IR 05000244/2006004

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IR 05000244-06-004 on 07/01/2006 Through 09/30/2006; R.E. Ginna Nuclear Power Plant
ML063040159
Person / Time
Site: Ginna Constellation icon.png
Issue date: 10/31/2006
From: Arthur Burritt
Reactor Projects Branch 1
To: Korsnick M
Ginna
References
IR-06-004
Download: ML063040159 (41)


Text

October 31, 2006

SUBJECT:

R. E. GINNA NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000244/2006004

Dear Mrs. Korsnick:

On September 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your R. E. Ginna facility. The enclosed integrated inspection report documents the inspection results, which were discussed on October 5, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents one finding of very low safety significance (Green) and two NRC-identified findings which were determined to involve a violation of NRC requirements.

Additionally, a licensee-identified violation, which was determined to be of very low safety significance is listed in this report. However, because of the very low safety significance and because they were entered into your corrective action program, the NRC is treating the three violations as non-cited violations (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at R.E. Ginna Nuclear Power Plant.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Arthur L. Burritt, Acting Chief Projects Branch 1 Division of Reactor Projects Docket No. 50-244 License No. DPR-18 Enclosure:

Inspection Report 05000244/2006004 w/ Attachment: Supplemental Information cc w/encl:

M. J. Wallace, President, Constellation Generation J. M. Heffley, Senior Vice President and Chief Nuclear Officer P. Eddy, Electric Division, NYS Department of Public Service C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law C. W. Fleming, Esquire, Senior Counsel, Constellation Energy Group, Inc.

P. R. Smith, New York State Energy Research and Development Authority J. Spath, SLO Designee New York State Energy Research and Development Authority T. Wideman, Director, Wayne County Emergency Management Office M. Meisenzahl, Administrator, Monroe County, Office of Emergency Preparedness T. Judson, Central New York Citizens Awareness Network

SUMMARY OF FINDINGS

IR 05000244/2006-004; 07/01/2006 - 09/30/2006; R. E. Ginna Nuclear Power Plant; Operability

Evaluations, Other Activities.

The report covered a 3-month period of inspection by resident inspectors and announced inspections by regional specialists. Two non-cited violations (NCVs), one Green finding and one unresolved item were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified that Ginna personnel did not adequately assess the effects of a service water leak that occurred in the room cooler for the C Standby Auxiliary Feedwater (SAFW) pump. As a result, water that had accumulated in electrical control panels for the pump was not detected. When the water was found by Ginna personnel during the performance of a routine surveillance test of the C SAFW pump, the pump was declared inoperable until the water was removed, which resulted in approximately 19 additional hours of out-of-service time.

This finding is more than minor because it is associated with the Mitigating Systems Cornerstone and affects the cornerstone objective of ensuring the reliability of systems that respond to initiating events to prevent undesirable consequences. This finding was determined to be of very low safety significance (Green) by using Phase 1 of the Inspection Manual Chapter (IMC) 0609, Significance Determination Process. The finding screened to Green since it was not a design or qualification deficiency and did not result in a loss of safety function. This finding is related to the cross-cutting aspects of problem identification and resolution in that Ginna did not fully evaluate the operability of the C SAFW pump following the leak, which sprayed water on electrical components. (Section 1R15)

Severity Level IV. The inspectors identified that on two occasions Ginna personnel failed to notify the NRC that offsite power to the plant was inoperable. Specifically, on July 17 and August 1, 2006, Ginna did not report to the NRC that offsite power to the plant was inoperable. The finding was determined to be a non-cited violation of 10 CFR 50.72,

Immediate Notification Requirements for Operating Nuclear Power Reactors.

This deficiency was evaluated using the traditional enforcement process since the failure to make a required report could adversely impact the NRCs ability to carry out its regulatory mission. Because this finding was of very low safety significance and has been entered into the corrective action program it is being treated as an NCV.

(Section 1R13).

Severity Level IV. The inspectors identified that Ginna did not notify the NRC within 30 days of the identification of a medical condition that caused a reactor operator to fail to iv meet the requirements of 10 CFR 55.21. Specifically, Ginna became aware of a medical condition in June 2006 that caused a licensed reactor operator to fail to meet the requirements of 10 CFR 55.21 and for which a conditional (restricted) license would be required. However, Ginna did not provide a Form 396 (medical condition certification) to the NRC until August 2006. The finding was determined to be a non-cited violation of 10 CFR 50.74, Notification of Change in Operator or Senior Operator Status.

This deficiency was evaluated using the traditional enforcement process since the failure to make a required report could adversely impact the NRCs ability to carry out its regulatory mission. Because this finding was of very low safety significance and has been entered into the corrective action program it is being treated as an NCV.

(Section 4OA3).

Licensee-Identified Violations

A violation of very low safety significance, which was identified by Ginna, has been reviewed by the inspectors. Corrective actions taken or planned by Ginna have been entered into Ginnas corrective action program. This violation and corrective action(s)are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Ginna began the period at full Rated Thermal Power and operated at essentially full power for the entire report period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 2 samples weather-related, 1 sample cold

weather preparations with 2 specific systems)

a. Inspection Scope

During the weeks of July 17, and July 31, 2006, the Rochester area experienced unusually warm weather with temperatures in the mid 90s. In response to the warm weather, the inspectors performed walkdowns of plant areas that contain equipment which is vulnerable to high temperature conditions. Areas examined included the battery and diesel generator rooms, as well as the standby auxiliary feedwater pump room. As part of the walkdowns, local area temperatures were checked as well as the operability of ventilation and air conditioning cooling systems to ensure that the equipment located in the rooms was not affected by the high external air temperature conditions.

Using Ginna procedure M1306.1, Ginna Station Maintenance Department Winterizing Inspection Program and the Ginna Updated Final Safety Analysis Report (UFSAR) as references, the inspectors reviewed Ginnas preparations for cold weather by walking down plant areas and observing the installation of cold weather protective equipment.

Two risk-significant systems were selected for review as part of this inspection: the service water and auxiliary feedwater systems.

b. Findings

No findings of significance were identified.

==1R02 Evaluation of Changes, Tests, or Experiments (IP

==

71111.02 - 20 samples)

a. Inspection Scope

The inspectors reviewed four safety evaluations (SEs), three of which were either issued during the past two years or associated with plant modifications that were completed during the past two years, and one that had been issued and installed in the previous four years. The SEs reviewed were in the Initiating Event, Mitigating Systems, and Barrier Integrity cornerstones. The selected SEs were reviewed to verify that changes to the facility or procedures as described in the UFSAR were reviewed and documented in accordance with 10 CFR 50.59, and that the safety issues pertinent to the changes were properly resolved or adequately addressed. The reviews also included the verification that Ginna had appropriately concluded that the changes and tests could be accomplished without obtaining license amendments. The SEs reviewed are listed in

1. The inspectors also reviewed sixteen screened-out evaluations for changes, tests, and

experiments for which Ginna determined that SEs were not required. This review was performed to verify that Ginnas threshold for performing SEs was consistent with 10 CFR 50.59. The listing of the screened-out evaluations reviewed is provided in

1. In addition, the inspectors reviewed the administrative procedures that were used to

control the screening, preparation, and issuance of the SEs to ensure that the procedure adequately covered the requirements of 10 CFR 50.59.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdown (3 samples)

a. Inspection Scope

The inspectors used plant technical specifications, Ginna operating procedures, plant piping and instrument drawings (P&ID), and the UFSAR as guidance for conducting partial system walkdowns. The inspection reviewed the alignment of system valves and electrical breakers to ensure proper in-service or standby configurations as described in plant procedures and drawings. During the walkdown, the inspectors evaluated material conditions and general housekeeping of the system and adjacent areas. The inspectors also verified that operations personnel were following plant technical specifications (TS).

The following plant system alignments were reviewed:

  • On July 10, 2006, the inspectors completed a walkdown of the A Containment Spray train while the B Containment Spray was out of service for Motor Operated Valve Analysis and Test System (MOVATS) testing and maintenance on the B train discharge valve to containment. This system was examined because it is a redundant means of providing containment depressurization and atmospheric scrubbing in the event of a design basis accident.
  • On August 22, 2006, the inspectors completed a walkdown of the D Standbv Auxiliary Feedwater train while the C Standby Auxiliary Feedwater train was out of service for power-uprate related maintenance activities.

b. Findings

No findings of significance were identified.

.2 Complete Walkdown (1 sample)

a. Inspection Scope

The inspectors conducted a detailed walkdown of the alignment and condition of the containment penetration cooling system. This system was chosen because if it failed to properly operate, containment penetrations that are cooled by the system may begin to degrade, which could result in containment failure during certain postulated reactor plant events. In addition to verifying proper system alignment as required by section 9.4.1.2.10 of the Ginna Updated Final Safety Analysis Report (UFSAR) and Ginna procedures and drawings, the inspector reviewed system maintenance and condition reports.

b. Findings

Introduction:

The inspectors identified that Ginna did not have procedures which controlled the operation of the supply dampers for the containment penetration cooling system. Further, cooling air was not being supplied to several penetrations, and the operability of penetration instrumentation was not checked. Finally the system P&ID did not match what was installed in the field. This issue is unresolved pending further inspection and evaluation by Ginna.

Description:

Large containment penetrations at Ginna that contain hot fluid or steam are cooled by a containment penetration cooling system that supplies cool air to 17 penetrations. The system is located in the auxiliary building and consists of two cooling fans, a heat exchanger that is cooled by service water, piping which directs the air to the penetrations, and temperature probes and alarms that monitor the temperature of air leaving the individual penetrations. The system operates continuously using outside air from the auxiliary building roof. Although the system is not safety-related, it does have an important-to-safety function in that it is designed to keep the bulk concrete temperature surrounding the penetrations from exceeding 150 degrees. The temperature of the penetrations is monitored by alarm switches and temperature detectors located in the discharge plenums of each penetration. If the temperature of the exhaust air leaving the penetrations exceeds 120 degrees, an alarm will sound in the control room alerting operators of an impending high temperature condition.

While performing a walkdown of this system and a review of the system preventive maintenance program, the inspector noted the following:

  • Although a calibration procedure exists to calibrate the penetration temperature detectors, there was no record of Ginna calibrating the temperature elements for the containment penetration cooling system. Absent a calibration check, it was not evident to the inspector that the temperature detectors would alert operators that a penetration had become overheated.
  • The piping and instrument diagram (P&ID) for the penetration cooling system did not accurately reflect the configuration in the plant. Specifically, contrary to what was depicted on the system P&ID, exhaust air from the penetration cooling system for the B main steam piping discharged into the auxiliary building vice the outside air, and certain penetrations had multiple vice single exhaust monitoring systems.

When informed of these observations, Ginna personnel performed a walkdown of the system and initiated several condition reports and a Technical Services Request (TSR)that documented the inspectors observations. The condition reports documented the need to examine the surveillance program for the penetration cooling alarm switches, and assess the adequacy of the current system lineup. The TSR was initiated to evaluate the need to relocate the penetration exhaust piping for the B main steam line so the configuration would match the plant P&ID. Finally, the reports documented the need to determine if the concrete that was located adjacent to the penetrations was damaged because of inadequate cooling.

Analysis:

The configuration of the Containment Penetration Cooling system has not been maintained, controlled or operated as outlined in the plant UFSAR and the system P&ID. This issue is Unresolved pending further inspection and evaluation by Ginna.

(URI 05000244/20060004-01, Review the significance of not maintaining the Containment Penetration Cooling system in accordance with the UFSAR and system P&IDs)

1R05 Fire Protection

.1 Quarterly Inspection ( 8 samples)

a. Inspection Scope

Using the Ginna Fire Protection Program documents as a guide, the inspectors performed walkdowns of the following fire areas to determine if there was adequate control of transient combustibles and ignition sources. The material condition of fire protection systems, equipment and features, and the material condition of fire barriers were also inspected against industry standards. In addition, the passive fire protection features were inspected, including the ventilation system fire dampers, structural steel fire proofing, and electrical penetration seals. The following plant areas were inspected:

  • Screenhouse, Fire Zone SH-2
  • Service Building Basement, Fire Zone SB-1
  • A Battery Room, Fire Area BR1A
  • B Battery Room, Fire Area BR1B
  • A Diesel Generator Room, Fire Zone EDG1A
  • B Diesel Generator Room, Fire Area EDG 1B
  • Relay Room, Fire Zone RR

b. Findings

No findings of significance were identified.

.2 Fire Brigade Drill - Annual Sample

a. Inspection Scope

The inspectors observed an announced test of the Ginna station fire brigade conducted at 9:00 p.m. on July 18, 2006. The test involved a simulated fire in the B motor generator that is located in the lower level of the clean side of the intermediate building. The inspectors verified the fire brigade personnel, which consisted of three auxiliary operators and two contract personnel, responded quickly to the fire, and used appropriate personal protective equipment. While combating the fire, the inspector verified the brigade used proper firefighting techniques and performed satisfactorily as a team. Following the drill, the inspectors verified that the post-drill critique was thorough.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

a. Inspection Scope

To verify any potential heat exchanger (HX) deficiencies which could mask degraded performance are identified, the inspector examined a sample of HXs. Based on a plant-specific risk assessment, past inspection results, and recent operational experience, the inspector selected a sample of four safety-related heat HXs: the A Closed Cooling Water (CCW) HX, the A Emergency Diesel Generator (EDG) jacket water and lube oil HXs, and the B Standby Auxiliary Feedwater (SAFW) Pump room cooler. The Service Water (SW) system, which provides cooling to the CCW HXs, was also reviewed.

The inspector reviewed performance tests, periodic cleaning, eddy current inspections, chemical control methods, tube leak monitoring, tube plugging condition, potential water hammer analysis, operating procedures, maintenance practices, and verified that controls for the selected components conformed to Ginnas commitments to Generic Letter 89-13, Service Water System Problems Affecting Safety-Related Equipment.

The inspectors compared the inspection results to the established acceptance criteria to verify that the results were acceptable and that the HXs operated in accordance with design. The inspector walked down the systems, structures, and components. The inspectors reviewed system health reports and interviewed applicable system engineers.

The inspector verified that potential common cause heat sink performance problems that had the potential to increase risk were identified and corrected by Ginna. The inspectors closely examined potential macro fouling (silt, debris, etc.) issues and biotic fouling issues. The inspectors walked down accessible areas of the Service Water (SW) intake, chlorination system, and other support and sub components of the Service Water system to assess the material condition of these systems and components.

The inspectors reviewed a sample of condition reports (CRs) related to the CCW HXs, EDG HXs, the safety-related room coolers, and the SW system to ensure that Ginna was appropriately identifying, characterizing, and resolving problems related to these systems and components within regulatory requirements and Ginnas commitments.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

On September 21, 2006, the inspector observed a licensed operator simulator training scenario that was conducted using revised Emergency Operating Procedures (EOP)s which would be used following the completion of the October refuel outage when plant power would be increased by approximately 17 percent. The scenario observed was a small-break Loss of Coolant Accident (LOCA). The purpose of the training scenario was to inform operators of significant changes to the LOCA-specific EOPs, provide an overview of the rationale for the changes, and provide an opportunity for operators to use the procedures and identify possible areas for improvement.

The inspector attended the pre-scenario briefing where instructors provided operators an overview of changes to the EOPs and discussed differences between the current and post power uprate plant configurations. During the scenario the inspector observed and verified that operators were properly utilizing the EOPs, and training personnel were documenting issues that the operators had identified with the new EOPs.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors evaluated Ginnas work practices and follow-up corrective actions for selected system, structure, or component (SSC) issues to assess the effectiveness of Ginnas maintenance activities. The inspectors reviewed the performance history of those SSCs and assessed Ginnas extent-of-condition determinations for those issues with potential common cause or generic implications to evaluate the adequacy of Ginnas corrective actions. The inspectors reviewed Ginnas problem identification and resolution actions for these issues to evaluate whether Ginna had appropriately monitored, evaluated, and dispositioned the issues in accordance with Ginna procedures and the requirements of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance. In addition, the inspectors reviewed selected SSC classification, performance criteria and goals, and Ginnas corrective actions that were taken or planned, to verify whether the actions were reasonable and appropriate. The following issues were reviewed:

  • Corrective actions to address a through-wall leak in a weld for a relief valve off of the Service Water portion of the A Component Cooling Water heat exchanger that occurred initially during July 2005 and degraded over the next seven weeks.
  • Exposed rebar and spalled concrete on the containment structure were identified by the inspectors during a tour of the containment dome area. The inspector reviewed portions of the Ginna ASME Section XI Subsections IWE and IWL containment inspection program and procedure EP-2-P-0169, Ginna Structural Assessment and Monitoring Program and verified that these degraded areas had either been previously identified by Ginna or were subsequently dispositioned in accordance with these programs.
  • A failure of the Main Steam Check Valve counterweight arm with subsequent elevation of the Main Steam system to A(1)" status was reviewed by the inspectors. Immediate corrective actions and the plans for future monitoring of the system were reviewed.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors evaluated the effectiveness of Ginnas maintenance risk assessments required by paragraph a(4) of 10 CFR 50.65. This inspection included discussions with control room operators and scheduling department personnel regarding the use of Ginnas online risk monitoring software. The inspectors reviewed equipment tracking documentation and daily work schedules, and performed plant tours to gain reasonable assurance that actual plant configuration matched the assessed configuration.

Additionally, the inspectors verified that Ginnas risk management actions, for both planned and/or emergent work, were consistent with those described in procedure IP-PSH-2, "Integrated Work Schedule Risk Management." Risk assessments for the following out-of-service systems, structures, and/ or components were reviewed:

  • Planned maintenance on the C safety injection pump while the B containment spray system was still inoperable due to maintenance which occurred on the previous day. (July 11, 2006)
  • Unplanned maintenance on residual heat removal flow transmitters FT-931A and FT-931B. (July 25 and 26, 2006)
  • Response to a declaration of off-site power being inoperable, as calculated on the Contingency Monitor at the Energy Control Center, in the event of a plant trip. (August 1, 2006)
  • Unplanned maintenance to replace one of two A Main Steam Line Non-return Check Valve counter weight lever arms when it was found on the floor under the valve. (August 11, 2006)
  • Unplanned maintenance when the A Residual Heat Removal (RHR) Heat Exchanger flow control valve was determined to be incorrectly positioned and thus potentially rendering the system inoperable. (August 19, 2006)
  • Unplanned troubleshooting activities conducted on the steam driven auxiliary feedwater pump discharge valve MOV-3996. (September 19, 2006)

b. Findings

Introduction:

A non-cited violation (NCV) of 10 CFR 50.72(b)(3)(v)(A) was identified for not reporting to the NRC that offsite power had degraded on two occasions.

Description:

The operability of offsite power at Ginna is determined, in part, by a software Contingency Monitoring Program that monitors the local electrical distribution grid. The software program and supporting hardware are located at the energy control center (ECC) for the local electrical grid transmission system operator (TSO), Rochester Gas and Electric (RG&E). If the contingency monitoring program determines that conditions on the local electrical grid have deteriorated to a point that the offsite power lines to Ginna may not be operable, an alarm is generated at RG&Es ECC. This information is then relayed to the Ginna control room where operators are directed in procedure O-6.13, Daily Surveillance Logs to declare offsite power inoperable until the undesirable grid conditions are resolved.

On July 17, 2006 and August 1, 2006, the contingency monitoring program indicated that conditions on the electrical grid had degraded to the point that Ginnas offsite power may not be operable because of high electrical demand. These conditions existed for approximately nine minutes and eight hours respectively. Although Ginna control room operators declared offsite power inoperable, the inspectors noted that they did not report the degraded electrical conditions to the NRC Operations Center per 10 CFR 50.72(b)(3)(v)(A). Page 54 of NUREG-1022 Event Reporting Guidelines indicates that such reports should be made if either the offsite power or onsite emergency power is unavailable to the plant regardless of whether the other system is available.

Ginna personnel attributed the missed reports to an inaccurate interpretation of NUREG-1022 and stated that future occurrences would be reported. Subsequently on August 2, 2006, when the grid contingency monitor indicated that the electrical distribution grid was degraded for approximately five hours, Ginna properly informed the NRC Operations Center via the Emergency Notification System (ENS). The following day on August 3, Ginna updated the August 2, 2006, ENS report to the NRC with information pertaining to the July 17th and August 1st events. The failure to notify the NRC of the degraded grid conditions was documented in Condition Report (CR)2006-003331, Missed NRC Notifications per 10 CFR 50.72 Regarding Inoperability of Both Offsite Power Lines.

Analysis:

The performance deficiency involved a failure of Ginna personnel on two occasions to notify the NRC that offsite power to the plant was inoperable per 10 CFR 50.72(b)(3)(v)(A). This deficiency was evaluated using the traditional enforcement process since the failure to make a required report could adversely impact the NRCs ability to carry out its regulatory mission. The inspectors evaluated the severity of this violation using the criteria contained in Supplement l - Reactor Operations and Section Vl.A.1 of the NRCs Enforcement Policy and determined that this finding met the criteria for dispositioning as a non-cited violation.

Enforcement:

10 CFR 50.72(b)(3)(v)(A) requires the NRC to be informed of any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures, systems, or components that are needed to shutdown the reactor and maintain it in a shutdown condition. Contrary to the above, on July 17, 2006 and August 1, 2006, Ginna did not report to the NRC that offsite power to the plant was inoperable. This is a violation of 10 CFR 50.72(b)(3)(v)(A). Because this finding met the criteria contained in Section Vl.A.1 of the NRCs enforcement policy, it is being dispositioned as a non-cited violation. (NCV 5000244/2006004-02, Failure to Make a 10 CFR 50.72(b)(3)(v)(A) Notification)

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed operability determinations to verify that the operability of systems important to safety was properly established, that the affected components or systems remained capable of performing their intended safety functions, and that no unrecognized increase in plant or public risk occurred. In addition, the inspectors reviewed the following operability evaluations to determine if system operability was properly justified in accordance with IP-CAP-1.1, Technical Evaluation for Current Operability and Past Operability Determination Worksheet:

  • CR 2006-003054, Leak on A CCW Pump Mechanical Seal
  • CR 2006-003857, RHR Flow Control Valve is Incorrectly Set
  • CR 2006-004291, Water Leaking From Bolts on TDAFW Pump

b. Findings

Introduction:

A Green self-revealing finding was identified when Ginna personnel did not adequately assess the effects of a service water leak that occurred in the room cooler for the C Standby Auxiliary Feedwater (SAFW) pump. As a result, water that had accumulated in electrical control panels for the pump was not detected. When the water was found by Ginna personnel during the performance of a routine surveillance test of the C SAFW pump, the pump was declared inoperable until the water was removed, which resulted in approximately 19 additional hours of out-of-service time.

Description:

Ginna has a SAFW system that was installed in 1977 as a backup to the Auxiliary Feedwater (AFW) system. The system includes redundant pumps, valves, and air coolers that are cooled by service water. The air coolers are located above each SAFW pump, and are required to support pump operability when outside air temperature exceeds 85 degrees. Although both pumps are located in close proximity to each other, some separation is provided by a concrete divider wall located between both pumps. The system is manually actuated, and is intended to be used in the event the AFW system is damaged if a high energy line break (HELB) occurred in the intermediate building. On September 24, 2006, at 2016, a security guard informed control room personnel that a large amount of water was flowing out of the access door to the SAFW building. A subsequent investigation by Ginna operations personnel determined that the water was leaking from a failed gasket in the room cooler for the C SAFW pump. Operators isolated the leak and drained water from the SAFW pump room. Because water did not appear to have sprayed on any electrical components that were associated with the C SAFW pump, the pump was not declared inoperable.

On September 25, 2006, when preparing to perform a scheduled surveillance test on the C SAFW pump, per PT-36Q C Standby Auxiliary Feedwater Pump Quarterly operators discovered water in electrical controllers for the C SAFW pump. Because the water could affect pump operability, Ginna control room personnel declared the pump inoperable.

After the water had been removed from the electrical controllers, resistance measurements checked, and PT-36Q successfully completed, the pump was declared operable at 0421 on September 26. Because Ginna personnel did not perform an adequate assessment of how the service water leak would affect the operability on September 24, a potential undetected failure mechanism-water accumulation in the SAFW pump electrical controllers was not identified and corrected. As a result, the C SAFW pump was potentially inoperable for an additional 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br />.

Analysis:

The performance deficiency associated with this finding was a failure to adequately assess the operability of the C SAFW pump following a service water leak in the associated room cooler. This was contrary to the guidance contained in 1 of Station Procedure IP-CAP-1, Condition Reporting, which states that when a condition report has been prepared, a licensed SRO/Shift Manager will review it to ensure appropriate actions are taken as required by the situation. This finding is more than minor because it is associated with the Mitigating Systems Cornerstone and affects the cornerstone objective of ensuring the reliability of systems that respond to initiating events to prevent undesirable consequences. This finding was determined to be of very low safety significance (Green) by using Phase 1 of the Inspection Manual Chapter (IMC) 0609, Significance Determination Process. The finding screened to Green since it was not a design or qualification deficiency and did not result in a loss of safety function. This finding is related to the cross-cutting aspects of problem identification and resolution in that Ginna did not fully evaluate the operability of the C SAFW pump following the leak, which sprayed water on electrical components.

Enforcement:

No violation of NRC requirements occurred since the C SAFW pump was not out of service for greater than the seven day Limiting Condition for Operation (LCO) time outlined in plant Technical Specifications (TS). This issue has been entered into the Ginna corrective action program as CR 2006-004391, Service Water Leak in SAFW Pump Room Cooler and CR 2006-004420, Found Water in Standby Aux Feedwater Pump C Instrument and Local Control Panels. (FIN 05000244/2006-004-03, Did not conduct a thorough operability assessment and identify that the C SAFW was degraded)

==1R17 Permanent Plant Modifications (IP

==

71111.17B - 7 samples)

a. Inspection Scope

The inspectors reviewed seven risk-significant plant modification packages selected from the design changes and procedure changes that were completed within the past two years. The review was performed to verify that:

(1) the design bases, licensing bases, and performance capability of risk-significant structures, systems, and components (SSCs) had not been degraded through the modifications; and
(2) the modifications performed during increased risk configurations did not place the plant in an unsafe condition. The modifications reviewed are listed in Attachment 1.

The selected plant modifications were distributed among the Initiating Event, Mitigating Systems, and Barrier Integrity cornerstones. For these selected modifications, the inspectors reviewed applicable design inputs, assumptions, and design calculations to determine the design adequacy. The inspectors also reviewed field change notices that were issued during the installation to confirm that the problems associated with the installation were adequately resolved. In addition, the inspectors reviewed the post-modification testing, functional testing, and instrument and relay calibration records to determine readiness for operations. Finally, the inspectors reviewed the affected procedures, drawings, design basis documents, and UFSAR sections to verify that the affected documents were appropriately updated.

For the accessible components associated with the hardware modifications, the inspectors also walked down the systems to detect possible abnormal installation conditions.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors observed portions of six post-maintenance testing activities in the field to determine whether the tests were performed in accordance with approved procedures.

The inspectors assessed the tests adequacy by comparing the test methodology to the scope of maintenance work performed. In addition, the inspectors evaluated the test acceptance criteria to verify that the tested components satisfied the applicable design and licensing bases and technical specification requirements. The inspectors reviewed the recorded test data to determine whether the acceptance criteria were satisfied. The following post-maintenance testing activities were reviewed:

  • PT-3Q, Containment Spray Pump Quarterly Test, to retest after motor swap out of MOV 860D under Work Order (WO) 20404504, Swap out Existing Actuator with Rebuilt Actuator (July 11, 2006)
  • CPI-IR-N36, Calibration of Nuclear Instrument System Intermediate Range N-36," conducted after WO 20601304, Install New Low Voltage and High Voltage Power Supplies in IRNI N-36" (September 12, 2006)
  • PT-33A, Spent Fuel Pool Pump A conducted after WO20604079, Rebuild of SFP Pump A (September 21, 2006)

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

Prior to the refuel outage, the inspectors observed preparatory activities which included the performance of surveillance tests on equipment that is used during outage activities.

Activities observed included observation of a surveillance test that tests the auxiliary building crane interlocks.

The inspectors also reviewed the outage schedule and risk profile to verify that Ginna had attempted to identify and assess risk-significant activities and mitigate risk where appropriate.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed the performance and/or reviewed test data for the following seven surveillance tests that are associated with selected risk-significant systems, structures, and components (SSCs) to verify that Technical Specifications (TS) were followed and that acceptance criteria were properly specified. The inspectors also verified that proper test conditions were established as specified in the procedures, that no equipment preconditioning activities occurred, and that acceptance criteria had been met or the deficiency was appropriately entered into the Ginna Corrective Action Program.

  • PT-13.3, Fire Pump Electrical Equipment Checks (July 3, 2006)
  • PT-2.9, Check Valve and Manual Valve Exercising Quarterly Surveillance (July 7, 2006)
  • PT-17.2, Process Radiation Monitors R-11-R-22 Iodine Monitors R-10A and R-10B (July 18, 2006)
  • Work Order 20600605, Performance Test LS-6848 and LS-6851, Intermediate Building Sump Pump Level Switches (August 10, 2006)
  • S-12.4, RCS Leakage Surveillance Record Instructions (August 31, 2006)

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the following temporary plant modifications to determine whether the temporary change adversely affected system or support system availability or adversely affected a function important to plant safety. The inspectors reviewed the associated system design bases, including the UFSAR and TS, and assessed the adequacy of the safety determination screening and evaluation. The inspectors also assessed configuration control of the temporary change by reviewing selected drawings and procedures to verify whether appropriate updates had been made. The inspectors compared the actual installation with the temporary modification documents to determine whether the implemented change was consistent with the approved documented modification. The inspectors reviewed the post-installation test results to verify whether the actual impact of the temporary change had been adequately demonstrated by the test. The temporary modifications were reviewed by the inspectors to verify they were installed in conformance with the instructions contained in procedure IP-DES-3, Temporary Modifications.

  • 2006-0015, Use of a Temporary Reverse Osmosis Skid to Remove Silica From the Reactor Water Storage Tank (RWST) and Spent Fuel Pool (SFP)

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

On August 8, 2006, the inspectors observed portions of the third quarter emergency preparedness drill. The drill scenario involved a small break loss of coolant accident, and tested use of the Outage Control Center as the new Operations Support Center.

The inspector verified that the appropriate emergency classifications were made, and notifications to external parties were completed in a timely manner as required by the Ginna emergency response plan.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems (IP 71152)

.1 Identification and Resolution of Problems - Permanent Plant Mods (71111.17-02.03)

a. Inspection Scope

The inspectors reviewed condition reports (CRs) associated with 10 CFR 50.59 issues and plant modification issues to ensure that Ginna had identified, evaluated, and corrected problems associated with these areas and that the planned or completed corrective actions for the issues were appropriate. The listing of the CRs reviewed is provided in Attachment 1.

b. Findings

No findings of significance were identified.

.2 Review of Items Entered into the Corrective Action Program

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the Ginna corrective action program. This review was accomplished by reviewing electronic versions of each condition report (CR), attending daily screening meetings, and accessing Ginnas computerized database.

4OA3 Event Follow-up

.1 Loss of Spent Fuel Pool Cooling

a. Inspection Scope

During the week of September 18, 2006, the inspectors followed Ginnas response to a loss of both spent fuel pool (SFP) cooling pumps in the spent fuel pool cooling system and the corrective actions taken. The B pump failed when it was started for surveillance testing on the 12th of September, and found to be cavitating later that evening. Subsequently on September 18th, the A pump failed when it was being stopped and restarted to facilitate testing of the B pump SFP motor. In response to the loss of cooling, the plant entered ER-SFP.1, Loss of Spent Fuel Pool Cooling, and formed an Incident Response Team to provide 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> coverage until the issue was resolved. On September 21, spent fuel pool cooling was restored when a temporary skid-mounted SFP pump was installed. The A and B pumps were subsequently repaired and restored to service on September 22. Ginna formed a root cause inspection team to investigate the pump failures.

b. Findings

No findings of significance were identified.

.2 (Closed) LER 05000244/2006001-00 Potential Failure of Charging Pumps due to

Unevaluated Fire Scenario On May 17, 2006, Ginna identified a previously unevaluated failure mode that potentially existed for the charging pumps in certain Appendix R fire scenarios. This event was reviewed, assessed, and dispositioned by the Triennial Fire Inspection Team (Inspection Report 05000244/2006007) as part of the Problem Identification and Resolution portion of that inspection. As outlined in the report, no enforcement action was taken by the NRC regarding this issue since the item met the enforcement discretion criteria for fire-related design issues. Accordingly this LER is closed.

.3 (Closed) LER 05000244/2006002-00 Off-Site Power Systems Declared Inoperable

This LER was written to document that on July 17, August 1, and August 2, 2006, offsite power was inoperable at Ginna for up to eight hours at various times because of high demand on the electrical grid. Details surrounding the events are discussed in section 1R13 of this report. This LER was reviewed by the inspectors and no additional findings of significance or violations of NRC requirements were identified. Ginna documented the degraded offsite power events in several condition reports, including CR 2006-003290, Offsite Power Inoperability. This LER is closed.

.4 (Closed) LER 05000244/2006003-00 Inoperability of Two Channels of Flow

Instrumentation On July 25, 2006, during a review of planned work on Residual Heat Removal (RHR) to Safety Injection (SI) flow transmitters, Ginna identified that the flow transmitters were not powered from the electrical train which powers the associated RHR pump. As a result, electrical train separation was not maintained in accordance with the plant licensing basis. The condition was an original plant design deficiency and constituted a violation of Technical Specification 3.3.3, which requires two operable channels of RHR instrumentation. When this condition was discovered, Ginna promptly entered the appropriate Limiting Condition for Operation (LCO) in TS 3.3.3 and initiated a modification to reconfigure the electrical power to the flow transmitters so the power would be aligned with the respective RHR pump. The modification was completed and the LCO exited on July 26, 2006. This finding is more than minor because it affected the design control attribute of the Mitigating Systems Cornerstone impacting the objective to ensure reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically the design flaw would have impacted the operators ability to properly transfer the plant into a high pressure recirculation mode in certain accident sequences. The violation was considered to have very low safety significance (Green), screening directly to Green in accordance with the SDP because it does not result in a loss of operability of the RHR system. This Ginna-identified finding involved a violation of TS 3.3.3, Post Accident Monitoring Instrumentation. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.

4OA5 Other Activities

Introduction:

A Green NRC-identified non-cited violation (NCV) of 10 CFR 50.74(c),

Notification of Change in Operator or Senior Operator Status, was identified for failure to notify the NRC within thirty days of a change in a licensed operators medical status.

Description:

The NRC identified that during the period between June 2, 2006, and August 15, 2006, a licensed reactor operator stood several watches in a Technical Specification (TS) license position with a medical condition that would prohibit solo operation as outlined in ANSI/ANS-3.4-1983, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants. When Ginna became aware of the operators medical condition on June 2, 2006, the facility failed to notify the NRC within 30 days as required by 10 CFR 50.74, Notification of Change in Operator or Senior Operator Status.

The Ginna training department is responsible for the scheduling of operator medical examinations. IP-TQS-3, Operator and Fire Brigade Physicals is the governing procedure for tracking these items. The inspector noted that IP-TQS-3, did not specify when the NRC should be notified regarding the development of long term medical conditions.

When the inspector informed the Ginna training department of the missed notification, Condition Report 2006-003168, Failure to Notify NRC in Accordance With 10 CFR 50 74, was written. On August 15, 2006, Ginna sent a letter to the NRC that, in part, informed the NRC of the change in the medical status of the licensed operator.

Analysis:

The performance deficiency associated with this finding was a failure of Ginna to notify the NRC within 30 days of the identification of a medical condition that caused a licensed reactor operator to fail to meet the standards of 10 CFR 55.21 as required by 10 CFR 50.74(c). The NRC relies on facility licensees to evaluate medical conditions and, if warranted, to report those changes to the NRC, so that the NRC can take appropriate regulatory action, including issuance of a conditional (restricted) license.

The inspectors determined that Ginnas failure to report the medical status of the operator to the NRC impacted the regulatory process, in that between June and August 2006, the NRC was unaware of a medical condition that warranted issuance of a conditional (restricted) license. Because this finding impacted the regulatory process, it was dispositioned using the traditional enforcement process instead of the SDP.

Enforcement:

10 CFR 50.74(c) requires, in part, that each facility licensee notify the NRC within 30 days of a permanent disability or illness as described in 10 CFR 55.25 in regards to a licensed or senior licensed operator. 10 CFR 55.25 requires, in part, that if a licensed reactor operator develops a permanent physical or mental condition that causes the reactor operator to fail to meet the requirements of 10 CFR 55.21, the facility must notify the NRC within 30 days of learning of the diagnosis. For conditions for which a conditional (restricted) license is required, the facility licensee must provide medial certification on NRC Form 396, Certification of Medical Examination by Facility Licensee. Contrary to the above, Ginna did not notify the NRC within 30 days of learning of a medical condition of a licensed reactor operator for which a conditional (restricted) licensed was required. Specifically, Ginna became aware of a medical condition in June 2006 that caused a licensed reactor operator to fail to meet the requirements of 10 CFR 55.21 and for which a conditional (restricted) license was required. Ginna did not provide the NRC Form 396 medical condition certification to the NRC until August 2006.

Ginnas failure to notify the NRC of the licensed reactor operators medical condition is considered a violation of 10 CFR 50.74(c). The violation is determined to be a Severity Level lV (Supplement 1) violation. Because this finding met the criteria contained in Section Vl.A.1 of the NRCs enforcement policy, it is being dispositioned as a non-cited violation. (NCV 5000244/2006004-04, Ginna Did Not Notify the NRC of a Licensed Operators Medical Condition)

4OA6 Meetings, Including Exit

Exit Meeting Summary

On October 5, 2006, the resident inspectors presented the inspection results to Mrs.

Korsnick and other members of her staff, who acknowledged the findings. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. Proprietary information was examined during this inspection, but is not specifically discussed in the report.

4OA7 Licensee-identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements, which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • TS 3.3.3 requires that two channels of flow indication for RHR to SI, one for each medium head injection recirculation flowpath be available for post-accident monitoring and to support operator response. Contrary to this requirement, the flow transmitters for each pump were not powered from the same electrical train as the respective RHR pump. As a result, both flow transmitters were inoperable for post-accident monitoring. This condition was documented by Ginna in CR 2206-003090 and subsequently corrected. This finding is of very low safety significance because it did not involve a loss of operability of the RHR system.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

S. Adams

Manager of Operations

D. Blankenship

Manager, Radiation Protection

E. Groh

Assistant Operations Manager (Shift)

D. Holm

Plant Manager

S. Kennedy

Emergency Preparedness Manager

M. Korsnick

Vice President, Ginna

J. Pacher

Manager Nuclear Engineering Services

B. Randall

Nuclear Safety and Licensing Manager

P. Swift

Principal Engineer, Electrical/I&C

W. Thomson

General Supervisor, Chemistry

R. Whalen

Manager, Ginna Maintenance

D. Wilson

Principal Engineer, Balance of Plant

J. Yoe

Scheduling Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000244/2006004-01 UNR Review the significance of not maintaining the Containment Penetration Cooling system in accordance with the UFSAR and system P&IDs

Opened and Closed

05000244/2006004-02 NCV Failure to Make a 10-CFR 50.72(b)(3)(v)(A) Notification
05000244/2006004-03 FIN Did not conduct a thorough operability assessment and identify that the C SAFW was degraded
05000244/2006004-04 NCV Ginna Did Not Notify the NRC of a Licensed Operators Medical Condition

Closed

05000244/2006001-00 LER Potential Failure of Charging Pumps due to Unevaluated Fire Scenario (Section 4OA3.2)
05000244/2006002-00 LER Off-Site Power Systems Declared Inoperable (Section 4OA3.3)
05000244/2006003-00 LER Inoperability of Two Channels of Flow Instrumentation (Section 4OA3.4)

Discussed

NONE

LIST OF DOCUMENTS REVIEWED