05000397/LER-2002-001

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LER-2002-001,
Docket Number
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
Initial Reporting
3972002001R00 - NRC Website

Description of Event

On February 11, 2002 at 0314 Columbia Generating Station (Columbia) began planned online maintenance on Emergency Diesel Generator (EDG) 2. Maintenance was completed as scheduled. Surveillance testing to demonstrate operability of the EDG-2, and exit from the Limiting Condition of Operation (LCO), was started on February 13. Immediately after the EDG-2 output breaker was closed, the control room received an annunciator alarm. As this was not an expected alarm, the System Engineer and the Electrical Supervisor were contacted for evaluation. Further investigation revealed that the circuit breaker had closed but the Mechanism Operated Cell (MOC) switch assembly had failed to change state as expected. The circuit breaker is a Westinghouse model DHP-VR, which was installed during an upgrade process in June 2001. Columbia was at 100% power when the decision was made to shutdown the plant, due to the inability to restore EDG-2 to an Operable status within the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> completion time of TS 3.8.1 Required Action B.4. OP February 14, 2002 at 1257 the plant entered Mode 3 as required by 7'S 3.8.1.F.1. On February 15, 2002 at 0242 the plant entered Mode 4 as required by TS 3.8.1.F.2 A four hour event notification telephone call was made to the NRC Operations Center at 0418 EST on February 14, 2002 pursuant to 10 CFR 50.72(b)(2)(i) after the plant shutdown was initiated (Event Number 38694).

Immediate Corrective Actions

All Safety Related circuit breakers of the DHP-VR design and associated breaker cubicle, and other 4160 and 6900 volt breakers and their cubicles, that have an active safety function, have had preventive maintenance performed in accordance with the guidance developed by Columbia, Westinghouse, and Cutler Hammer staff. The MOC assemblies for these breaker cubicles were completely disassembled, inspected for wear, cleaned, re-greased, and worn parts were replaced as needed. The Vendor also helped to establish acceptable operating limits for the breaker applied MOC operating pin force and the MOC linkage resistance force to be used to assess the degradation rate of the breaker's MOC switch interface.

Cause of the Event

The failure of the MOC switches to fully actuate was excessive resistance in the pantograph assembly due to a lack of preventive maintenance. The root cause was the failure to recognize the sensitivity of the new breakers to the importance of MOC assembly maintenance. During the last refueling outage that ended July 2, 2001, 22 obsolete magnetic air DHP type breakers were replaced with vacuum element DHP-VR type breakers. The original DHP breakers 968-26158 RI (9/01)

Assessment of Safety Consequences

An evaluation was performed of the period of time from when the DHP-VR breakers were installed until the plant was shutdown as a result of this event. There was no time at which any of the affected systems were called ,ipon where they were unable to perform their required safety functions; therefore there were no safety consequences. Actuation force analysis performed on the MOC switch assemblies subsequent to plant shutdown showed that the reduced breaker applied force would not have resulted in a loss of any safety function.

Actions to Prevent Recurrence Additional corrective actions include establishing the preventive maintenance frequency and scope of work for the MOC switches, MOC switch linkage, and pantograph channels of all the 4160 VAC and 6900 VAC cubicle switchgears. A plant procedure will be revised to include lubrication and maintenance instructions for the pantograph and MOC linkage assemblies. The Circuit Breaker Program will be enhanced to provide guidance on circuit breaker and cell maintenance.

Previous Similar Events

Three previous similar events have been identified. Two cases were intermittent, could not be repeated, and both occurred in the same cubicle. In the first instance the cause was degradation in the MOC switch linkages. Corrective actions were to inspect all cubicles with the 22 DHP-VR type breakers installed and change the procedural guidance to lubricate the MOC switches that are in the DHP type switchgears.

In the second case, looseness with side-to-side movement in the pantograph was the cause.

Generic MOC linkage maintenance was a concern and corrective action was initiated to evaluate the preventive maintenance program for 211 MOC linkages and pantograph assemblies.

However this action was not scheduled to be complete on all 22 breakers until Jul:, 1, 2002.

The third case that occurred on January 17, 2002, was an unexpected alarm in the control room of a breaker trip that immediately cleared. The breaker functioned correctly and did not trip. The system engineer was concerned and a work order was initiated to address the failure, but the February 13, 2002 failure occurred before the work order was worked.

50-397