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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARGO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With 05000397/LER-1992-032, :on 920702,unplanned Actuation of ESF Component Occurred Due to Decrease in Reactor Water Level Resulting from Voided Feedwater Piping.Water Level Restored within Normal Operating Parameters1992-12-0303 December 1992
- on 920702,unplanned Actuation of ESF Component Occurred Due to Decrease in Reactor Water Level Resulting from Voided Feedwater Piping.Water Level Restored within Normal Operating Parameters
05000397/LER-1989-001, :on 890112,discovered Four New Unanalyzed Failure Modes in Containment Nitrogen Inerting Sys.Caused by Inadequate Design Procedures.Design Change Initiated to Install low-temp Cutoff Device1991-11-14014 November 1991
- on 890112,discovered Four New Unanalyzed Failure Modes in Containment Nitrogen Inerting Sys.Caused by Inadequate Design Procedures.Design Change Initiated to Install low-temp Cutoff Device
05000397/LER-1990-025, :on 901023,HPCS Sys Declared Inoperable.Caused by Equipment Failure.Plant Policy Reviewed,Design Differential Pressure Calculation Process Revised & Thrust Calculation HPCS-V-23 Revised1991-05-15015 May 1991
- on 901023,HPCS Sys Declared Inoperable.Caused by Equipment Failure.Plant Policy Reviewed,Design Differential Pressure Calculation Process Revised & Thrust Calculation HPCS-V-23 Revised
05000397/LER-1987-031, :on 871118,condition Prohibited by Tech Specs Not Identified When Performing Weekly Tech Spec Surveillance for Plant Batteries.Caused by Lack of Mental Attention & Poor Work Practice.Individual Counseled1987-12-18018 December 1987
- on 871118,condition Prohibited by Tech Specs Not Identified When Performing Weekly Tech Spec Surveillance for Plant Batteries.Caused by Lack of Mental Attention & Poor Work Practice.Individual Counseled
05000397/LER-1987-021, :on 870703,inadvertent Isolation of Nuclear Steam Supply Shutoff Sys Occurred.Caused by Technician Failure to Have Operations Reset half-trip Logic.Personnel Counseled Re Proper Communications W/Operations1987-08-0303 August 1987
- on 870703,inadvertent Isolation of Nuclear Steam Supply Shutoff Sys Occurred.Caused by Technician Failure to Have Operations Reset half-trip Logic.Personnel Counseled Re Proper Communications W/Operations
05000397/LER-1987-019, :on 870628,reactor Scram & Partial Containment Isolation Occurred Due to Reactor Protection Sys (RPS) Full Trip.Caused by Concurrent Component Failures in Both RPS Channels.Pressure Switch Replaced1987-07-28028 July 1987
- on 870628,reactor Scram & Partial Containment Isolation Occurred Due to Reactor Protection Sys (RPS) Full Trip.Caused by Concurrent Component Failures in Both RPS Channels.Pressure Switch Replaced
05000397/LER-1986-044, :on 861222,liquid Radwaste Effluents Discharged W/Radioactive Liquid Effluent Monitor Inoperable & Only One Predischarge Batch Sample Obtained & Analyzed.Caused by Personnel Error.Personnel Counseled1987-01-16016 January 1987
- on 861222,liquid Radwaste Effluents Discharged W/Radioactive Liquid Effluent Monitor Inoperable & Only One Predischarge Batch Sample Obtained & Analyzed.Caused by Personnel Error.Personnel Counseled
05000397/LER-1986-043, :on 861217 & 19,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal.Cause Unknown.Control Room Emergency Filtration Sys Returned to Normal Lineup1987-01-0808 January 1987
- on 861217 & 19,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal.Cause Unknown.Control Room Emergency Filtration Sys Returned to Normal Lineup
05000397/LER-1986-042, :on 861201,plant Nonconformance Rept Issued to Document Omission of Fire Door C228 from Two Surveillance Procedures.Caused by Personnel Error.Door Verified Operable & Locked & All Surveillance Procedures Checked1986-12-31031 December 1986
- on 861201,plant Nonconformance Rept Issued to Document Omission of Fire Door C228 from Two Surveillance Procedures.Caused by Personnel Error.Door Verified Operable & Locked & All Surveillance Procedures Checked
05000397/LER-1986-040, :on 861125,technicians Failed to Obtain Drywell Samples Every 12 H as Required.Caused by Failure of Personnel to Follow Procedures.Personnel Counseled1986-12-23023 December 1986
- on 861125,technicians Failed to Obtain Drywell Samples Every 12 H as Required.Caused by Failure of Personnel to Follow Procedures.Personnel Counseled
05000397/LER-1986-039, :on 861123,control Room Emergency Filtration Sys Initiated on False High Chlorine Signal.Caused by Incorrect Lamp (5.6V) Inadvertently Installed.Lamp Replaced1986-12-23023 December 1986
- on 861123,control Room Emergency Filtration Sys Initiated on False High Chlorine Signal.Caused by Incorrect Lamp (5.6V) Inadvertently Installed.Lamp Replaced
05000397/LER-1986-041, :on 861126,1202,05 & 06,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal for No Apparent Reason.Investigation of Chlorine Monitor Did Not Reveal Any Malfunctions1986-12-22022 December 1986
- on 861126,1202,05 & 06,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal for No Apparent Reason.Investigation of Chlorine Monitor Did Not Reveal Any Malfunctions
05000397/LER-1986-037, :on 861120,plant Shut Down After Connector for Signal Cable of Acoustic Monitoring Channel 5C Determined to Be Not Environmentally Qualified.Caused by Inadequate Maint Work Request.Vital Work Requests Reviewed1986-12-19019 December 1986
- on 861120,plant Shut Down After Connector for Signal Cable of Acoustic Monitoring Channel 5C Determined to Be Not Environmentally Qualified.Caused by Inadequate Maint Work Request.Vital Work Requests Reviewed
05000397/LER-1986-036, :on 861110,control Room Emergency Filtration Sys Automatically Initiated on False High Chlorine Signal. Caused by Broken chlorine-sensitive Paper Tape.Chlorine Monitor Investigated & Tape Replaced1986-12-10010 December 1986
- on 861110,control Room Emergency Filtration Sys Automatically Initiated on False High Chlorine Signal. Caused by Broken chlorine-sensitive Paper Tape.Chlorine Monitor Investigated & Tape Replaced
05000397/LER-1986-035, :on 861101 & 08,emergency Filtration Sys Initiated on High Chlorine Signal.No Root Cause Determined. Chlorine Detectors Will Be Removed After Tech Spec Approval1986-11-26026 November 1986
- on 861101 & 08,emergency Filtration Sys Initiated on High Chlorine Signal.No Root Cause Determined. Chlorine Detectors Will Be Removed After Tech Spec Approval
05000397/LER-1986-038, :on 861120,reactor Scram Occurred.Caused by Rapid Decrease in Reactor Water Level Upon Incorrect Alignment of Condensate Cleanup Block Valves & Feedwater Diversion to Empty Line.Operators Counseled1986-11-19019 November 1986
- on 861120,reactor Scram Occurred.Caused by Rapid Decrease in Reactor Water Level Upon Incorrect Alignment of Condensate Cleanup Block Valves & Feedwater Diversion to Empty Line.Operators Counseled
05000397/LER-1986-034, :on 861017,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal.No Cause Established.Tech Spec Amend Requested to Delete Chlorine Detection Requirements.W/Undated Ltr1986-11-13013 November 1986
- on 861017,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal.No Cause Established.Tech Spec Amend Requested to Delete Chlorine Detection Requirements.W/Undated Ltr
05000397/LER-1986-032, :on 861007,review of Plant Records Revealed That Control Rod Block intermediate-range Neutron Monitoring Quarterly Calibr Not Performed.Caused Insufficient Programmatic Controls.Items Now Tracked1986-11-0606 November 1986
- on 861007,review of Plant Records Revealed That Control Rod Block intermediate-range Neutron Monitoring Quarterly Calibr Not Performed.Caused Insufficient Programmatic Controls.Items Now Tracked
05000397/LER-1986-025, :on 860725,reactor High Pressure Scram Occurred During Turbine Control Operability Surveillance Test.Caused by Failed Turbine Governor Valve 4 Stem anti-rotation Device.Evaluation Continuing1986-10-27027 October 1986
- on 860725,reactor High Pressure Scram Occurred During Turbine Control Operability Surveillance Test.Caused by Failed Turbine Governor Valve 4 Stem anti-rotation Device.Evaluation Continuing
05000397/LER-1986-033, :on 861008,safety Evaluation Concluded That Cable Derating Calculations for Standby Svc Water Pump Feeders Did Not Consider Cable Routed to Duct Banks.Review on 861017 Found Addl Problems.Part 21 Related1986-10-22022 October 1986
- on 861008,safety Evaluation Concluded That Cable Derating Calculations for Standby Svc Water Pump Feeders Did Not Consider Cable Routed to Duct Banks.Review on 861017 Found Addl Problems.Part 21 Related
05000397/LER-1986-033, :on 861008,safety Evaluation Found Incorrect Sizing of Underground Cables in Duct Banks Between Main Plant & Svc Water Pumphouses.Caused by B&R Error in Cable Calculations.Also Reported Per 10CFR211986-10-13013 October 1986
- on 861008,safety Evaluation Found Incorrect Sizing of Underground Cables in Duct Banks Between Main Plant & Svc Water Pumphouses.Caused by B&R Error in Cable Calculations.Also Reported Per 10CFR21
05000397/LER-1986-031, :on 860910,RCIC Inboard Steam Line Isolation Valves Closed on Erroneous RCIC Equipment Area High Temp Signal.Caused by Technicians Inadvertently Connecting Test Equipment to Wrong Circuit.Personnel Counseled1986-10-0909 October 1986
- on 860910,RCIC Inboard Steam Line Isolation Valves Closed on Erroneous RCIC Equipment Area High Temp Signal.Caused by Technicians Inadvertently Connecting Test Equipment to Wrong Circuit.Personnel Counseled
05000397/LER-1986-030, :on 860903,reactor Scram Occurred Due to Low Reactor Water Level.Caused by Reactor Feedwater Pump Trip & Failure of Recirculation Flow Control Valve to Run Back. Preventive Maint Procedure Will Be Written1986-10-0303 October 1986
- on 860903,reactor Scram Occurred Due to Low Reactor Water Level.Caused by Reactor Feedwater Pump Trip & Failure of Recirculation Flow Control Valve to Run Back. Preventive Maint Procedure Will Be Written
05000397/LER-1986-029, :on 860822,drywell Hydrogen Analyzers Calibr Using 2% & 6% by Vol Hydrogen Gas Rather than 0% & 25% Required by Tech Specs.Caused by Personnel Error.Analyzers Recalibr.Tech Spec Amend Requested1986-09-19019 September 1986
- on 860822,drywell Hydrogen Analyzers Calibr Using 2% & 6% by Vol Hydrogen Gas Rather than 0% & 25% Required by Tech Specs.Caused by Personnel Error.Analyzers Recalibr.Tech Spec Amend Requested
05000397/LER-1986-028, :on 860819,lack of Flooding Analysis for Control Room Discovered.Caused by Error in Ae Design Control Process.Control Room Isolated & Fire Watch Initiated. Reportable Per Part 211986-09-18018 September 1986
- on 860819,lack of Flooding Analysis for Control Room Discovered.Caused by Error in Ae Design Control Process.Control Room Isolated & Fire Watch Initiated. Reportable Per Part 21
05000397/LER-1986-027, :on 860903,evaluation Concluded That Engineering Criteria Supplied by Burns & Roe,Inc,In Electrical Spec 2808-218 Nonconservative.Procedures Utilizing Faulty Data Will Be Modified1986-09-0808 September 1986
- on 860903,evaluation Concluded That Engineering Criteria Supplied by Burns & Roe,Inc,In Electrical Spec 2808-218 Nonconservative.Procedures Utilizing Faulty Data Will Be Modified
05000397/LER-1986-026, :on 860725,following Reactor Scram,Containment Isolation at RWCU Sys Actuated Due to High Differential Flow.Caused by Inadequate Design.Sys Returned to Svc in Blowdown Mode W/Reduced Blowdown Flow1986-08-22022 August 1986
- on 860725,following Reactor Scram,Containment Isolation at RWCU Sys Actuated Due to High Differential Flow.Caused by Inadequate Design.Sys Returned to Svc in Blowdown Mode W/Reduced Blowdown Flow
05000397/LER-1986-025, :on 860725,reactor High Pressure Scram Occurred During Surveillance Testing.Caused by Failure of Turbine Governor Valve 4 Stem Antirotation Device Allowing Damage to Valve Position Indicator1986-08-22022 August 1986
- on 860725,reactor High Pressure Scram Occurred During Surveillance Testing.Caused by Failure of Turbine Governor Valve 4 Stem Antirotation Device Allowing Damage to Valve Position Indicator
05000397/LER-1986-024, :on 860721,standby Diesel Generator 2 (DG2) Started.Caused by Internal Electrical Fault on One of Three Condensate Booster pumps.DG2 Secured Per Plant Procedure & Returned to Normal Backup1986-08-18018 August 1986
- on 860721,standby Diesel Generator 2 (DG2) Started.Caused by Internal Electrical Fault on One of Three Condensate Booster pumps.DG2 Secured Per Plant Procedure & Returned to Normal Backup
05000397/LER-1986-023, :on 860710,reactor Scram Occurred Following Opening of Incorrect Circuit Breaker During Electrical Ground Isolation.Caused by Personnel Error.Engineer Drawing & Circuit Breaker Labeling Will Be Changed1986-08-0101 August 1986
- on 860710,reactor Scram Occurred Following Opening of Incorrect Circuit Breaker During Electrical Ground Isolation.Caused by Personnel Error.Engineer Drawing & Circuit Breaker Labeling Will Be Changed
05000397/LER-1986-022, :on 860627,during Planned Outage While Electrical Loads Supplied by Offsite Power Source,Standby Diesel Generators Automatically Started.Caused by Momentary Loss of Power from nonplant-related Trip1986-07-21021 July 1986
- on 860627,during Planned Outage While Electrical Loads Supplied by Offsite Power Source,Standby Diesel Generators Automatically Started.Caused by Momentary Loss of Power from nonplant-related Trip
05000397/LER-1986-021, :on 860620,plant Shutdown Commenced Due to Leakage from RCS Pressure Isolation Valve Exceeding 1 Gpm. Caused by Damage to Valve Seat,Disk & Internal Surfaces from Cavitation.Valve Replaced1986-07-21021 July 1986
- on 860620,plant Shutdown Commenced Due to Leakage from RCS Pressure Isolation Valve Exceeding 1 Gpm. Caused by Damage to Valve Seat,Disk & Internal Surfaces from Cavitation.Valve Replaced
05000397/LER-1986-015, :on 860606,RWCU Sys Isolated During Leak Detection Sys Temp Indicator Calibr.Caused by Technician Incorrectly Lifting Lead.Technician Counseled & Training Package Modified to Include Calibr Procedure1986-07-10010 July 1986
- on 860606,RWCU Sys Isolated During Leak Detection Sys Temp Indicator Calibr.Caused by Technician Incorrectly Lifting Lead.Technician Counseled & Training Package Modified to Include Calibr Procedure
05000397/LER-1986-016, :on 860612,RWCU Sys Isolation Occurred.Caused by Instrument Technician Using Wrong Switch While Performing Channel Functional Test for RWCU High Delta Flow.Labels for Test Switches Will Be Improved1986-07-10010 July 1986
- on 860612,RWCU Sys Isolation Occurred.Caused by Instrument Technician Using Wrong Switch While Performing Channel Functional Test for RWCU High Delta Flow.Labels for Test Switches Will Be Improved
05000397/LER-1986-020, :on 860610,while Recovering from Overspeed Trip Test,Reactor Scrammed.Caused by Inadequate Turbine Operating Procedure.Procedure Modified to Include Addl Info Re Tv/Gv Transfer & Expected Plant Response1986-07-0909 July 1986
- on 860610,while Recovering from Overspeed Trip Test,Reactor Scrammed.Caused by Inadequate Turbine Operating Procedure.Procedure Modified to Include Addl Info Re Tv/Gv Transfer & Expected Plant Response
05000397/LER-1986-017, :on 860608,RWCU Sys Automatically Isolated Due to High Differential Flow.Caused by Personnel Error.Rwcu Sys Returned to Svc in Blowdown Mode W/Reduced Blowdown Flow.Personnel Counseled1986-07-0707 July 1986
- on 860608,RWCU Sys Automatically Isolated Due to High Differential Flow.Caused by Personnel Error.Rwcu Sys Returned to Svc in Blowdown Mode W/Reduced Blowdown Flow.Personnel Counseled
05000397/LER-1986-019, :on 860415,deficiencies Identified in RHR Valve 9 in Limitorque motor-operated Valve During Insp.Similar Environ Qualification Deficiencies Found in 27 Valves.All Deficiencies Corrected1986-07-0202 July 1986
- on 860415,deficiencies Identified in RHR Valve 9 in Limitorque motor-operated Valve During Insp.Similar Environ Qualification Deficiencies Found in 27 Valves.All Deficiencies Corrected
05000397/LER-1986-018, :on 860526 & 29,diesel Generator 2 Failed During post-mod Diagnostic Testing.Cause Undetermined. Procedure Will Be Written to Provide More Detailed Guidance Re post-mod Retesting1986-06-27027 June 1986
- on 860526 & 29,diesel Generator 2 Failed During post-mod Diagnostic Testing.Cause Undetermined. Procedure Will Be Written to Provide More Detailed Guidance Re post-mod Retesting
05000397/LER-1986-014, :on 860523,discovered That Two Containment Exhaust Purge Sys Test Connection Isolation Valves Not Tested at 24-month Interval.Caused by Personnel Error. Surveillance Procedure Modified1986-06-20020 June 1986
- on 860523,discovered That Two Containment Exhaust Purge Sys Test Connection Isolation Valves Not Tested at 24-month Interval.Caused by Personnel Error. Surveillance Procedure Modified
05000397/LER-1986-010, :on 860513,Diesel Generator 1 Fuel Storage Tank Below Min Inventory.Caused by 24 H Diesel Generator Run When Diesel Generator 2 Out of Svc.Fuel Storage Tank Filled & in Compliance1986-06-12012 June 1986
- on 860513,Diesel Generator 1 Fuel Storage Tank Below Min Inventory.Caused by 24 H Diesel Generator Run When Diesel Generator 2 Out of Svc.Fuel Storage Tank Filled & in Compliance
05000397/LER-1986-012, :on 860512,isolation Function of Nuclear Steam Supply Shutoff Sys Actuated Due to Deenergization of Reactor Protective Sys Supply Bus A.Caused by Inadequate Procedures. Inboard Isolation Valves Restored1986-06-11011 June 1986
- on 860512,isolation Function of Nuclear Steam Supply Shutoff Sys Actuated Due to Deenergization of Reactor Protective Sys Supply Bus A.Caused by Inadequate Procedures. Inboard Isolation Valves Restored
05000397/LER-1986-011, :on 860509,nuclear Steam Supply Shutoff Sys Actuated Due to Momentary Loss of Instrument Power. Cause Unknown.Reactor Protection Sys Half Scram & Isolation Signals Reset1986-06-0505 June 1986
- on 860509,nuclear Steam Supply Shutoff Sys Actuated Due to Momentary Loss of Instrument Power. Cause Unknown.Reactor Protection Sys Half Scram & Isolation Signals Reset
05000397/LER-1986-013, :on 860514,full Reactor Protective Sys Trip Occurred Due to Spurious High Signal on Neutron Monitor Trip Channel B2.Caused by Electrical Noise Generated on Power Cable Due to Welding.Procedure Revised1986-06-0505 June 1986
- on 860514,full Reactor Protective Sys Trip Occurred Due to Spurious High Signal on Neutron Monitor Trip Channel B2.Caused by Electrical Noise Generated on Power Cable Due to Welding.Procedure Revised
05000397/LER-1986-008, :on 860505,potential Transformer Secondary Fuse Blew,Resulting in Spurious Voltage Loss Signal to SM-8 Undervoltage Protection Cricuitry.Caused by Electrical Maint Technician Error.Technician Counseled1986-05-23023 May 1986
- on 860505,potential Transformer Secondary Fuse Blew,Resulting in Spurious Voltage Loss Signal to SM-8 Undervoltage Protection Cricuitry.Caused by Electrical Maint Technician Error.Technician Counseled
05000397/LER-1986-009, :on 860426,secondary Containment Sys Emergency Operation Initiated When Control Power Fuse in Reactor Bldg Ventilation High Radiation Monitoring Circuitry Blew.Cause Undetermined1986-05-23023 May 1986
- on 860426,secondary Containment Sys Emergency Operation Initiated When Control Power Fuse in Reactor Bldg Ventilation High Radiation Monitoring Circuitry Blew.Cause Undetermined
05000397/LER-1986-006, :on 860421,reactor Protective Trip Occurred During Installation of Shorting Links for Reactor Protection Sys.Caused by Operator Error,Resulting in Short Circuit. Operator Counseled & Procedure Enhanced1986-05-21021 May 1986
- on 860421,reactor Protective Trip Occurred During Installation of Shorting Links for Reactor Protection Sys.Caused by Operator Error,Resulting in Short Circuit. Operator Counseled & Procedure Enhanced
05000397/LER-1986-007, :on 860217,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal.Cause Undetermined.Method of Circulating Water Treatment Will Be Changed1986-05-15015 May 1986
- on 860217,control Room Emergency Filtration Sys Automatically Initiated on High Chlorine Signal.Cause Undetermined.Method of Circulating Water Treatment Will Be Changed
05000397/LER-1986-005, :on 860401,refueling Mode 5 Entered Prior to Completing Instrument Surveillances Required by Tech Specs. Caused by Inadequate Procedures.Tech Specs Received & Surveillances Performed1986-05-0101 May 1986
- on 860401,refueling Mode 5 Entered Prior to Completing Instrument Surveillances Required by Tech Specs. Caused by Inadequate Procedures.Tech Specs Received & Surveillances Performed
05000397/LER-1986-003, :on 860314,reactor Scram Occurred Due to Incorrect Switch Position During APRM Channel a Functional Test.Caused by Personnel Error.Technicians Counseled & Trained in Proper Actions1986-04-11011 April 1986
- on 860314,reactor Scram Occurred Due to Incorrect Switch Position During APRM Channel a Functional Test.Caused by Personnel Error.Technicians Counseled & Trained in Proper Actions
1999-10-01
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
text
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WASHINGTON PUllLIC POWER SUPPLY SYSTEM l' O. flas 968
- 3n00 George \\Yashington \\Yuv
- Hi<hland. \\Yashington 99352 Docket No.
50-397 November 14, 1991 G00-91-207 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C.
20555
Subject:
NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO. 89-001-02
Dear Sir:
Transmitted herewith is Licensee Event Report No. 89-001-02 for the HNP-2 Plant.
Inis report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrencc.
Very truly yours,
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HNP'2 Plan Man ger CMP:Ig
Enclosure:
Licensee Event Report No. 89-001-02 cc:
Mr. John B. Martin, NRC - Region V Mr. C. Sorensen, NRC Resid(nt Inspector (M/D 901A)
INPO Records Center - Atlanta, GA Ms. Dottle Sherman, ANI Mr. D.L. Hilliams, BPA (H/D 399)
NRC Resident Inspector - Halk Over Copy 1~li ?- 2.
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On January 12, 1989, during an engineering evaluation of the Containment Nitrogen inerting (CN) System, four new unanalyzed failure modes were discovered.
These fdilure modes all have the potential to impact safety reldted equipment required to attain safe shutdown of the reactor.
A summary of the failure modes is os follows:
1)
Failure Mode 1 - Loss of auxilidry steam or pressure control to the "high flow'* nitrogen line, 2)
Failure Mode 2 - A break in the " low flow" nitrogen line or loss of electric heater on the " low flow" line 3)
Failure Mode 3 - A tornado missile causes failure of liquid nitrogen storage tank and/or associated piping 4)
Failure Mode 4 - Non-mechdnistiC rupture of liquid nitrogen stordge tank or liquid lines beneath the tank.
failure Modes 1 and 2 involve potential damage to safety related compenents due to contoct with liquid nitrogen and/or low temperatures.
Failure Modes 3 and 4 involve the potential for oxygen starvation of all three divisions of emergency diesel ;enerators under certain low probability conditions, immediate corrective action was to modify procedures to require additional operator coverage and provide specific guidance to ensure correct response to failure mode conditions.
The root cause of the event was determined to be inadequate design procedures in effect at the time that this system was originally designed.
As a result of an ingineering evaluation, a design change was initiated to instdll low temperature isolation valves in both the low and high flow sides of the CN system.
This event posed no threat to the health and safety of either the public or Plant personnel.
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Event Description
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On January 12, 1989 as a result of an engineering evaluation of the Containment Nitrogen Inerting-(CN) system, four new failure modes of this non-safety related system were' identified.
This condition was discovered during performance of corrective action for-the event reported in LER 88-034-00 " Pipe failure Caused by-
[
Introduction of liquid Nitrogen into the Primary Containment Supply Purge Piping Due to Personnel / Design / Maintenance Problems"._ An engineering review of the CN System
- - design, being performed to investigate potential f ailure modes, found four new f ailure modes which could result in the degradation of safety related equiptrent as summarized below (see attached diagram figure 1):
a)-
Failure Mode 1 - Loss of auxiliary steam or nitrogen pressure control (failure of high N2 flow pressure control valve CN-PCV-6) resulting'in liquid nitrogen i-being introduced into the "high flow" Inerting header.
This header is not
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capabic of withstanding cryogenic temperatures.
i-b)
Failure Mode 2 - A break in the " low flow" line or loss of electric heater on i.
the " low flow" line when this line is supplied from the bottom of the liquid Nitrogen Tank CN-lK-1.
Again, liquid nitrogen is introduced into piping not designed for cryogenic temperatures, i
c)
Failure Mode 3 - A tornado missile that causes failure of the exposed CN-TK-1
'and associated piping outside the buildings that results in release of-large 4
quantities of liquid nitrogen which might starve the emergency diesel 4
generators of oxygen.
I d)
Failure Mode 4 - Non-mechanistic rupture of the Liquid Nitrogen Storage Tank
[
CN-TK-1-_ or the liquid lines beneath the tank that might result in oxygen starvation of the emergency diesel generators.
At 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, these new failure modes were identified as conditions which alone could have-prevented the fulfillment of the safety func tiot, of the Emergency AC
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Electrical Power Distribution System..At 1701 hours0.0197 days <br />0.473 hours <br />0.00281 weeks <br />6.472305e-4 months <br />, the NRC Operations Center was notified via the Emergency Notification System that this condition was reportable 7
under the four hour report requirement of 10CFR50.72(b)(2)(lii).
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~As'a-result of actions taken during the previous CN System event reported in-LER 88-034-00, the system operating procedure had been modified to require an operator to be stationed at the CN System skid whenever high volume containment inerting was being performed.
Guidance was glweis to the operators via night orders that the only
- - duty-of this_ additional operator was to isolate the nitrogen supply line if nitrogen effluent temperrture dropped to 30'f.
lhis action was to limit entry of liquid nitrogen into piping-not-designed for extreme low temperature use in response to failure Modes l'and 2.
Additionally, a night order was issued which requires an alarming oxygen monitor to be used whenever taking-suction with the Control Room Ventilation system from the remote air intake nearest the CN skid without use of the normal system intakes.
This measure was taken to mitigate the effects of possible reduction in oxygen content of control room air due to induction of nitrogen which potentially could be r: dased'in large quantity as a result of CN System failure in response to failure Hode 4.
Further Evaluation and Corrective Ac!lon
(
- Further Evaluation 1.
This event is being reported as an event or condition which alone could have-prevented the fulfillment of the safety function of structures or systems that are needed to :
(A)
Shut down the reactor an maintain it in a safe shutdown condition per the requirements of 10CfR50.73(a)(2)(V).
E.
1he root cause of'this event was determined to be inadequate design procedures which were in existence at the time that the Containment Nitrogen-Inerting System was originally designed.
During intial plant construction and-startup, the design procedures then in ef fect did not cause single f ailure analyses or-break pipe analyses to be performed on these types of non-safety related systems.
The CN System was not reviewed as a system which supported safety related equipment.
Also, dt that time, no piping outside the " Power Block" was considered-for analysis.
Based on this root cause, no additional corrective action is necessary.-
In light of the improvements to-the design procedures which have been made since.
that time, the probability for recurrence has already been signif icantly minimized, lhe self-initiated Safety System functional Inspection being i
performed by the Supply System Engineering Assurance Group will continue to-j
. attempt to discover additional system design deficiencies of a similar nature, i
Therefore, no additional corrective action is needed to examine other systems.
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3.
The potential for the four unanalyzed failure modes and the compensdtory I
measures presenting an unreviewed safety question was recognized.
An ar'olysis per 10CFR50.59 was completed which concluded that an unreviewed saf ety quest ion s'
did not exist.
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There were no structures, components or systems that were inoperable at the start of the event that contributed to the event.
5.
A comprehensive engineering calculation was perfornied pertaining to a non-mechanistic rupture of the Liquid Nitrogen Storage lank (f ailure Mode 4).
The results of that calculation, which was perf ornied by a contrac tor, are presented in the Safety Significance section of this LtR.
Further Corrective Actlon An Engineering evaluation was perf ormed to determine the need for design changes to the CN System. As a result of the evaluation, a de5ign change was initiated to install low temperature cut-off devices (isolat.lon valves) in both the low and high flow sides of the system.
The low temperature isolation valves have been installed in the low flow side of the system.
Installatiori of the isolation valves in the high flow side of the system is also complete; however, procedural restrictions have been established to operate the valves manually pending resolution of problems associated with the automatic actuation switches.
The isolation valves will provide adequate protection against Failure Mode 1 and 2 events by isolating the nitrogen in the storage tank any time the flowing nitrogen temperature f alls below -20*f on the high flow side and -30*F on the low flow side.
Safety Significance
Any potential for adverse safety consequences as a result of this event occurred during the time between initial startup of the CN System and the time compensatory measures were implemented.
If the low probability condition posed by f ailure Modes 1 or 2 had occurred during this period in conjuction with a Design Basis Loss of Coolant Accident (itself a low probability event), it is possible that the ability l
to shut down the reactor and maintain it in a safe shutdown condition could have t c compromised.
Neither f ailure Mode 3 nor Failure Mode 4 represents a credible
(/ent which could have occurred during this period.
Since the postulated CN System f ailure modes did not occur, no adverse safety significant consequences actually resulted.
The following is a sumri)ary of the safety significance for each postulated f ailure mode:
o failure Modes I and 2 - Both failure modes potentially could have caused piping breaks within the various rooms in the Diesel Generator and Reactor Buildings through which these lines are routed.
Consequently, the safety related equipment in these rooms (primarily emergency diesel generators and related l
components) could have been exposed to liquid nitrogen resulting in conditions beyond the design capabilities of this equipment.
Without compensatory measures applied to avert these failure modes, the resultant impact on safety related equipment could have compromised the ability of the equipment to achieve its design f unc tion.
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f ailure Mode 3 - A tornado which produces a missile suf ficient to topple arid /cr ruuture the CN Liquid Nitrogen Storage lank and associated piping would include enough wind to provide mixing and dilution to the point that the emergency diesel generators would not be starved for oxygen.
lhe ability of the reactor to achieve safe shutdown is not compromised in this failure mode, o
failure Mode 4 - In accordance with the guidelines of Standard Review Plans 3.6.1 and 3.6.2, a moderate encrgy crack was assumed to occur in the piping associated with the nitrogen tank.
The analysis completed for this event indicates that the only Plant equipment directly af f ected by the crack and subsequent nitrogen release were the three emergency diesel generators.
Dispersion analysis for the most limiting crack size could result in a loss of the three diesel generators for up to eight minutes. However, from a safe shutdown analysis perspective, this is acceptable because a loss of offsite power need not be assumed concurrent with an assumed moderate energy pipe crack if the event does not lead to a reactor scram or turbi je trip.
Because the postulated crack and resultant conserences do not result in a reactor scram or i
turbine trip, offsite power remains o.allable and reliance on the diesel generators is rat required.
The potential for the loss of nitrogen supply to indirectly cause a turbine trip or reactor scram due to loss of the nitrogen supply to the Main Steam Isolation Valves (MSIVs) was also evaluated, lhe design of the MSIV system is such that the check valves and accumulators have been shown by testing to maintain adequate nitrogen supply pressure for at least 60 minutes to hold the MSIVs open.
A loss of nitrogen pressure would also alarrii in the Control Room and operator response to such an alarm would be to line up alternate pressurized air / nitrogen supplies, thereby, preventing MSIV isolation.
As a result, the safety significance associated with this failure mode is minimal due to 1) the short time (eight minutes) the emergency diesel generators would be inoperable, 2) the design characteristics of the MSIV nitrogen supply, and 3) operator actions to prevent MSIV closure.
Accordingly, a non-mechanistic failure of the liquid nitrogen storage tank would not compromise the ability to shutdown the reactor and maintain it in a safe shutdown condition.
This event posed no threat to the health and safety of either the public or Plant personnel.
Similar Events
LER 89-001-00 and LER 89-0d1-01 l
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System Component Cohtoinment Nitrogen Inerting System LK l
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FIGURE 1 CONTAINENT NITROGEN INERTING 4
NRC Form 36CA iM93 e