IR 05000245/2012002

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IR 05000336-12-002, 05000423-12-002, on 1/1/12-3/31/12, Millstone Units 2 and 3, Routine Quarterly Integrated Report
ML12114A204
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 04/23/2012
From: Bellamy R R
NRC/RGN-I/DRP/PB5
To: Heacock D
Dominion Resources
References
IR-12-002
Download: ML12114A204 (30)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PENNSYLVANIA 19406-1415 April 23, 2012

Mr. David Heacock President and Chief Nuclear Officer Dominion Resources 5000 Dominion Boulevard Glen Allen, VA 23060-6711

SUBJECT: MILLSTONE POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000336/2012002 AND 05000423/2012002

Dear Mr. Heacock:

On March 31, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Millstone Power Station, Units 2 and 3. The enclosed inspection report documents the inspection results, which were discussed on April 19, 2012 with Mr. Stephen E. Scace, Site Vice President, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

No NRC-identified or self-revealing findings were identified during this inspection.

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ Ronald R. Bellamy, Chief Reactor Projects Branch 5 Division of Reactor Projects

Docket Nos.: 50-336, 50-423 License Nos.: DRP-65, NPF-49

Enclosure:

Inspection Report 05000336/2012002 and 05000423/2012002

w/Attachment:

Supplemental Information cc w/encl: Distribution via ListServ

SUMMARY OF FINDINGS

........................................................................................................... 3 1. REACTOR SAFETY .............................................................................................................. 4 1R04 Equipment Alignment .............................................................................................. 4 1R05 Fire Protection ......................................................................................................... 5 1R11 Licensed Operator Requalification Program ........................................................... 5 1R12 Maintenance Effectiveness ..................................................................................... 6 1R13 Maintenance Risk Assessments and Emergent Work Control ............................... 7 1R15 Operability Determinations and Functionality Assessments ................................... 8 1R18 Plant Modifications .................................................................................................. 9 1R19 Post-Maintenance Testing ...................................................................................... 9 1R22 Surveillance Testing .............................................................................................. 10 1EP6 Drill Evaluation ...................................................................................................... 11 2. RADIATION SAFETY .......................................................................................................... 11 2RS01 Radiological Hazard Assessment and Exposure Controls .................................... 11 2RS02 Occupational ALARA Planning and Controls ........................................................ 12 2RS04 Occupational Dose Assessment ........................................................................... 13 4. OTHER ACTIVITIES ............................................................................................................ 14 4OA1 Performance Indicator Verification ........................................................................ 14 4OA2 Problem Identification and Resolution .................................................................. 15 4OA5 Other Activities ...................................................................................................... 15 4OA6 Meetings, Including Exit ........................................................................................ 17 ATTACHMENT: SUPPLEMENTARY INFORMATION................................................................ 17 SUPPLEMENTARY INFORMATION ........................................................................................

KEY POINTS OF CONTACT ....................................................................................................

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED .....................................

LIST OF DOCUMENTS REVIEWED ........................................................................................

LIST OF ACRONYMS .............................................................................................................

SUMMARY OF FINDINGS IR 05000336/2012002, 05000423/2012002; 1/1/2012-3/31/2012; Millstone Units 2 and 3; Routine Quarterly Integrated Report This report covered a three-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. No findings or violations were identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

REPORT DETAILS

Summary of Plant Status Millstone Unit 2 and Unit 3 began the inspection period operating at 100 percent power. On January 13, both units reduced power because of storm related fouling of the intake structure.

Unit 2 reduced power to 73 percent at 8:45 p.m. and resumed 100 percent power operations at 10:00 p.m. on January 14. Unit 3 reduced power to 80 percent at 8:20 p.m. on January 13 and resumed 100 percent power operations at 5:18 PM on January 14. On January 20, Unit 2 reduced power to 83 percent at 12:00 a.m. to replace seals on the 'B' and 'C' condensate pumps. On January 23, Unit 2 resumed 100 percent power operations at 2:43 a.m. On February 25, Unit 3 reduced power to 75 percent due to environmental factors affecting plant conditions. Unit 3 resumed to 100 percent power operations on February 27.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems: Unit 2 * 'B' Control Room Air Conditioning System (CRAC) while the 'A' CRAC was out of service (OOS) for repairs on March 21 * 'A' Emergency Diesel Generator (EDG) while the 'B' EDG was OOS for surveillance testing on March 28 Unit 3

  • Station Blackout (SBO) Diesel on March 30 The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the Updated Final Safety Analysis Report (UFSAR), technical specifications (TS), work orders, condition reports (CR), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Dominion staff had properly identified equipment issues and entered them into their corrective action program (CAP) for resolution with the appropriate significance characterization. Documents reviewed for each section of this inspection report are listed in the Attachment.

b. Findings

No findings were identified.

1R05 Fire Protection

Resident Inspector Quarterly Walkdowns (71111.05Q - 3 samples)

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that Dominion controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

Unit 2 * 'B' EDG Compartment, Fire Area A-16

  • East DC Switchgear Room, Fire Area A-20 Unit 3
  • SBO Diesel and Tank Enclosure, Fire Area SBO-1

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

a. Inspection Scope

The inspectors observed a licensed operator simulator training for Unit 2 on January 10, which included letdown controller malfunction followed by flooding in the turbine building and a rupture of the auxiliary feed water pump discharge piping. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the TS action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

The inspectors observed licensed operator simulator training for Unit 3 on January 17, which included a loss of condenser vacuum followed by a small break loss of coolant accident. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the technical specification action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

a. Inspection Scope

The inspectors observed and reviewed the crew's preparations for a potential TS shutdown due to inoperable Unit 3 Steam Generator (SG) pressure transmitters during the evening of February 9 and turbine valve testing on February 17. The inspectors observed infrequently performed tests or evolution briefings, pre-shift briefings, and reactivity control briefings to verify that the briefings met the criteria specified in Dominion's Operations Section Expectations Handbook and Dominion's Administrative Procedure OP-AA-329, "Conduct of Infrequently Performed Tests and Evolutions,"

Revision 1. Additionally, the inspectors observed test performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structures, systems, and components (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, maintenance work orders, and maintenance rule basis documents to ensure that Dominion was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria established by Dominion staff was reasonable. As applicable, for SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2). Additionally, the inspectors ensured that Dominion staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.

Unit 2

  • Radiation Monitoring System Unit 3
  • 480 VAC Motor Control Center Breakers

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that Dominion performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that Dominion personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When Dominion performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the station's probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

Unit 2

  • Moderate Trip Risk due to maintenance on 345 KV Line 310 which removed Unit 2's output tie to the North Bus on January 9
  • Yellow Risk due to the 'A' high pressure safety injection (HPSI) pump being out for testing on January 19
  • Increased Trip Risk due to 'B' condensate pump being taken OOS for repair immediately followed by a similar repair on the 'C' condensate pump starting on January 20 and finishing on January 23
  • Increased Trip Risk due to 'A' stator cooling pump being replaced on February 7 Unit 3
  • Unplanned loss of the 'A' EDG during surveillance testing with the 'A' HPSI pump, 'B' RPCCW pump, and 'A' TBCCW pump OOS on January 18
  • Extended maintenance period due to frequency fluctuation on the 'A' EDG during Preventive Maintenance Test (PMT) surveillance on February 21

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:

Unit 2

  • CR457554, Terry Turbine HELB door not fully contacting the knife edge
  • CR459124, 'B' condensate pump elevated mechanical seal leakage and its associated Operational Decision Making (ODM)
  • OD000468, 'A' EDG Governor Load Swings
  • CR464272, Rosemount Transmitter Part 21
  • CR464818, Ground Water Intrusion through ESF Cable Penetrations The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to Dominion's evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by Dominion. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.

b. Findings

No findings were identified.

1R18 Plant Modifications

.1 Temporary Modifications

a. Inspection Scope

The inspectors reviewed a temporary modification to the Unit 3 'D' SG level transmitter low level setpoint described in Temp Mod 3-12-005, "3FWS*LB547B 'D' SG Level Setpoint Change" to determine whether the modification affected the safety functions of systems that are important to safety. The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.

b. Findings

No findings were identified.

.2 Permanent Modifications

a. Inspection Scope

The inspectors evaluated a modification to the Unit 2 Refueling Water Storage Tank (RWST) remote temperature sensor implemented by design modification package DM2-00-0253-09, "Unit 2 RWST RTD Modification." The inspectors reviewed the 10 CFR 50.59 justification and verified that the design bases, licensing bases, TS and performance capability of the affected systems were not degraded by the modification.

In addition, the inspectors reviewed modification design documents associated with the design change for the replacement of the RTD temperature sensor with a modified, flexible RTD and walked down the proposed field installation site.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions.

Unit 2

  • Post Maintenance Test for 'A' stator cooling pump following a motor replacement on February 8
  • Post Maintenance Test for 'A' EDG following channel head replacement of the diesel jacket water heat exchanger on February 15 Unit 3
  • Post Maintenance Test for the 'A' EDG following routine maintenance and failed fuse replacement on February 21 * 'C' Condensate Pump following replacement on March 3
  • Post Maintenance Test for the 'A' EDG sequencer following replacement of the 15 volt and 48 volt power supplies on March 2
  • Post Maintenance Test for the 'A' EDG sequencer following the second replacement of the 48 volt power supplies on March 24
  • Post Maintenance Test for the TDAFW Pump Governor Speed Setting Issue on March 26

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TS, the UFSAR, and Dominion procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:

Unit 2

  • SP 2613L, "Diesel Generator Slow Start Operability Test, Facility 2," Revision 005-01
  • SP 2610BO-005, "TDAFP Operational Test form C-10," Revision 000-00
  • SP 2613N, "'A' EDG Operability Tests, SIAS Start, Facility 2," Revision 001-05
  • CP 2802N, "Primary Systems Sampling and Analysis," Revision 001-03 Unit 3

b. Findings

No findings were identified. Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

Training Observations

a. Inspection Scope

The inspectors observed a simulator training evolution for Unit 3 licensed operators on January 17, which required emergency plan implementation by an operations crew. Dominion planned for this evolution to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspector's activities was to note any weaknesses and deficiencies in the crew's performance and ensure that Dominion evaluators noted the same issues and entered them into their CAP.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstone:

Public and Occupational Radiation Safety

2RS0 1 Radiological Hazard Assessment and Exposure Controls

a. Inspection Scope

The inspectors performed walk downs of the Dominion facility, including radioactive waste processing, storage, and handling areas to evaluate material conditions and potential radiological conditions. The inspectors selected containers holding non-exempt licensed radioactive materials that may cause unplanned or inadvertent exposure of workers, and verified that they were labeled and controlled. During tours of the facility and review of ongoing work the inspectors evaluated ambient radiological conditions. The inspectors verified that existing conditions were consistent with posted surveys, radiation work permits (RWP), and worker briefings, as applicable. The inspectors verified that radiation monitoring devices were placed on the individual's body consistent with the method that Dominion was employing to monitor dose from external radiation sources. The inspectors verified that the dosimeter was placed in the location of highest expected dose or that Dominion was properly employing an NRC-approved method of determining effective dose equivalent. For high-radiation work areas with significant dose rate gradients (a factor of 5 or more), the inspectors reviewed the application of dosimetry to effectively monitor exposure to personnel. The inspectors verified that Dominion controls were adequate. The inspectors verified that problems associated with radiation monitoring and exposure control were being identified by Dominion at an appropriate threshold and were properly addressed for resolution in their CAP. In addition, the inspectors verified the appropriateness of the corrective actions for a selected sample of problems documented by Dominion that involve radiation monitoring and exposure controls. The inspectors determined that Dominion was assessing the applicability of operating experience to their plants.

b. Findings

No findings were identified.

2RS0 2 Occupational ALARA Planning and Controls

a. Inspection Scope

The inspectors obtained from Dominion a list of work activities ranked by actual or estimated exposure that occurred during the last outage (3R14), and selected work activities of the highest exposure significance.

The inspectors reviewed the as low as reasonably achievable (ALARA) work activity evaluations, exposure estimates, and exposure mitigation requirements. The inspectors determined that Dominion had reasonably grouped the radiological work into work activities, based on historical precedence, industry norms, and/or special circumstances. The inspectors verified that Dominion's planning identified appropriate dose mitigation features considered alternate mitigation features commensurate with the risk of the work activity and defined reasonable dose goals. The inspectors verified that Dominion's ALARA assessment had taken into account decreased worker efficiency from use of respiratory protective devices and or heat stress mitigation equipment. The inspectors determined that Dominion's work planning considered the use of remote technologies as a means to reduce dose and the use of dose reduction insights from industry operating experience and plant-specific lessons learned. The inspectors verified the integration of ALARA requirements into work procedure and radiation work permit (RWP) documents. The inspectors compared the results achieved with the intended dose established in Dominion's ALARA planning for these work activities. The inspectors compared the person-hour estimates provided by maintenance planning and other groups with the actual work activity performance, and evaluated the accuracy of these time estimates. The inspectors determined the reasons for any inconsistencies between intended and actual work activity doses. The inspectors focused on those work activities with planned or accrued exposure greater than 5 person-rem (Boric Acid Corrosion Control Program, insulation, mechanical maintenance, reactor disassembly/reassembly, scaffolding, SG work, and valve repairs).

The inspectors determined that post-job reviews were conducted and all issues identified were entered into Dominion's CAP.

The inspectors evaluated Dominion's method of adjusting exposure estimates, or re-planning work, when unexpected changes in scope or emergent work were encountered.

The inspectors determined that adjustments to exposure estimates were based on sound radiation protection and ALARA principles. The inspectors determined whether the frequency of these adjustments question the adequacy of the original ALARA planning process. The inspectors verified that issues associated with ALARA planning and controls were being identified by Dominion at an appropriate threshold and were properly addressed for resolution in their CAP.

b. Findings

No findings were identified.

2RS0 4 Occupational Dose Assessment

a. Inspection Scope

The inspectors reviewed the most recent National Voluntary Laboratory Accreditation Program (NVLAP) accreditation report pertaining to Dominion's dosimetry program. The inspectors reviewed Dominion procedures associated with dosimetry operations, including issuance/use of external dosimetry, assessment of internal dose, and evaluation of dose assessment for radiological incidents. The inspectors verified that Dominion had established procedural requirements for determining when external and internal dosimetry was required. The inspectors verified that Dominion's personnel dosimeters that require processing were NVLAP accredited. The inspectors verified the vendor's NVLAP accreditation.

The inspectors ensured that the approved irradiation test categories for each type of personnel dosimeter used were consistent with the types and energies of the radiation present, and the way that the dosimeter was being used. The inspectors selected dosimetry occurrence reports or CAP documents for adverse trends related to electronic dosimeters. The inspectors determined that Dominion had not identified any trends and where appropriate, implemented appropriate corrective actions. The inspectors reviewed procedures used to assess dose from internally deposited nuclides using whole body counting equipment. The inspectors verified that the procedures addressed methods for determining if an individual was internally or externally contaminated, the release of contaminated individuals, the determination of entry route, and assignment of dose.

The inspectors verified that the frequency of such measurements was consistent with the biological half-life of the potential radionuclides available for intake. The inspectors evaluated the minimum detectable activity (MDA) of instrument. The inspectors determined that the MDA were adequate to determine the potential for internally deposited radionuclides sufficient to prompt additional investigation. The inspectors verified that the system used in each bioassay had sufficient counting time/low background to ensure appropriate sensitivity for the potential radionuclides of interest. The inspectors verified that the appropriate radionuclide library was used. The inspectors verified that any anomalous count peaks indicated in each output spectra received appropriate disposition.

The inspectors reviewed the counting laboratory's QA program and verified that if a vendor lab is used, Dominion audits of the lab were conducted. The inspectors verified that the lab participated in an analysis cross-check program and that out-of-tolerance results were evaluated and resolved appropriately. The inspectors reviewed Dominion's methodology for monitoring external dose in situations where non-uniform fields are expected or large dose gradients exist. The inspectors verified that Dominion had established criteria for determining when alternate monitoring techniques were to be implemented. The inspectors reviewed dose assessments performed using multi-badging during the current assessment period. The inspectors verified that the assessments were performed consistently with Dominion procedures and dosimetric standards. The inspectors evaluated Dominion's neutron dosimetry program, including dosimeter type(s) and/or survey instrumentation. The inspectors verified that problems associated with occupational dose assessment were being identified by Dominion at an appropriate threshold and were properly addressed for resolution in their CAP. In addition, the inspectors verified the appropriateness of the corrective actions for a selected sample of issues documented by Dominion.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

Reactor Coolant System (RCS) Specific Activity and RCS Leak Rate

a. Inspection Scope

The inspectors reviewed Dominion's submittal for the RCS specific activity and RCS leak rate performance indicators for both Unit 2 and Unit 3 for the period of January 1, 2011 through December 31, 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors also reviewed RCS sample analysis and control room logs of daily measurements for RCS leakage, and compared that information to the data reported by the performance indicator. Additionally, the inspectors observed surveillance activities that determined the RCS identified leakage rate, and chemistry personnel taking and analyzing a RCS sample.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, "Problem Identification and Resolution," the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that Dominion entered issues into the CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP.

b. Findings

No findings were identified.

4OA5 Other Activities

(Closed) NRC Temporary Instruction 2515/177 - Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal and Containment Spray Systems

a. Inspection Scope

The inspectors performed the inspection at Units 2 and 3 in accordance with Temporary Instruction (TI) 2515/177, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal and Containment Spray Systems." The NRC developed TI 2515/177 to support the NRC's confirmatory review of Dominion's responses to NRC Generic Letter (GL) 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal and Containment Spray Systems." Based on a review of Dominion's GL 2008-01 response letters, the NRC Office of Nuclear Reactor Regulation (NRR) staff provided additional plant specific guidance on inspection scope to the regional inspectors. The inspectors used this inspection guidance along with the TI to verify that Dominion implemented or was in the process of acceptably implementing the commitments, modifications, and programmatically controlled actions described in their GL 2008-01 response. The inspectors verified that the plant-specific information (including licensing basis documents and design information) was consistent with the information that Dominion submitted to the NRC in response to GL 2008-01.

The inspectors reviewed a sample of isometric drawings, and piping and instrumentation diagrams, and conducted selected system piping walkdowns to verify that Dominion's drawings reflected the subject system configurations and UFSAR descriptions. Specifically, the inspectors verified the following related to a sample of isometric drawings for the safety injection (SI), containment spray, and shutdown cooling systems for Unit 2 and the SI, residual heat removal system, quench spray system, and containment recirculation spray system for Unit 3.

  • High point vents were identified
  • High points that did not have vents were recognized and evaluated with respect to their potential for gas buildup
  • Other areas where gas could accumulate and potentially impact subject system operability, such as orifices in horizontal pipes, isolated branch lines, heat exchangers, improperly sloped piping, and under closed valves, were acceptably evaluated in engineering reviews or had ultrasonic test (UT) points which would reasonably detect void formation
  • For piping segments reviewed, branch lines and fittings were clearly shown The inspectors performed walkdowns of portions of the above systems to evaluate the acceptability of Dominion's drawings utilized during their review of GL 2008-01. The inspectors verified that Dominion performed walkdowns of the applicable systems to confirm that the combination of system orientation, vents, instructions and procedures, testing, and training, would ensure that each system was sufficiently full of water to ensure operability. The inspectors reviewed Dominion's methodology used to determine system piping high points, identification of negative sloped piping, and calculations of void sizes based on UT equipment readings, to ensure the methods were reasonable.

The inspectors also reviewed engineering analyses associated with the development of acceptance criteria for as-found voids. The review included engineering assumptions for void transport and acceptability of void fractions at the suction and discharge piping of the applicable system pumps. In addition, the inspectors verified that Dominion included all emergency core cooling systems, along with supporting systems, within the scope of the GL. The inspectors also observed several field UT measurements of the applicable piping in Unit 3 to assess the adequacy of the monitoring techniques used to ensure system operability. The inspectors reviewed a sample of Dominion's procedures used for filling and venting the systems associated with GL 2008-01 to verify that the procedures were effective in venting or reducing voiding to acceptable levels. The inspectors verified that Dominion's venting surveillance frequencies were consistent with TS and associated bases, and the UFSAR. The inspectors reviewed a sample of system venting surveillance results to ensure proper implementation of the surveillance program. The inspectors reviewed CAP documents to verify that selected actions described in Dominion's nine-month and supplemental submittals were acceptably documented including completed actions, and implementation schedule for incomplete actions. The inspectors also verified that the commitments in Dominion's submittals were included in the CAP. The inspectors specifically verified the installation of hardware vents, located in the containment spray and emergency core cooling suction header and the safety injection discharge piping, as committed to in Dominion's GL response. Additionally, the inspectors reviewed evaluations and corrective actions for various issues Dominion identified during their GL 2008-01 review. The inspectors performed this review to ensure Dominion appropriately evaluated and adequately addressed any gas voiding concerns, including the evaluation of operability for gas voids discovered in the field.

Finally, the inspectors reviewed Dominion's training associated with gas accumulation to assess if appropriate training had been provided to the operations and engineering support staff to ensure appropriate awareness of the effects of gas voiding. This completes the inspection requirements for TI 2515/177 at Units 2 and 3.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On April 19, 2012, the inspectors presented the inspection results to Stephen E. Scace, Site Vice President, and other members of the Millstone staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

M. Adams Plant Manager

L. Armstrong Manager, Training R. Arquaro Unit 3 Shift Manager G. Auria Nuclear Chemistry Supervisor
B. Bartron Supervisor, Licensing

R. Beale Unit 2 Shift Manager

R. Bonner Nuclear Engineering Supervisor R. Burnham Consulting Engineer C. Chapin Assistant Operations Manager

W. Chestnut Supervisor, Nuclear Shift Operations Unit 2
F. Cietek Nuclear Engineer, PRA
T. Cleary Licensing Engineer G. Closius Licensing Engineer L. Crone Supervisor, Nuclear Chemistry
J. Curling Manager, Protection Services
G. D'Auria Nuclear Supervisor, Chemistry

P. Dillon Nuclear Engineer III

J. Dorosky Health Physicist III B. Ferguson Unit 2 Shift Manager M. Finnegan Supervisor, Health Physics, ISFSI

A. Gharakhanian Nuclear Engineer III

W. Gorman Supervisor, Instrumentation & Control
D. Grindle Senior Nuclear Instrumentation Technician J. Grogan Assistant Operations Manager K. Grover Manager, Nuclear Operations

C. Houska I&C Technician

C. Janus Nuclear Engineer III

P. Kolz Nuclear Chemistry Technician

J. Kunze Supervisor, Nuclear Operations Support
J. Laine Manager, Radiation Protection/Chemistry
M. Legg Manager, Nuclear Oversight

M. O'Neill Unit 3 Plant Equipment Operator

R. MacManus Director, Nuclear Station Safety & Licensing
G. Marshall Manager, Outage and Planning R. McDonald Nuclear Engineer III H. McKenney Supervisor Nuclear Operations Support

D. Reed Unit 3 Shift Manager

R. Riley Supervisor, Nuclear Shift Operations Unit 3

M. Roche Senior Nuclear Chemistry Technician

D. Russo Nuclear Engineer Level III L. Salyards Licensing, Nuclear Technology Specialist J. Semancik Engineering Director

S. Scace Site Vice President

C. Sloan Nuclear Plant Equipment Operator

Attachment

A. Smith Asset Management D. Smith Manager, Emergency Preparedness
S. Smith Manager, Engineering
S. Turowski Supervisor, Health Physics Technical Services
C. Vournazos IT Specialist, Meteorological Data
B. Wilkens Site Fire Marshall, Senior Safety Specialist

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Closed

005000336,423/2515/177 TI Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal and Containment Spray Systems (4OA5)

LIST OF DOCUMENTS REVIEWED

Section 1R04: Equipment Alignment

Procedures

OP 2315A-001, "Control Room Air Conditioning System," Revision 006-05
OP 2346A-011, "'A'DG Service Water Valve Alignment," Revision 000-04
OP 2346A-012, "'A' DG Starting Air Valve Alignment," Revision 000-00
OP 2346A-013, "'A' DG Jacket Water Valve Alignment," Revision 000-02
OP 2346A-014, "'A' DG Lube Oil Valve Alignment," Revision 000-02
OP 2346B-002, "'A' DG Fuel Oil Valve Alignment," Revision 000-00

Section 1R05: Fire Protection

Procedures

U2-24-FRR-FHA, Millstone Unit 2 Fire Hazards Analysis (FHA), Revision 12 Millstone Unit 2 Firefighting Strategies, April 2002

Section 1R11: Licensed Operator Requalification Program

Condition Reports

CR458763

Miscellaneous

ES 12-1A, "MP2 LORT Cycle Operating Exam"
LORT SE46, Revision 2, Change 1
Attachment

Section 1R12: Maintenance Effectiveness

Procedures

ER-AA-MRL-100, "Implementing Maintenance Rule," Revision 5
ER-AA-BKR-1001, "Circuit Breaker Program," Revision 0
ER-AA-SYS-1003, "System Performance Monitoring," Revision 3
NF-AA-PRA-101-3060, "Probabilistic Risk Assessment Procedures and Methods: Maintenance Rule Performance Criteria," Revision 0

Condition Reports

CR458424
CR458756
CR459688
CR380201
CR451919
CR454196
CR457931
CA223098

Miscellaneous

Condensate, CPF, and Main Feedwater system Health Report 1st Quarter 2011 and 2012 Main Feedwater Unavailability, November 2009 to November 2011
System 3322 Auxiliary Feedwater & DWST Health Report January 1, 2011 to March 31, 2011
System 3322 Auxiliary Feedwater & DWST Health Report April 1, 2011 to June 30, 2011 System 3322 Auxiliary Feedwater & DWST Health Report July 1, 2011 to September 30, 2011 System 3322 Auxiliary Feedwater & DWST Health Report October 1, 2011 to December 31, 2011
Unit 3 480 VAC MCC System Health Report 1st Quarter 2012 MRE011803
MRE012148 MRE012166 MRE013602
MRE013623
MRE013849
MRE013911
MRE014177 MRE011826 MRE011938
MRE011948
MRE012026
MRE012041 MRE012052 MRE012292
MRE012515
MRE013428 MRE013726 MRE014038 MRE014334 MRE014341
MRE014382
MRE014393
MRE014413
MRE014456 MRE014469 MRE014476
MRE014491
MRE014517
MRE014518 MRE014521 MRE014522
MRE014537
MRE014539 MRE014540 MRE011808 MRE011941 MRE011983
MRE012074
MRE013162
MRE013819
MRE014048 MRE014058 MRE014060
MRE014361
MRE014365
MRE014384 MRE014385 MRE014414
MRE014460
MRE014485

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

NF-AA-PRA-370, "Probabilistic Risk Assessment Procedures and Methods: PRA Guidance for MRule (a)(4)," Revision 12
Attachment Miscellaneous High Risk Contingency Plan for Cutting Synchrophasor Metering Unit into the 310 Line
EOOS Operator Risk Report dated January 18, 2012 High Risk Contingency Plan dated February 7, 2012 Troubleshooting plan for CR463624

Section 1R15: Operability Evaluations

Procedures

U2 EN7, "Unit 2 High Energy Line Break (HELB) Barrier Inspection," Revision 002-02

Condition Reports

CR427558
CR445936
CR460214
CR460803
CR460805
CR460806
CR460807
CR460830
CR460065
CR464272
CR464818
CR465069
CR465095 Miscellaneous 98ENG02718C2, "MP2 Auxiliary and Turbine Buildings, HELB Barrier Steam Infiltration Analysis," Revision 0 OD000463, Unit 3 'A' EDG Load Exceeds Continuous Load Rate
OD000468, Unit 3 'A' EDG Load Swings Calc
RPS-ESF-0428613, "SG Level Uncertainty" Calc 3444A01-0112E3, "SG Level Instrument Scaling" Rosemount 10CFR21 Notification dated February 23, 2012 Rosemount 10CFR21 Notification dated March 2, 2012
Wyle Laboratories Test Report 47506-02

Section 1R18: Plant Modifications

Procedures

CM-AA-RSK-1001, "Engineering Risk Assessment"

Condition Reports

CR464272
CR464430
CR465069
CR465095
Maintenance Orders/Work Orders 53M20602364

Miscellaneous

Temp Mod 3-12-005, "Increase Bistable Setpoint of 3FWS*LB547B, 'D' Steam Generator Low-low Water Level Reactor Trip and Aux Feedwater Initiation," Revision 000 Calc
RPS-ESF-0428613, "SG Level Uncertainty"
Calc 3444A01-0112E3, "SG Level Instrument Scaling" Rosemount 10CFR21 Notification dated March 2, 2012
DM2-00-0253-09, "Replacement of Rosemount Transmitter RTD with Moore Industries Flexible RTD" Attachment

Section 1R19: Post-Maintenance Testing

Procedures

SP 2613I-001, "'A' EDG Loss of Load Test," Revision 003
OP 2346A-004, "'A' EDG Data Sheet," Revision 023-09
SP 2624A-001, "'A' EDG Starting Air Vent Valves IST," Revision 000-03
SP 3646A.1-001, "EDG 'A' Operability Tests," Revision 018-02
OP 3346A-014, "EDG 'A' - Operating Log," Revision 012
SP 3622.3, "Auxiliary Feedwater Pump 3FWA*P2 Operational Readiness Test," Revision 017-09 SP3622.3-001, "TDAFW Pump Operational Readiness Test and Quarterly IST Group B Pump Tests," Revisions 014-04 and 014-05

Condition Reports

CR463767
CR467660
CR467654
CR467657
CR467858
CR468001
CR468122
CR468131
CR468133
CR468137
Maintenance Orders/Work Orders
WO 53102493358
WO 53102463914
WO 53102480231
WO 53102457360
WO 53102500853
WO 53102495719
WO 53102421224
WO 53102449638
WO 53102501255
WO53102510734
WO 53102278486
WO 53102434017
WO 53102447008
WO 53102500994
WO 53102465248
WO 53102504479
WO 53102504493
WO 53102511132
WO 53102511051

Miscellaneous

DCN
MP3-11-01128, "Operations acceptance Checklist for 3CNM-P1C motor connections"

Section 1R22: Surveillance Testing

Procedures

SP 2602A-001, "Manual RCS Leak Rate Determination," Revision 006-02
SP 2610BO-001, "2-MS-201, 2-MS-202 and 2-MS-464 (SV-4188) Stroke and Timing IST," Revision 001-03
SP 2610BO-004, "AFP Turbine Trip Throttle Valve Exercise Test," Revision 000-00
CP 2802N, "Primary Systems Sampling and Analysis," Revision 001-03
SP 3855, "Reactor Coolant analysis for Dose Equivalent I-131," Revision 007-02
C
OP 200.15, "RCS Leakage Trending and Investigation," Revision 1
NF-AA-NSA-101-5009, "Reactor Coolant System Leak Rate Monitoring," Revision 1
SP 3601F.6, "Reactor Coolant System, Water Inventory Measurement," Revision 006-06
SP 3601F.6-001, "RCS Inventory Balance," Revision 003-02

Condition Reports

CR457939

Miscellaneous

Reactor Coolant Leakage Report for 2011 dated February 23, 2012
Attachment
Section 2RS01, 2RS02, 2RS04: Radiological Hazard Assessment and Exposure Controls, Occupational ALARA Planning and Controls, Occupational Dose Assessment

Condition Reports

463685;
4558425,
450892,
461061,
461473,
459978

Procedures

RP-AA-105, Revision 0, External Radiation Exposure Control Program
RPM-1.3.13, Revision 010-01, Bioassay Sampling and Analysis
RP-AA-123, Revision 2, Effective Dose Equivalent
PM-2.5.8, Revision 004-01, Stay Time Tracking and Multi-Badging for Special Work
RP-AA-150, Revision 2, TLD Performance Testing
NVLAP Certificate of Accreditation to ISO/IEC 17025:2005 for Mirion Technologies (GDS), Inc. Dominion Site Audit of Global Solutions, Inc. (MIRION), 2009 NVLAP On-Site Assessment Report for Mirion Technologies (GDS), Inc. February 2012
Calibration for Accuscan Whole Body Counter, December 2011
GEL Laboratories Scope of Accreditation to ISO/IEC 17025:2005

Section 4OA1: Performance Indicator Verification

Miscellaneous

NEI 99-02, "Regulatory Assessment Performance Guidelines," Revision 6
Unit 2 Dose Equivalent I-131 Activity for 2011
Unit 2 Identified Leakage for 2011 Unit 3 Reactor Coolant Leakage Report for 2011 dated February 23, 2012 Unit 3 RCS Specific Activity Database for 2011 dated February 29, 2012
NRC PI BI01, "RCS Specific Activity, Millstone Unit 3, January through December 2011"
NRC PI BI02, "RCS Leak Rate Millstone Unit 3 for January through December 2011"
C
OP 200.15, "RCS Leakage Trending and Investigation," Revision 1
NF-AA-NSA-101-5009, "Reactor Coolant System Leak Rate Monitoring," Revision 1
NF-AA-FPA-3301, "Reactor Coolant Radiochemistry Analysis," Revision 2
NF-AA-FPA-3002, "Monthly Fuel Reliability Indicator," Revision 1
SP 3601F.6, "Reactor Coolant System, Water Inventory Measurement," Revision 006-06
SP 3601F.6-001, "RCS Inventory Balance," Revision 003-02

Section 4OA2: Problem Identification and Resolution

Procedures

SP 2602A, "Reactor Coolant Leakage," Revision 006-03
SP 2602A-001, "Manual RCS Leak Rate Determination," Revision 006-002

Section 4OA5: Other Activities

Calculations

and Evaluations 98-ENG-02558M2, Determination of Minimum Submergence Criteria for RWST Suction Piping, Revision 0 M2-EV-08-0027, Technical Evaluation for Generic Letter 2008-01 Response, Millstone Unit 2, Revision 0 M2-EV-09-0015, Basis of

GL 2008-01 ECCS, DHR & CS Gas Accumulation Surveillance Program, Millstone Unit 2, Revision 0
Attachment M3-EV-04-0021, Technical Evaluation for Generic Letter 2008-01 Response, Millstone Unit 3, Revision 2 M3-EV-05-0008, Determination of Allowable ECCS Gas Accumulations in Support of Surveillance 4.5.2.b.1, Millstone Unit 3, Revision 5 M3-EV-08-0026, Technical Evaluation for Generic Letter 2008-01 Response, Millstone Unit 3, Revision 2 M3-EV-08-0035,"Evaluation of Gas Void Discovered in the 24" RWST ECCS Supply Line,"
Revision 0 S-04425S3, MP3 RELAP5 Analysis of Gas Void in the ECCS Suction Piping from RWST,
Revision 0
Completed Tests/Procedures/Examinations
SP 2604Z, ECCS, SDC and CS System Gas Accumulation Verification, Quarterly UT Results from April 2010 - January 2012
SP 3606.5, Containment Recirculation Spray System Train 'A' Valve Lineup and Loop Seal Verification, Monthly UT Results from December 2009 - December 2011
SP 3606.6, Containment Recirculation Spray System Train 'B' Valve Lineup and Loop Seal Verification, Monthly UT Results from December 2009 - December 2011
SP 3608.4, High Pressure Safety Injection System Vent and Valve Lineup Verification, Monthly UT Results from December 2009 - December 2011
SP 3610A.3, RHR System Vent and Valve Lineup Verification, Monthly UT Results from December 2009 - December 2011

Procedures

ER-AA-NDE-UT-724, Ultrasonic Examination Procedure for Liquid Level Measurements, Revision 1
OP 2308X11, 'A' HPSI Pump Maintenance, Revision 7
OP 2308X51, 'B' HPSI Pump Maintenance, Revision 4
OP 2309X11, 'A' CS Pump Maintenance, Revision 0
OP 2353A, Filling and Venting Various Emergency Core Cooling System Piping and Components, Revision 7
OP 2353C, Filling and Venting SIT Recirculation Header, Revision 1
OP 3250.04A, Charging Pump Fill and Vent, Revision 0
OP 3250.08, Safety Injection System Fill and Vent, Revision 0
OP 3250.09, QSS Pump Discharge Header Fill, Revision 0
OP 3250.10A, Removing RHR from Service for LLRT or Maintenance, Revision 3
OP 3304A, Charging and Letdown, Revision 31
OP 3304C, Primary Makeup and Chemical Addition, Revision 23
OP 3309, Quench Spray, Revision 13
OP 3310A, Residual Heat Removal System, Revision 17
OP 3310B, Accumulator Low Pressure Safety Injection, Revision 15
SP 2604Z, ECCS, SDC, and CS System Gas Accumulation Verification, Revision 1
SP 3604A.5, Chemical and Volume Control System Valve Operability Test, Revision 13
SP 3606.6, Containment Recirculation Spray System Train 'B' Valve Lineup and Loop Seal Verification, Revision 4
SP 3608.6, Safety Injection System Valve Operability Test, Revision 14
SP 3610A.3, RHR System Vent and Valve Lineup Verification, Revision 7

Drawings

25203-20146, Isometric - Refueling Water Supply, Unit 2, Sheet 422, Revision 4
203-20150, Isometric - Containment Spray System, Unit 2, Sheet 13, Revision 10
Attachment 25203-20150, Isometric - Containment Spray System, Unit 2, Sheet 81, Revision 8 25203-20150, Isometric - H.P. and L.P. Injection and Containment Spray Pump Suction, Unit 2, Sheet 2, Revision 28 25203-20150, Isometric - High Pressure and Low Pressure Injection and Containment Spray Pump Suction, Unit 2, Sheet 1, Revision 23 25203-20150, Isometric - Shutdown Cooling from Exchanger to Spray Header, Unit 2, Sheet 71, Revision 18 25203-20150, Isometric - Shutdown Cooling from Exchanger to Spray Header, Unit 2, Sheet 13, Revision 10 25203-20150, Low Pressure Safety Injection Pump Discharge, Sheet 8, Revision 28 25203-26015, P&ID - High Pressure Safety Injection Pumps, Unit 2, Sheet 2, Revision 41
203-26015, P&ID - LP Safety Injection System, Unit 2, Sheet 1, Revision 38
203-26015, P&ID - LP Safety Injection System, Unit 2, Sheet 2, Revision 41
203-26015, P&ID - Safety Injection Tanks, Unit 2, Sheet 3, Revision 30 25212-20402, Isometric - Quench Spray System, Unit 3, Sheet 21, Revision 6 25212-20403, Fabrication Installation Control Drawing ASME Section III, Code Class 2, Sheet 17, Revision 9 25212-26904, P&ID - Chemical and Volume Control, Unit 3, Sheet 1, Revision 54
212-26904, P&ID - Chemical and Volume Control, Unit 3, Sheet 3, Revision 54 25212-26912, P&ID - Low Pressure Safety Injection, Unit 3, Sheet 1, Revision 50 25212-26912, P&ID - Low Pressure Safety Injection/Containment Recirculation, Unit 3, Sheet 3, Revision 38 25212-26913, P&ID - High Pressure Safety, Unit 3, Sheet 1, Revision 39
212-26913, P&ID - High Pressure Safety, Unit 3, Sheet 2, Revision 39
212-26915, P&ID - Quench Spray & H2 Recombiner - Unit 3, Revision 37
Design Changes
DM2-00-0007-09, Installation of Vent Valves on High/Low Pressure SI Discharge Header Piping to RCS Loops 2A/2B, Revision 0
DM2-00-0380-08, Addition of Vent Valves to Containment Spray and LPSI/HPSI Suction Piping, Revision 0

Miscellaneous

C11504C, Outage OE Training, dated August 22, 2011
Millstone Unit 2 Potential Areas for Gas Intrusion in Unit 2, Attachment B, Revision 0
System Health Report, Chemical and Volume Control, Unit 3, 3rd Quarter 2011 System Health Report, Containment Recirculation Spray, Unit 3, 3rd Quarter 2011 System Health Report, Containment Spray and RWST, Unit 2, 3rd Quarter 2011 System Health Report, LPSI and Shutdown Cooling, Unit 2, 3rd Quarter 2011 System Health Report, Quench Spray and RWST, Unit 3, 3rd Quarter 2011 System Health Report, Residual Heat Removal, Unit 3, 3rd Quarter 2011 System Health Report, High Head Safety Injection, Unit 3, 3rd Quarter, 2011
TM-1876A, Transport of a Small Air Pocket, Creare Incorporated dated February 1998
Design & Licensing Bases Letter from J. A. Price (Dominion Nuclear Connecticut, Inc.) to USNRC, "Nine-Month Response to NRC Generic Letter 2008-01" dated October 14, 2008 Letter from W. R. Matthews (Dominion Nuclear Connecticut, Inc.) to USNRC, "Supplemental Response to the NRC Generic Letter 2008-01" dated January 15, 2009 Letter from L.N. Hartz (Dominion Nuclear Connecticut, Inc.) to USNRC, "Response to Request for Additional Information Regarding Generic Letter 2008-01" dated January 14, 2010
Attachment Millstone Nuclear Power Station - Technical Specifications, Unit 2, Amendment 309 Millstone Nuclear Power Station - Technical Specifications, Unit 3, Amendment 252
Millstone Nuclear Power Station Updated Final Safety Analysis Report, Unit 2, Revision 28 Millstone Nuclear Power Station Updated Final Safety Analysis Report, Unit 3, Revision 23
Corrective Action Documents
113720
168879
356722
460344
113726
319295
359613
461221
114275
319371
369371
461308
118407
322563
377876
461437
166748
327719
347276
454766
455434
461455
Attachment

LIST OF ACRONYMS

ADAMS Agencywide Documents Access and Management System

ALARA as low as reasonably achievable

CAP Corrective Action Program
CFR Code of Federal Regulations
CR condition reports
CR [[]]

AC control room air conditioning system

DRP Division of Reactor Projects

DRS Division of Reactor Safety
EDG emergency diesel generator
EP emergency preparedness GL generic letter
HP [[]]

SI high pressure safety injection

IMC Inspection Manual Chapter
IN [[]]
PO Institute of Nuclear Power Operations
MDA minimum detectable activity

NCV non-cited violation NEI Nuclear Energy Institute

NRC Nuclear Regulatory Commission
NVL [[]]
AP National Voluntary Laboratory Accreditation Program
ODM operational decision making
OOS out of service
PA [[]]

RS Publicly Available Records

RCP reactor coolant pump

RCS reactor coolant system

RWP radiation work permit
SBO station blackout

SDP significance determination process SG steam generator

SI safety injection

SSC structures, systems, and components
SW service water
TI temporary instruction TS technical specifications
UFSAR Updated Final Safety Analysis Report

UT ultrasonic test

URI unresolved item