May 2, 2018. The inspectors used IMC 0609, Appendix F, 1, Fire Protection Significance Determination Process Worksheet, and determined the finding needed to be assigned a fire degradation rating using IMC 0609, Appendix F, Attachment 2, Degradation Rating Guidance. The inspectors concluded the finding represented a high fire degradation rating because the finding was related to fire detection and annunciators were disabled, inaudible, or nonfunctional. Specifically, FAS device 32-24 was non-functional, and control room annunciators would not have alerted operators of a fire in the Unit 1 residual heat removal service water vaults (local alarm panel annunciation was available).

In IMC 0609, Appendix F, Attachment 1, Step 1.4.2: Fixed Fire Protection Systems, the inspectors determined that the non-functional detection system did not adversely affect the ability of the system to protect any equipment important to safe shutdown. The affected residual heat removal service water rooms were supplied with a fixed fire suppression system that were always functional. Therefore, the inspectors determined the finding was of very low safety significance (Green).

Corrective Action References: The licensee identified this issue in condition report Issue Report 4251296. The licensee corrected this concern on May 16, 2019, when FAS device 32-24 was repaired and tested.

Observation: Drywell Radiation Monitor Failures 71152 The inspectors reviewed recent failures of the 2A drywell radiation monitors as documented in IRs 4251706 and 4258115, written on May 24 and June 19, 2019, respectively. Both failures were attributed to dirty contacts in the radiation monitor chassis. After the first failure, documented under IR 4251706, the licensee was able to clean the contacts in the detector chassis and retested it satisfactorily. In the most recent failure documented in IR 4258115, the licensee documented that they had replaced the detector chassis and attributed the failure of the chassis to dirty contacts in the detector selector switch. The licensee decided to replace the entire chassis because this was the second failure of the detector within the previous month. The failed chassis was sent to Power Labs for a failure analysis under assignment number 05 (IR 4258115-05). The inspectors recommend the biennial problem identification and resolution (PI&R) team review the results of the failure analysis and any licensee generated corrective actions. In addition, the licensee discussed that all four drywell radiation monitor chassis (2 per unit) sit in the same environment; they are close to the floor in the control room and susceptible to dust intrusion. The licensee also documented in IR 4251706 that IR 4252208 assignment number 04 was created to evaluate if a preventative maintenance change frequency was warranted for the drywell radiation monitors. The inspectors recommend the biennial PI&R team review both the licensee's evaluation of IR 4252208 assignment number 04 and the performance of all of the drywell radiation monitors because they are in a similar environment. The licensee's corrective actions should address the extent of cause and condition.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On June 6, 2019, the inspectors presented the radiation protection inspection results to Mr. K. Ohr, Site Vice President, and other members of the licensee staff.
  • On July 11, 2019, the inspectors presented the integrated inspection results to Mr. K. Ohr, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

or Date

71111.01

Corrective Action

Documents

IR 4238374

U1 Main Transformer Leaking Oil

04/11/2019

IR 4244757

1A ASD Temporary Cooling Needed for Summer Readiness

04/30/2019

IR 4244760

1B ASD Temporary Cooling Needed for Summer Readiness

04/30/2019

IR 4244763

2A ASD Temporary Cooling Needed for Summer Readiness

04/30/2019

IR 4244768

2B ASD Temporary Cooling Needed for Summer Readiness

04/30/2019

Miscellaneous

Advanced Nuclear Dispatch, Number: 229

2/26/2016

Nuclear Load Following Congestion Relief Program;

Number: 219

11/18/2014

Risk Issue

Number: QDC-2-

2019-0124

ODM: U2 Main

SPOG: 1-3-C

Station 4 Quad Cities Units 1 and 2 Special Protection

System

Procedures

OP-AA-102-102

General Area Checks and Operator Field Rounds

OP-AA-108-107

Switchyard Control

OP-AA-108-107-

1001

Station Response to Grid Capacity Conditions

OP-AA-108-107-

1002

Interface Procedure Between BGE/ComEd/PECO and

Exelon Generation (Nuclear/Power) for Transmission

Operations

QCOA 0010-16

Flood Emergency Procedure

QCOA 6100-03

Loss of Offsite Power

WC-AA-107

Seasonal Readiness

WC-QC-8003-

1008

Quad Cities Station Units 1 and 2, Nuclear Plant Interface

Requirements (NPIRs)

Work Orders

Contingency Seasonal Readiness Work Orders

71111.04

Procedures

AD-AA-101-F-10

Unit 1 Core Spray System Preparation for Standby

Operation

QCOP 1400-09

Unit 2 Core Spray System Preparation for Standby

Operation

QCOP 6600-04

Diesel Generator 1/2 Preparation for Standby Operation

QOM 2-1400-08

Core Spray System Fuse and Breaker Checklist

Inspection

Procedure

Type

Designation

Description or Title

or Date

QOM 2-1400-09

2A Core Spray Valve Checklist

QOM 2-1400-10

2B Core Spray Valve Checklist

QOM-1-1400-10

Unit 1B Core Spray Valve Checklist

71111.04S

QCOP 6600-04

Diesel Generator 1/2 Preparation for Standby Operation

QCOP 6600-24

Unit 2 Diesel Generator Preparation for Standby Operation

QOM 0-6600-01

Unit 0 Diesel Generator Valve Checklist

QOM 2-6600-01

Unit 2 Diesel Generator Checklist

71111.05Q Corrective Action

Documents

CR 4251296

Missed QCAP 1500-01 Actions

05/23/2019

IR 4232291

FAS Device 32-24 and 52-11 Alarm

03/23/2019

IR 4251296

Missed QCAP 1500-01 Actions

05/23/2019

Drawings

Drawing F-264

Fire Suppression System RHR Service Water Pumps Area G

Control Rod Drive Feed Pumps Area J

H

Engineering

Changes

EC 623395

Temporary Supplemental Cooling to the ASD Cabinets

EC 623395

CC-AA-209; Approved Fire Protection Program

Configuration Change Impact Review

Fire Plans

Fire Zone 8.2.8.E

Unit 1 TB 639-0 Elev. Main Turbine Floor (Outside Shield

Wall)

June 2010

FZ 11.1.1 A, B,

and C

Unit 1 TB 547-0 Elev. RHR Service Water Pumps

March 2012

FZ 11.1.1.B

Unit 1 RHR Service Water Pump Room

FZ 11.1.1.C

Unit 1 RHR Service Water Pump Room

Procedures

ER-AA-425-1001

Surveillance Test Interval (STI) Evaluation Form

QCAP 1500-01

Administrative Requirements for Fire Protection

QCMM 5700-04

Installation and Removal of ASD Temporary Cooling Units

QCOA 4100-11

TRX(I) Supervisory (Trouble) Devices Monitoring Local

System Panels

71111.12

Corrective Action

Documents

IR 4121737

Unexpected Trip of GCB 3-4 In 345kV Switchyard

04/01/2018

IR 4234556

QDC Readiness to Replace/Address a Failed 4kV/480V

XFMR

03/30/2019

IR 4247012

Create WO to Document Risk Assessment for 345 kV

Switching

05/07/2019

IR 4247090

MRule A1DE Required for SY9700-01, 345kV Switchyard

05/07/2019

IR 4250438

Issue in IR 4233332 Requires MRFF Processing

05/20/2019

Inspection

Procedure

Type

Designation

Description or Title

or Date

71111.13

Miscellaneous

Tagout: 02-IA-

240FIX-001

2/11/2019

Procedures

OP-AA-109-103

Tag-Out Requester Checklist; WO 04768967-01

01/14/2019

WC-AA-104-F-01

Risk Screening/Mitigation Plan; MM Repair Instrument Air

Leak on Solder Joint WO 04768967-01

01/14/2019

71111.15

Corrective Action

Documents

IR 4236078

EDG to ESS Bus Ducts in EQ Harsh Zones

04/03/2019

IR 4238910

RV 1-1402-28A Set-Point Test Exceeded 10-Year Test

Frequency

04/12/2019

IR 4242536

Unexpected Speed Hold on B ASD

04/23/2019

IR 4258635

B CREVS Rough Pre-Filters Installed Backwards

06/21/2019

Drawings

Drawing 4E-1426

Recirculating Pump ASD 1B Input Breaker Control

J

Drawing 4E-1426

Recirculating Pump ASD 1B Input Breaker Control

E

Drawing 4E-

6577F

ATWS Recirc Pump Trip System ECCS INIT-FW, RCIC,

HPCI and Turb Trips Div I and Div II - Part 6

T

Engineering

Changes

EC 440244

Review Use of Materials in Non-Seg Bus Routed from EDGS

to Dash Busses through EQ Harsh Zones

ECR 441826

Engineering Evaluate Acceptability of Filters for the Control

Room HVAC Charcoal Absorber Installed Backwards

06/20/2019

Miscellaneous

Consolidated Safety Relief Valve Sizing and Selection

Report for Core Spray Pump Discharge Over Fire Protection

08/07/2013

ASME OM Code-

2004

Code for Operation and Maintenance of Nuclear Power

Plants

Procedures

QCAN 901(2)-4

C-5

Recirculation Adjustable Speed Drive B Speed Hold

QCOA 0202-08

Reactor Recirculation Control System Trouble

QCOA 0202-08

D; RRCS/ASD Event List

QCOS 0202-19

Online Testing of Unit 1 Division I ATWS Recirculation Pump

Trip and Alternate Rod Insertion Logic

QCOS 0202-20

Online Testing of Unit 1 Division II ATWS Recirculation

Pump Trip and Alternate Rod Insertion Logic

UFSAR 7.8

Anticipated Transient Without Scram Mitigation System

Work Orders

WO 1817554

Flushing Cores Spray Lines into Reactor (IST)

03/27/2017

71111.18

Miscellaneous

FWAA 4227272-

66-08

NC-19-004-Y, Yellow NER for Fitzpatrick Loss of Instr Air

Inspection

Procedure

Type

Designation

Description or Title

or Date

Procedures

DOA 4700-01

Instrument Air System Failure

OP-AA-101-111

Roles and Responsibilities of On-Shift Personnel

OP-AA-101-111-

1001

Operations Standards and Expectations

OP-QC-103-102-

1002

Quad Cities Strategies for Successful Transient Mitigation

71111.19

Corrective Action

Documents

IR 4230579

PSU Leakage Identified on the 0203-1D Inboard MSIV

03/18/2019

IR 4235323

1D RHR Pump Tripped During QCOS 1000-06

04/01/2019

Miscellaneous

Inservice Testing

Bases Document

Valve EPN: 0-5741-319A-AO; CR HVAC-B Train RCU HX

RHRSW Supply Isolation

Inservice Testing

Bases Document

Valve EPN: 0-5741-319B-AO; CR HVAC-B Train RCU HX

Serv Wtr Supply Isolation

Procedures

QCOS 0250-04

MSIV Closure Timing (PMT for MSIV Outage Maintenance)

QCOS 0250-12

MSIV Closure Scram Sensor Channel Outage Functional

Test

QCOS 1000-06

RHR Pump/Loop Operability Test

QCOS 5750-04

Quarterly Testing of Control Room HVAC System Valves

and Dampers

Work Orders

WO 4832132

CRD Scram Timing in Hot Condition (IST)

04/07/2019

WO 4877341

Control Room HVAC System Check Vlv Test (IST)

04/08/2019

WO 4911981

RHR C Pump Flow Rate (IST)

04/01/2019

WO 4911983

RHR D Pump Flow Rate (IST)

04/02/2019

71111.20

Corrective Action

Documents

IR 4230600

PSU Q1R25 As Found MSIV 1B LLRT Exceeds TS Limit

<34

03/18/2019

IR 4231752

PSU Q1R25: Failed Relay

03/21/2019

IR 4231753

Found Bad Relay for HPCI Circuit

03/21/2019

IR 4231897

Fatigue Assessment IR

03/21/2019

IR 4232031

Rapid Trending Identified Negative Trend in FME

03/22/2019

IR 4232329

Foreign Material Event - Unit 1 Reactor Vessel

03/23/2019

IR 4232493

WHR Fatigue Assessment

03/24/2019

IR 4232916

Incorrect Valve Tag Removed

03/25/2019

IR 4236198

Unable to Perform DW Spray Header Air Flow Test

04/04/2019

IR 4236574

MSIV-1-0203-1A As-Left Thrust Readings Less Than As-

04/05/2019

Inspection

Procedure

Type

Designation

Description or Title

or Date

Found

Drawings

Diagram 4E-

1331A

Relaying and Metering Diagram Generator and Main Power

Transformer 1

Drawing 4E-1331 Relaying and Metering Diagram Generator and Main

Transformer 1

BB

Drawing 4E-1338

Schematic Diagram Generator and Transformer Tripping

Relays Primary System

AY

Miscellaneous

Haul/Deployment Paths

01/03/2019

Shutdown Safety

Log #01

Modification Activities for Q1R25

01/09/2019

Shutdown Safety

Log #02

Q1R25 Shutdown Safety FLEX Considerations

01/09/2019

Shutdown Safety

Log #03

List of High Risk Activities and First Time Activities for

Q1R25

01/09/2019

Shutdown Safety

Log #04

Communication Plan for Q1R25

01/09/2019

Shutdown Safety

Log #05

List of System Health Review for Q1R25

01/16/2019

Procedures

MA-AA-736-620

Application of Freeze Seal Using RIDGID SuperFreeze

SF-2500

NF-AB-715

Critical Prediction Checklist

NF-AB-720-F-1

Control Rod Sequence Review and Approval Sheet for Unit

Cycle 26

OU-AA-103

Shutdown Safety System Health Review

QCGP 1-1

Normal Unit 1 Startup

115

QCOP 1000-24

Draining Reactor Cavity and Vessel to the Torus

QCOS 0201-02

Primary System Boundary Thermal Limitations

QCOS 0201-02

Reactor Thermal Limitations Surveillance Data Sheet

Work Orders

WO 4628169

Core Verification

03/31/2019

71111.22

Corrective Action

Documents

IR 4232248

PSU Q1R25 FW CV 1-0220-62A Exceeded Required Action

Limit

03/23/2019

IR 4232654

Q1R25 LLRT 1-2001-3 Leakage Could Not Be Quantified

03/25/2019

IR 4235847

Q1R25 RPV Class 1 & Class 2 System Leakage Test

Results

04/03/2019

Inspection

Procedure

Type

Designation

Description or Title

or Date

Procedures

ER-AA-425

Implementation of the Technical Specification Surveillance

Frequency Control Program

QCOS 1000-31

1A Loop LPCI and Containment Cooling Modes of RHR

Non-Outage Logic Test

QCOS 6600-50

Unit One Division II Emergency Core Cooling System

Simulated Automatic Actuation and Diesel Generators

Auto-Start Surveillance

STI Change

Request Number

QC-18-008

Review the Frequency of Technical Specification (TS)

Surveillance Requirements (SR) for the HPCI/RCIC Low

Pressure Flow Rate and RCIC Automatic Initiation Testing

from 24 Months to 48 Months

Work Orders

WO 1659536

Part 21 Issue on 1-1201-2

03/30/2019

WO 4620642

MM Part 21 Action Item for MOV 1-1201-5 in Q1R25

04/01/2019

WO 4690630

Core Flow Calibration

04/09/2019

WO 4907182

RX WTR Cleanup Valve Timing Test (IST)

04/07/2019

71124.06

Calculations

Permit Number

2018005

Liquid Release Permit Report - River Discharge Tank

05/04/2018

Permit Number

2019191

Gaseous Release Permit Report - Main Chimney Noble Gas

Unit 1+2

06/03/2019

Permit Number

2019193

Gaseous Release Permit Report - Reactor Vent Noble Gas

Unit 1

06/03/2019

Permit Number

2019199

Gaseous Release Permit Report

06/04/2019

Permit Number

2019201

Gaseous Release Permit Report

06/04/2019

Permit Number

2019203

Gaseous Release Permit Report - Reactor Vent Iodine and

Particulate Unit 2

06/04/2019

Release Report

2019004

Liquid Release Permit Report - Discharge Bay

05/01/2019

Miscellaneous

CY-QC-170-301

Offsite Dose Calculation Manual Quad Cities Station Units 1

and 2

SVP-18-029

Radioactive Effluent Release Report for 2017

04/27/2018

SVP-19-026

Radioactive Effluent Release Report for 2018

04/30/2019

Procedures

CY-QC-110-605

Reactor Building Cent Gaseous & Particulate Sampling

Inspection

Procedure

Type

Designation

Description or Title

or Date

CY-QC-110-606

Main Chimney Gaseous & Particulate Sampling

CY-QC-120-735

Main Chimney & Reactor Building Vent Noble Gas Release

Rate

Work Orders

01836282-01

Stand-By Gas Treatment Charcoal Absorber Test

05/10/2017

01906646-01

Technical Support Center Charcoal Absorber Surveillance

09/07/2017

01918595-01

Control Room Emergency Filtration System Charcoal

Absorber

10/11/2017

04635819-01

Main Chimney Noble Gas Monitor Calibration

03/06/2019

04670696

Service Water Monitor Calibration

2/20/2018

0467582-01

Radwaste Effluent Monitor Calibration

01/04/2019

04876363-01

Reactor Building Vent/Fuel Pool Rad Monitor

Calibration/Functional Test

2/20/2019

71124.07

Corrective Action

Documents

04120126

Water Found in Radwaste Piping Vault

03/28/2018

04136730

REMP 2018 1st Quarter Missing/Anomalies Samples

05/11/2018

202852

REMP Air Sampler Station Found Without Power

2/07/2018

249167

1st Quarter 2019 Missed REMP Samples

05/15/2019

Miscellaneous

Quad Cities Nuclear Power Station, Units 1 and 2 Annual

Radiological Environmental Operation Report

05/10/2019

Meteorological Monitoring Program at the Quad Cities

Nuclear Generating Station January 2019

03/21/2019

Meteorological Monitoring Program at the Quad Cities

Nuclear Generating Station February 2019

04/25/2019

Procedures

EIML-SPM-1

Sampling Procedures Manual Environmental Incorporated

Midwest Laboratory

EN-AA-407

Response to Inadvertent Releases of Licensed Materials to

Groundwater, Surface Water, Soil or Engineered Structures

EN-AA-408

Radiological Groundwater Protection Program

EN-AA-408-4000

Radiological Groundwater Protection Program

Implementation

EN-QC-408-4160

Quad Cities Station Radioactive Groundwater Protective

Program Reference Material

71151

Miscellaneous

CY-QC-120-720

Actual Dose Data and Supporting Information Package

10/31/2018

through

03/31/2019

Inspection

Procedure

Type

Designation

Description or Title

or Date

Procedures

CY-QC-120-720

Plant Effluent Dose Calculations

71152

Corrective Action

Documents

IR 3990038

MSIVs 1-0203-1B, 1-0203-1D, 1-0203-2C and 1-0203-2D

Closure Times Exceeded the Maximum Technical

Specification Limit of <5 Seconds

03/27/2017

IR 4116642

MSIVs 2-0203-1A and 2-0203-1C Closure Times Exceeded

the Maximum Technical Specification Limit of <5 Seconds

03/19/2018

IR 4230672

EO ID: 1C RHRSW HP O/B Seal Leaking

03/18/2019

IR 4231463

HPCI Motor Speed Changer Cycling Off of High Speed Stop

03/21/2019

IR 4232959

Bus 19 Main Feed Breaker Failed to Trip During Crosstie

03/26/2019

IR 4233634

Paint Flaking from Refuel Floor Ceiling (FME)

03/27/2019

IR 4234060

Evaluation of Paint Chips that Fell from RB Overhead

03/28/2019

IR 4235733

Rising Trend on PI 2-0262-17D 2B Recirc Pump OB Seal

Press

04/02/2019

IR 4237779

MCR Alarm Not Received on 902-56 Panel

04/09/2019

IR 4238831

1C RHRSW High Pressure Pump OB Seal Leak During Run

04/12/2019

IR 4245286

VT3 of Support M-994D-22 During Q1R26

05/01/2019

IR 4251168

Logic Test Discrepancies and Improvements QCOS 1000-31

05/23/2019

IR 4251706

The U2 A Drywell Rad Monitor (2-2419A) Failed Downscale

05/24/2019

IR 4252249

OOT, RIS 1-2419-A, Trend Code B3

05/28/2019

IR 4258115

U2 A Drywell Radiation Monitor, 2-2419A, Failed

Downscale

06/19/2019

IR 4259369

MRule A1DE Required for CM2400-02, Unit 2 DW Rad

Monitor

06/25/2019

Drawings

Drawing M-37

Diagram of RHR Service Water Piping

BI

Procedures

QCIS 2400-04

Unit 2 Division I Drywell Radiation Monitor Calibration and

Functional Test

Work Orders

WO 4924935

The Unit 2 A Drywell Rad Monitor Failed Downscale

05/28/2019

71153

Corrective Action

Documents

ECAPE 4217557

U1 HPCI Failed to Roll During QCOS 2300-27

03/08/2019