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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEAR2CAN119504, Special Rept Re SG Tube Surveillance Category C-3 Results1995-11-13013 November 1995 Special Rept Re SG Tube Surveillance Category C-3 Results 0CAN079502, Special Rept:On 950608,electric Fire Pump P-6A Declared Inoperable.Cause of Degraded Performance Indeterminate at Time But Believed to Be Result of Normal Wear.Temp Fire Pump for Backup Fire Suppression Water Supply Installed1995-07-14014 July 1995 Special Rept:On 950608,electric Fire Pump P-6A Declared Inoperable.Cause of Degraded Performance Indeterminate at Time But Believed to Be Result of Normal Wear.Temp Fire Pump for Backup Fire Suppression Water Supply Installed 1CAN109302, Special Rept:On 930922,EFP P-6A Exceeded AOT of Seven Days Due to Mod Work on 4,160 Volt Bus A-1.Power to non-vital Bus A-1 Restored on 930922 & Weekly Surveillance on EFP P-6A Performed Satisfactorily on 9309231993-10-14014 October 1993 Special Rept:On 930922,EFP P-6A Exceeded AOT of Seven Days Due to Mod Work on 4,160 Volt Bus A-1.Power to non-vital Bus A-1 Restored on 930922 & Weekly Surveillance on EFP P-6A Performed Satisfactorily on 930923 2CAN049107, Special Rept:On Eighth Refueling Outage,Consisting of Insp of Steam Generator.Insp Revealed Three Defective Tubes in B Steam Generator & No Defective Tubes in a Steam Generator.Condenser Tubing Routinely Cleaned1991-04-0505 April 1991 Special Rept:On Eighth Refueling Outage,Consisting of Insp of Steam Generator.Insp Revealed Three Defective Tubes in B Steam Generator & No Defective Tubes in a Steam Generator.Condenser Tubing Routinely Cleaned 2CAN019101, Special Rept:On 901219,fire Pumps Inoperable During Performance of Surveillance Test.Method of Performing Surveillance Procedure Will Be Revised by 9103011991-01-0202 January 1991 Special Rept:On 901219,fire Pumps Inoperable During Performance of Surveillance Test.Method of Performing Surveillance Procedure Will Be Revised by 910301 0CAN129002, Special Rept:On 901026,fire Pump Inoperable for More than 7 Days.Temporary Pump Installed as Backup1990-12-0303 December 1990 Special Rept:On 901026,fire Pump Inoperable for More than 7 Days.Temporary Pump Installed as Backup 1CAN119012, Special Rept:On 901022,Unit 1 Control Room Halon Sys Inoperable for More than 14 Days Due to Removal of Ceiling Tiles in Auxiliary Control Room for Installation of Conduit Pulling of Cables.Operability Restored on 9011061990-11-21021 November 1990 Special Rept:On 901022,Unit 1 Control Room Halon Sys Inoperable for More than 14 Days Due to Removal of Ceiling Tiles in Auxiliary Control Room for Installation of Conduit Pulling of Cables.Operability Restored on 901106 2CAN089008, Voluntary Rept 50-368/90-V01-00:revises Completion Date for Commitment Date in Voluntary Rept from 900801 to 900831 Re Inadvertent Starting of Emergency Diesel Generator While Attempting to Air Roll Engine During Maint1990-08-0303 August 1990 Voluntary Rept 50-368/90-V01-00:revises Completion Date for Commitment Date in Voluntary Rept from 900801 to 900831 Re Inadvertent Starting of Emergency Diesel Generator While Attempting to Air Roll Engine During Maint 2CAN089010, Voluntary Rept 50-368/90-V02-00 Re Result of Postulating Failure of Check Valve in LPSI Sys Not Previously Postulated.Caused by Higher Differential Pressure Not Considered.Valve Mfg Consulted1990-08-0303 August 1990 Voluntary Rept 50-368/90-V02-00 Re Result of Postulating Failure of Check Valve in LPSI Sys Not Previously Postulated.Caused by Higher Differential Pressure Not Considered.Valve Mfg Consulted 2CAN098905, Special Rept 50-368/89-013-00 on 890626,pressurizer Level Decreased While Flushing Header C of LPSI Sys.Caused by Backleakage Through Header Safety Injection Check Valve.Hpsi Pump Started & Valve Opened to Inject Water Into RCS1989-09-23023 September 1989 Special Rept 50-368/89-013-00 on 890626,pressurizer Level Decreased While Flushing Header C of LPSI Sys.Caused by Backleakage Through Header Safety Injection Check Valve.Hpsi Pump Started & Valve Opened to Inject Water Into RCS 05000313/LER-1986-002, Requests Extension Date of 860930 to Allow Time to Update LER 86-002-00 Re Inadequate 10CFR50.59 Design Change Review1986-08-19019 August 1986 Requests Extension Date of 860930 to Allow Time to Update LER 86-002-00 Re Inadequate 10CFR50.59 Design Change Review 2CAN078504, Ro:On 850410,unmonitored Release of Radioactive Water Into Oily Water Separator Occurred.Caused by Inadvertent Opening of HX Drain During Maint Insp.Drain Closed After Approx 3 H. Dardanelle Reservoir Unaffected.Personnel Counseled1985-07-11011 July 1985 Ro:On 850410,unmonitored Release of Radioactive Water Into Oily Water Separator Occurred.Caused by Inadvertent Opening of HX Drain During Maint Insp.Drain Closed After Approx 3 H. Dardanelle Reservoir Unaffected.Personnel Counseled 2CAN068508, Ro:On 850529 high-range Containment Radiation Monitor 2RITS-8925-2 Discovered Failed Low.Redundant Monitor 2RITS-8925-1 Verified Operable.Caused by Open Circuit in Signal & High Voltage Cable Connectors.Connectors Replaced1985-06-28028 June 1985 Ro:On 850529 high-range Containment Radiation Monitor 2RITS-8925-2 Discovered Failed Low.Redundant Monitor 2RITS-8925-1 Verified Operable.Caused by Open Circuit in Signal & High Voltage Cable Connectors.Connectors Replaced 1CAN108305, Ro:On 831013,single Battery Cell in One Bank of Batteries Found Unacceptable & Declared Inoperable.Util Application of 3.7.2 Series of Specs Discussed1983-10-21021 October 1983 Ro:On 831013,single Battery Cell in One Bank of Batteries Found Unacceptable & Declared Inoperable.Util Application of 3.7.2 Series of Specs Discussed ML20054D8561982-04-16016 April 1982 RO 50-368/82-011:on 820415,leak Discovered Inside Containment in Steam Generator B Blowdown Line Between Valve 2CV1065 & Containment Penetration.Unit Shut Down.Blowdown Line Will Be Repaired ML20064H4491978-12-14014 December 1978 RO 50-368/78-17 on 781201:Emergency Feedwater Train B Response Time Was Less Conservative than Assumed in the Safety Analysis Due to Unknown Cause.Emergency Feedwater Train B Reset to a Valve Consistent W/Safety Analysis 1995-07-14
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8931999-10-31031 October 1999 Rev 1 to BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20212L1141999-10-0101 October 1999 Safety Evaluation Granting Request for Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c 0CAN109902, Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20216J6271999-09-27027 September 1999 Rev 0 to CALC-98-R-1020-04, ANO-1 Cycle 16 Colr ML20212F5261999-09-22022 September 1999 SER Approving Request Reliefs 1-98-001 & 1-98-200,parts 1,2 & 3 for Second 10-year ISI Interval at Arkansas Nuclear One, Unit 1 0CAN099907, Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with ML20211F4281999-08-25025 August 1999 Safety Evaluation Concluding That Licensee Provided Acceptable Alternative to Requirements of ASME Code Section XI & That Authorization of Proposed Alternative Would Provide Acceptable Level of Quality & Safety 0CAN089904, Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with ML20210K8831999-07-29029 July 1999 Non-proprietary Addendum B to BAW-2346P,Rev 0 Re ANO-1 Specific MSLB Leak Rates 0CAN079903, Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with ML20207E7231999-06-0202 June 1999 Safety Evaluation Authorizing Proposed Alternative Exam Methods Proposed in Alternative Exam 99-0-002 to Perform General Visual Exam of Accessible Areas & Detailed Visual Exam of Areas Determined to Be Suspect ML20196A0191999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20196A6251999-05-31031 May 1999 Non-proprietary Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20195D1991999-05-28028 May 1999 Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14 ML20206M7711999-05-11011 May 1999 SER Accepting Relief Request from ASME Code Section XI Requirements for Plant,Units 1 & 2 0CAN059903, Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with ML20206F0691999-04-29029 April 1999 Safety Evaluation Accepting Licensee Re ISI Plan for Third 10-year Interval & Associated Requests for Alternatives for Plant,Unit 1 ML20205M6941999-04-12012 April 1999 Safety Evaluation Granting Relief for Second 10-yr Inservice Inspection Interval for Plant,Unit 1 ML20205D6061999-03-31031 March 1999 Safety Evaluation Supporting Licensee Proposed Approach Acceptable to Perform Future Structural Integrity & Operability Assessments of Carbon Steel ML20205R6351999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ano,Units 1 & 2. with ML20205D4711999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Employ Alternative Welding Matls of Code Cases 2142-1 & 2143-1 for Reactor Coolant System to Facilitate Replacement of Steam Generators at Arkansas Nuclear One,Unit 2 ML20204B1861999-03-15015 March 1999 Safety Evaluation Authorizing Licensee Request for Alternative to Augmented Exam of Certain Reactor Vessel Shell Welds,Per Provisions of 10CFR50.55a(g)(6)(ii)(A)(5) 0CAN039904, Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with ML20212G6381999-02-25025 February 1999 Ano,Unit 2 10CFR50.59 Rept for 980411-990225 ML20203E4891999-02-11011 February 1999 Rev 1 to 97-R-2018-03, ANO-2,COLR for Cycle 14 ML20199F0351998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ano,Units 1 & 2 ML20198M7841998-12-29029 December 1998 SER Accepting Util Proposal to Use ASME Code Case N-578 as Alternative to ASME Code Section Xi,Table IWX-2500 for Arkansas Nuclear One,Unit 2 0CAN129805, LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With1998-12-11011 December 1998 LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20198D2441998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ano,Units 1 & 2. with ML20199F7401998-11-16016 November 1998 Rev 9 to ANO-1 Simulator Operability Test,Year 9 (First Cycle) ML20195B4801998-11-0707 November 1998 Rev 20 to ANO QA Manual Operations ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 0CAN119808, Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with ML20197H0741998-10-29029 October 1998 Rev 1 to Third Interval ISI Program for ANO-1 ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20154J2471998-10-0909 October 1998 SER Accepting Inservice Testing Program,Third ten-year Interval for License DPR-51,Arkansas Nuclear One,Unit 1 0CAN109806, Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods 0CAN099803, Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with ML20237B7671998-08-19019 August 1998 ANO REX-98 Exercise for 980819 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed 0CAN089804, Monthly Operating Repts for July 1998 for Ano,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ano,Units 1 & 2 ML20196C7831998-07-30030 July 1998 Summary Rept of Results for ASME Class 1 & 2 Pressure Retaining Components & Support for ANO-1 ML20155H7161998-07-15015 July 1998 Rev 1 to 96-R-2030-02, Revised Reactor Vessel Fluence Determination ML20236R0531998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ano,Units 1 & 2 ML20249B7791998-06-22022 June 1998 Part 21 Rept Re Findings,Resolutions & Conclusions Re Failure of Safety Related Siemens 4KV,350 MVA,1200 a Circuit Breakers to Latch Closed ML20249B5091998-06-15015 June 1998 SG ISI Results for Fourteenth Refueling Outage 1999-09-30
[Table view] |
Text
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w;r Ent' na e m o e u.o:,ia. - [
em . ' Route 3. Box 137G -I N *'-
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, August 3, 1990' ml . 2CAN089010
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U. S. Nuclear Regulatory Commission -l Document-Control Desk Mail Station P1-137.
Washington, D. C.. 20555
SUBJECT:
Arkansas Nuclear One - Unit 2 Li Docket No._ 50-368 '
- License No. NPF-6 Voluntary Report No. 50-368/90-V02-00 - !
Gentlemen: -
This . report is being-submitted as a voluntary report to provide information ,
.obtained as a result of postulating a failure of a check valve in the Low ,~
Pressure Safety Injection System which had not previously been postulated.- >
Very truly yours, -
/'E!C.-Ewing. '
General Manager,
- Assessment ECE/DM/sgv Attachment cc:- Regional Administrator Region IV U. S. Nuclear Regulatory Commission 611 Ryan Plaza-Drive, Suite 1000 !
Arlington, TX 76011 INP0 Records Center .
Suite 1500 l 1100 Circle 75 Parkway .l Atlanta, GA 30339-3064 l l
4008080234 900803 ff
-hO POCK 05000368 4 PDC , l l
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4
,Page.11 4
'A. Plant' Status At the time of discovery of this condition Arkansas Nuclear One, Unit <
Two (ANO-2) was operating at 100 percent of rated thermal power in Mode 1 (Power Operation). Reactor Coolant System (RCS) [AB] temperature was-approximately 580 degrees Fahrenheit and RCS pressure about 2250 psia.
B. Event Description As part of an ongoing program implemented to ensure that switch settings on_c_ertain motor operated valves (MOVs) are. set and maintained ,
correctly to accommodate the maximum differential pressures expected on these valves, the. calculations used in establishing the design and functional _ requirements (e.g., torque switch settings, valve actuator sizing, etc.), for MOVs in various plant systems are being reviewed and revised,.if~necessary. The_ calculation revisions are sometimes necessary due to the development of new differential pressures (APs) that:are postulated to exist across the valve (s). The new APs are being derived by utilizing different assumptions for plant operating conditions (usually worst case conditions) than those used to establish the current design requirements for the valves. Postulating various equipment failures (act_ive and passive component failures), that were not assumed to occur when the original calculations were performed, is a major factor in establishing new APs and thus revised functional requirements for the valves. This approach essentially creates new
' operability' requirements for MOVs and established a new and enhanced design basis for individual MOVs. In some cases, the new postulated AP -
that a valve is required to operate against (open and close) is higher than that used in the original design calculations, thus requiring modifications to the valve and/or valve actuator to provide the identified functional capability. Additionally, if modification of the-valve or actuator is necessary to ensure the valve will operate properly under the_new postulated conditions, a question of whether the valve (s) was operable during previous plant operations is generated.
The Emergency Core Cooling System (ECCS) is comprised of the High -
Pressure Safety Injection (HPSI) [BQ], Low Pressure Safety Injection (LPSI) [BP] pumps and piping, and the Safety Injection Tanks (SITS).and associated piping. There are four injection headers from the ECCS to provide a cooling water flowpath to each of the RCS cold legs. A typical. injection header is supplied by a LPSI header and HPSI header which are joined together. (See Figure 1.) Design pressures for the different portions of system piping are as indicated on Figure 1.
In April 1989, revisions to calculation k-2054-00 for the LPSI system header isolation M0V's (2CV-5017, 2CV-5037, 2CV-5057 and 2CV-5077) were completed. This calculation indicated that based on assumed worst case conditions the maximum AP these valves should be required to operate against was approximately 1260 psid. This AP was significa M y larger that the original maximum AP (approximately 480 psid), wb k n was used to establish the existing design requirements for these MOVs.
Additionally, the new calculated AP for these valves was somewhat
- unique in that contrary to the original calculations, the highest L system pressure was now postulated to occur on the downstream side of the valve disc. The original calculation had assumed that the valve
, would be required to operate against the maximum discharge pressure
_p .
Page 2 '
1 produced by an operating LPSI pump. The LPSI pump pressure is exerted i
-on the upstream side of the valve disc.
i The revised calculation utilized new assumptions for plant conditions and considered that during certain accident conditions (a limited range - ,
of small break LOCAs) both a HPSI and LPSI pump would be operating and with the current system design all the safety injection MOVs would be open. Under the postulated conditions RCS pressure could remain elevated above LPSI pump pressure and since HPSI discharge pressure would be significantly higher than LPSI discharge pressure, the LPSI v check valves (2SI-14s) would be in a closed position essentially acting as passive components under these conditions.- Following a postulated i failure (passive failure) of one_of the 251-14 check valves, the LPSI system could be subjected to the pressure of the operating HPSI pump (approximately 1450 psig). With a design pressure of approximately 500 psi, the LPSI-system could be overpressurized. The AP across the LPSI MOVs would be approximately 1260 psid (1450 psig minus the LPSI pump ',
discharge pressure of approximately 190 psig). Additionally, utilizing these assumptions the highest pressure exerted across the valve would
- become the_ operating pressure of the HPSI pump; the highest pressure would exist on what is'normally considered to be the downstream side of ,
the valve. Due to the physical design of the LPSI valves,.the high pressure would b exerted under the valve disc and would significantly increase the torque required to close the valve if open (i.e., the valve would have'to close against a AP of 1260 psid). The previous t LPSI MOV calculations had assumed a maximum AP of 480 psid across the valve with the highest pressure on the LPSI pump side of the valve.
Further evaluation of the condition was completed in August 1989, and-included a detailed review of the design capability of the LPS1 MOVs in their existing configuration. Based on this evaluation'it was determined that if the LPSI valves were open the valve actuators would not be capable of closing the valves under these new postulated conditions..
C. Root Cause L The criteria that existed during initial plant construction for l establishing the design and functional requirements for the LPSI header l- isolation MOVs did not consider the assumptions aiscussed above which were used to derive a new AP across the valves. Therefore,'this higher
'AP was not considered and the valve actuator was not originally l
designed to accommodate the effects of the higher AP.
D. Corrective Actions l The valve manufacturer, Target Rock Corporation (TRC) [T020], was consulted and concurred that if the LPSI MOV was open, the Limitorque actuator presently used on the valve would not be able to fully close against the.AP created by the postulated conditions. TRC stated that the Limitorque actuator could be modified by changing the gearing, and torque switch setting which would allow the actuator to close the valve against the postulated AP. .
Modifications to the LPSI valve actuators were developed and implemented during the 2R7 refueling outage (September 1989 to November 1989) to increase the capability of the valve actuator to close against a AP of 1260 psid with the highest pressure on the downstream side of the valve.
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Additionally, the ANO-2 Emargency Operating Procedure was revised to specify closing the LPSI MOVs after a Recirculation (Actuatior Signal (RAS) was initiated. This should ensure that the LPSI piping would not' be' exposed to pressures greater _ than its design pres ore if one of the 2SI-14s failed and RCS pressure or HPSI pressure were still above,the design pressure for the LPSI piping.
As afresult'of the MOVATS program established by Engineering in 1986' to evaluate the design and functional requirements for safety related ,
MOVs, deficiencies related to MOVs installed in.the plant are being identified. The valves or actuators'are being modified (as necessary)_
to; ensure design requirements are satisfied. "
E. Safety Significance
-The function of the LFSI MOVs in an accident condition (SBLOCA) is to open to provide a flovpath for injection of water to the RCS. The :
ability of the valve (:) to open was not affected prior to or after the :
, calculations were revised and the valve actuators modified. One of the [
~
primary concerns related to the as found condition of the LPSI NVs !
considering the postulated scenario was the potential effect of the condition on the functioral capability of the ECCS, while operating in i a post LOCA containment sump recirculation mode. If a failure of one 1 of the 2SI-14 check vaives were to occur while in this configuration and the size of the iwitiating LOCA was such that RCS pressure and HPSI system pressure were still above the design pressure of the LPSI system at the. time of an RA'i, then the' LPSI piping might be exposed to pressure greater than its design pressure and could possibly rupture.-
This could result in diversion of HPSI flow through the ruptured LPSI piping thus reducing' flow delivered to the core. Additionally, any water wst through such a postulated break would not be recoverable !
(not returned to the containment sump for continued recirculation).
However, adequate Control Room indications were available to detect such a condition and procedural guidance existed to mcnitor HPSI flow during an accident situation. Therefore, should such a rupture have-occurred, the resultant decrease in cooling water injection' flow to the ,
RCS could have been detected and the appropriate Operator, actions taken
, (i.e., close HPSI injection MOVs associated with leakpath or secure
'HPSI pump if appropriate). Therefore, the safety concerns associated 1 with this condition are considered to be minimized by these factors.
F. Additional Information
- This report is being submitted as a voluntary report to provide information obtained as a result of postulating a failure of a single component which had not previously been postulated. The condition was reviewed considering the 10CFR50.72 and 10CFR50.73 reporting criteria and not considered to be reportable to the NRC based on original plant design criteria.
Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
._m__ 'l
( ~ ~
SIT '2 -
_HPSI HEADER 1 7'
(TYP0 CAL)
( u2
_ HPSI HEADER 2 7'
g '
(TYPICAL) ncs M '
= '
/ - 2 8-18 i j(o i
asi-is ass-1s @
i
_ , _ LP. EA.E. ;
F OP (H L)@' 2Ss-14 f '@' (TYPICAL) -
(H L) i ;
i DRAW U EGEND I
i I
Q = E:ZGIE PRESSURE / I4tf PREShBE.
i h=DESIGNPRESSUREPORNPSENEADERIUPSTREANOF80095IST.,485PSIG.
h = DESIGN NOURE FOR 1sti PERESSURE SIDE IS IMO PSIG.
h = DESIGN / RESSUGE FOR IAlf PERESSUttE SIDE IS SM PSIG.
h=DESIGIEPa'?3URE IS 2368 PSIG.
h=DESIGNP9tESCUmaIS700PSIG.
NPSI = NI2 PR2SSURE SAPETY IHJBCTION.
LPSI = I4W' P9tESSURE SAFETY IIEJECTIces.
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