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similar to the condition noted in IE Information Notice 84-90, non-conservative assump-tions were found in the Reactor Core Isolation Cooling (RCIC) and Reactor Water Cleanup (RWCU) High Energy Line Break (HELB) calculations which determined the Reactor Building environmental profiles used in determining equipment qualification per 10CFR50.49.
Further analysis has determined that correction of these non-conservative assumptions did result in predicted environmental conditions more severe than those used in the equipment qualification.
However, a review of the equipment involved has determined that required equipment could be qualified or justified for interim operation to the more severe conditions, and that mitigation of the event and safe shutdown would not be compromised.
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Plant Conditions
a) Plant Mode 1
b) Power Level 98%
Event On January 11, 1985, based on Supply System review of an independent consultant's calc-ulations, it was determined that a 10CFR21 condition existed due to non-conservative engineering assumptions associated with calculating the environmental profiles used to qualify Reactor Building equipment per 10CFR50.49.
The Supply System has identified non-conservative assumptions concerning 1) response times for Leak Detection System (LD) temperature detectors that were used and, 2) the use of saturated fluid conditions rather than subcooled fluid conditions for blowdown analysis following a line break.
The Supply System has determined that this event resulted because an adequate system level review was not performed, nor adequate valve closure operating times established, when the environmental qualification profiles were established.
Initial Corrective Action o
Prior to January 15, 1985, valve stroke times for the DC powered outboard RWCU and RCIC isolation valves were adjus.ted to provide isolation within time frames that preserve existing environmental profiles, o
During an unscheduled outage on January 31, 1985, the AC powered inboard RWCU and RCIC isolation valves were adjusted to provide isolation within the stroke time necessary to preserve the environmental profiles that had been used in equipment quali fication.
o The Supply System on February 1,1985, completed an evaluation to assess the pos-sible consequences of the non-conservative assumptions on the qualification of equipment identified in the Justification for Interim Operation (JIO) Table A pro-vided in the referenced transmittal.
This evaluation concluded that equipment could be qualified to the more severe environmental profiles and that the required safe shutdown path was'not compromised.
o The independent consultant, Impe11, Corp., was notified on January 22,1985, that the Supply System considers this event reportable per 10CFR21.
The Supply System presently has no knowledge of other plants where these non-conservative assumptions may have been applied during the equipment qualification process.
The independent consultant has expressed an interest in assisting the Supply System in correcting the documentation errors associated with the deficiency.
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Final Corrective Action A plant modification is scheduled to modify the motor operator of the inboard and out-board valves to eliminate the need for blocking the valves in a partially closed posi-tion.
Safety Significance
An evaluation has been completed to 1) assess the consequences of the non-conservative assumptions on the RCIC and RWCU HELB environmental profiles used in equipment qualifi-cation, and 2) assess the affect of the more severe profiles on the equipment required to mitigate the event and achieve safe shutdown.
This analysis was based on the fol-lowing key assumptions which are consistent with BTP ASB 3-1.
o RCIC and RWCU isolation valve closure speeds were based on existing Technical Specification limits.
Single active component failure of the faster of the inboard or outboard valve was assumed.
The limiting valve in both systems is the inboard AC powered valve.
o Loss of off-site power was assumed for the RWCU line breaks because direct actua-tion of the RPS, and hence turbine generator loss, may occur.
Off-site power is available for the RCIC breaks until operator action is taken to shutdown the Plant since no RPS actuation is postulated.
Since RCIC line isolation occurs within 30 seconds, AC power would be available to complete system isolation, but not to miti-gate the Reactor Building break zone environmental transient.
A sensitivity evaluation of the RWCU HELB environmental profiles considering both avail-ability and unavailability of AC power was conducted.
It was found that maximum break zone environmental conditions were not significantly affected by including additional diesel generator start time (10 sec.) delays in the profile calculations.
Therefore, the most severe postulated environmenal conditions, i.e., AC unavailable, were used in the RWCU HELB equipment qualification review.
The sensitivity of the RCIC HELB envi-ronmental profiles to AC power availability was also reviewed.
The profiles developed show loss of AC power would result in more severe environmental profiles.
- However, since no direct RPS actuation mechanistically results from the RCIC HELBs, AC power is available to terminate the mass energy release from the postulated pipe breaks.
The resulting environmental profiles were then used to determine, per the requirements of 10CFR50.49, if the equipment necessary to achieve one path to shutdown (JIO Table A) could be qualified to the more severe environmental profiles.
In summary, it was found that all equipment identified on JIO Table A could either be qualified to the more severe postulated environmental profiles, was not needed to miti-gate the event or achieve safe shutdown, or has been justified for interim operation without qualification per 10CFR50.49(i).
Based on this evaluation, it was concluded that the Plant was operating in a safe manner subsequent to the discovery of the defi-ciency reported on January 11 and prior to the January 31 unscheduled outage during which the AC powered inboard RCIC/RWCU isolation valves were blocked partially shut.
Blocking the valves ) reserves the environmental profiles that were and are being used in equipment qualificat on.
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No additional report will be submitted.
Similar Event Refer to 10CFR50.55(e) report #287, dated 10-28-83.
Reference G02-83-590, G.D.
Bouchey to A.
Schwencer, Nuclear Project No.
2, Justification for Interim Operation, June 30, 1983.
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Washington Public Power Supply System P.O. Box 968 3000 GeorgeWashington Way Richland, Washington 99352 (509)372-5000 Docket No. 50-397 March 8, 1985 Director Office of Inspection and Enforcement U.S. Nuclear Regulatory Connission Washington, D.C.
20555 Subject: NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO. 85-001-01
Dear Sir:
Transmitted herewith is Licensee Event Report No. 85-001-01 for WNP-2 Plant.
This report is submitted to provide supplementary information to Licensee Event Report No.85-001 with regard to corrective action.
Very truly yours, hk aw.4 J. D. Martin ( /D 927M)
WNP-2 Plant Manager JDM:mm
Enclosure:
Licensee Event Report No. 85-001-001 (3 copies) cc: Mr. John B. Martin, NRC - Region V Document Control Desk - NRC Mr. A. D. Toth, NRC - Site (901 A)
Ms. Dottie Sherman, ANI INPO Records Center - Atlanta, GA
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| 05000397/LER-1985-001, :on 850111,existence of 10CFR21 Condition Determined Due to Nonconservative Engineering Assumptions Associated W/Calculating Environ Profiles Used to Qualify Reactor Bldg Equipment |
- on 850111,existence of 10CFR21 Condition Determined Due to Nonconservative Engineering Assumptions Associated W/Calculating Environ Profiles Used to Qualify Reactor Bldg Equipment
| | | 05000397/LER-1985-002, :on 850101,lockout Relays 86XU & 86XUOA Tripped Main Generator/Turbine at BPA Substation & Resulted in Reactor Scram.Caused by Failed Potential Transformer |
- on 850101,lockout Relays 86XU & 86XUOA Tripped Main Generator/Turbine at BPA Substation & Resulted in Reactor Scram.Caused by Failed Potential Transformer
| | | 05000397/LER-1985-003-01, :on 850125,erroneous 500-kV Circuit Breaker Open Position Signal Received.Turbine Governor Valves Automatically Closed,Resulting in Reactor Scram.Caused by Disturbance in Microwave Link |
- on 850125,erroneous 500-kV Circuit Breaker Open Position Signal Received.Turbine Governor Valves Automatically Closed,Resulting in Reactor Scram.Caused by Disturbance in Microwave Link
| | | 05000397/LER-1985-003, Forwards LERs 85-003 & 85-004 Submitted on 850131 W/O Appropriate Signatures.W/O LER 85-003 | Forwards LERs 85-003 & 85-004 Submitted on 850131 W/O Appropriate Signatures.W/O LER 85-003 | | | 05000397/LER-1985-004-01, :on 841226,discovered That Weekly Surveillance of Fire Pump Batteries Not Completed within Scheduled Maint Sys Time Limit.Fire Pump Battery Found to Be within Spec. Event Determined Reportable on 850116 |
- on 841226,discovered That Weekly Surveillance of Fire Pump Batteries Not Completed within Scheduled Maint Sys Time Limit.Fire Pump Battery Found to Be within Spec. Event Determined Reportable on 850116
| 10 CFR 50.73(a)(2)(1) | | 05000397/LER-1985-004, :on 850116,determined That 841226 Discovery of Failure to Perform Weekly Fire Pump Battery Surveillance Reportable.Caused by Deficiency in Program Scheduling. Surveillance Scheduling Procedures Revised |
- on 850116,determined That 841226 Discovery of Failure to Perform Weekly Fire Pump Battery Surveillance Reportable.Caused by Deficiency in Program Scheduling. Surveillance Scheduling Procedures Revised
| 10 CFR 50.73(a)(2)(1) | | 05000397/LER-1985-007, :on 850131,one Generator Primary Protection Lockout Relay,Spuriously Tripped Causing Abnormal Electrical Operations.Caused by 500 Kv Breakers Opening & Causing Overspeed Condition |
- on 850131,one Generator Primary Protection Lockout Relay,Spuriously Tripped Causing Abnormal Electrical Operations.Caused by 500 Kv Breakers Opening & Causing Overspeed Condition
| | | 05000397/LER-1985-008, :on 850131,standby Electrical Diesel Generators Did Not Reach Required Voltage for Closure of Output Breakers.Caused by Procedural Error.Control Circuitry Modified.Procedures Changed |
- on 850131,standby Electrical Diesel Generators Did Not Reach Required Voltage for Closure of Output Breakers.Caused by Procedural Error.Control Circuitry Modified.Procedures Changed
| | | 05000397/LER-1985-009, :on 850119,reactor Water Cleanup Sys Isolated. Caused by Spurious Reactor Water Cleanup Sys High Flow Trip. Isolation Signals Reset |
- on 850119,reactor Water Cleanup Sys Isolated. Caused by Spurious Reactor Water Cleanup Sys High Flow Trip. Isolation Signals Reset
| | | 05000397/LER-1985-010, :on 850127,reactor Water Cleanup Sys Isolation Occurred.Caused by Spurious Reactor Water Cleanup Sys High Delta Flow Trip.Isolation Signals Reset |
- on 850127,reactor Water Cleanup Sys Isolation Occurred.Caused by Spurious Reactor Water Cleanup Sys High Delta Flow Trip.Isolation Signals Reset
| | | 05000397/LER-1985-011, :on 850203,two 3/4-inch Drain Lines Observed W/Slight Leakage.Caused by Low Load High Cycle Fatigue.Lines Repaired,Per ASME Section XI Procedures |
- on 850203,two 3/4-inch Drain Lines Observed W/Slight Leakage.Caused by Low Load High Cycle Fatigue.Lines Repaired,Per ASME Section XI Procedures
| | | 05000397/LER-1985-012, :on 850212,during Reactor Bldg Ventilation Sys Maint,Reactor Water Cleanup Sys Isolation Occurred.Caused by Pipe Routing in Area Causing High Temp Trip.Heating & Ventilation Sys Procedures Revised |
- on 850212,during Reactor Bldg Ventilation Sys Maint,Reactor Water Cleanup Sys Isolation Occurred.Caused by Pipe Routing in Area Causing High Temp Trip.Heating & Ventilation Sys Procedures Revised
| | | 05000397/LER-1985-013, :on 850214,reactor Protection Sys Actuation Occurred.Caused by Failure to Properly Reset Half Scram Condition Prior to Proceeding W/Surveillance Testing.Scram Reset & Surveillance Testing Continued |
- on 850214,reactor Protection Sys Actuation Occurred.Caused by Failure to Properly Reset Half Scram Condition Prior to Proceeding W/Surveillance Testing.Scram Reset & Surveillance Testing Continued
| | | 05000397/LER-1985-014, :on 850214,high Pressure Reactor Scram Initiated Due to Actuation of Turbine Bypass Valve 7 Inches Mercury Low Condenser Vacuum Interlock.Normal Scram Recovery Procedures Followed |
- on 850214,high Pressure Reactor Scram Initiated Due to Actuation of Turbine Bypass Valve 7 Inches Mercury Low Condenser Vacuum Interlock.Normal Scram Recovery Procedures Followed
| | | 05000397/LER-1985-015, :on 850213,fire Detection Instrument Discovered to Have Been Removed from RHR Valve Room During Plant Mod. from 840909-850213 No Fire Detection or Fire Watch Patrol Monitored RHR Valve Room |
- on 850213,fire Detection Instrument Discovered to Have Been Removed from RHR Valve Room During Plant Mod. from 840909-850213 No Fire Detection or Fire Watch Patrol Monitored RHR Valve Room
| | | 05000397/LER-1985-016, :on 850213,reactor Scrammed & HPCS Sys Automatically Initiated.Caused by Incorrect Differential Pressure Instrument Being Valved Into Svc.Instruments Verified for Proper Calibr |
- on 850213,reactor Scrammed & HPCS Sys Automatically Initiated.Caused by Incorrect Differential Pressure Instrument Being Valved Into Svc.Instruments Verified for Proper Calibr
| | | 05000397/LER-1985-017, :on 850214,temp Monitor in Leak Detection Sys Covering Reactor Water Cleanup Pump Room 1 Spuriously Actuated Delta Temp High Alarm,Initiating Signal to Close Outboard Containment Isolation Valve |
- on 850214,temp Monitor in Leak Detection Sys Covering Reactor Water Cleanup Pump Room 1 Spuriously Actuated Delta Temp High Alarm,Initiating Signal to Close Outboard Containment Isolation Valve
| | | 05000397/LER-1985-018, :on 850224,containment Monitoring Sys Temp Indicator Exceeded 150 F for Greater than 8 H.Caused by Circulating Water Sys Cooling Towers Alternately Being Taken Out of Svc for Electrical Repairs |
- on 850224,containment Monitoring Sys Temp Indicator Exceeded 150 F for Greater than 8 H.Caused by Circulating Water Sys Cooling Towers Alternately Being Taken Out of Svc for Electrical Repairs
| | | 05000397/LER-1985-019, :on 850216,temp Monitoring of RHR Pump Room Areas Not Accomplished in Accordance W/Tech Specs.Caused by Incorrect Transference of Instructions from Plant Procedure Deviation to Actual Procedure Used on 850216 |
- on 850216,temp Monitoring of RHR Pump Room Areas Not Accomplished in Accordance W/Tech Specs.Caused by Incorrect Transference of Instructions from Plant Procedure Deviation to Actual Procedure Used on 850216
| | | 05000397/LER-1985-020, :on 850227,four Excess Flow Check Valve Bypasses Found Partially Opened While Performing Field Measurements Required to Generate Design Change Package. Probably Caused by Personnel Error |
- on 850227,four Excess Flow Check Valve Bypasses Found Partially Opened While Performing Field Measurements Required to Generate Design Change Package. Probably Caused by Personnel Error
| | | 05000397/LER-1985-021, :on 850307,reactor Recirculation Flow Control Valve B Hydraulic Power Unit (HY-HP-3B) Tripped Off & Valves HY-V-17B,18B,19B,20B,33B,34B,35B & 36B Closed. Investigations Yielded No Apparent Cause |
- on 850307,reactor Recirculation Flow Control Valve B Hydraulic Power Unit (HY-HP-3B) Tripped Off & Valves HY-V-17B,18B,19B,20B,33B,34B,35B & 36B Closed. Investigations Yielded No Apparent Cause
| | | 05000397/LER-1985-022, :on 850307,two HPCS Initiation Status Lamps Damaged During Process of Replacing Nameplate Tags on Control Room Panel P-625.HPCS Sys Automatic Initiation Logic Rendered Inoperable While Bulbs Replaced |
- on 850307,two HPCS Initiation Status Lamps Damaged During Process of Replacing Nameplate Tags on Control Room Panel P-625.HPCS Sys Automatic Initiation Logic Rendered Inoperable While Bulbs Replaced
| | | 05000397/LER-1985-025, :on 850404,operations Failed to Notify Chemistry Lab When Transferring Drywell Purge Operation from Standby Gas Treatment Sys to Reactor Bldg Ventilation Sys.Caused by Personnel Error |
- on 850404,operations Failed to Notify Chemistry Lab When Transferring Drywell Purge Operation from Standby Gas Treatment Sys to Reactor Bldg Ventilation Sys.Caused by Personnel Error
| | | 05000397/LER-1985-027, :on 850412,automatic Isolation of Div 1 balance-of-plant Relay Cabinet Occurred.Caused by Inadequate Procedure.Logic Reset.Surveillance Procedures Revised.W/ |
- on 850412,automatic Isolation of Div 1 balance-of-plant Relay Cabinet Occurred.Caused by Inadequate Procedure.Logic Reset.Surveillance Procedures Revised.W/
| | | 05000397/LER-1985-028, :on 850426,unsealed Penetration in Reactor Bldg Fire Barrier Floor Discovered.Caused by Failure to Install Fire Seal During Const.Hourly Fire Watch Patrol Placed on Penetration Until Seal Installation Completed |
- on 850426,unsealed Penetration in Reactor Bldg Fire Barrier Floor Discovered.Caused by Failure to Install Fire Seal During Const.Hourly Fire Watch Patrol Placed on Penetration Until Seal Installation Completed
| | | 05000397/LER-1985-029, :on 850503,control Rods Inserted Until 15% Power Obtained When Rod Sequence Control Sys Failed to Automatically Initiate to Enforce Predetermined Control Rod Programming at 20% Rated Thermal Power |
- on 850503,control Rods Inserted Until 15% Power Obtained When Rod Sequence Control Sys Failed to Automatically Initiate to Enforce Predetermined Control Rod Programming at 20% Rated Thermal Power
| | | 05000397/LER-1985-030, :on 850507,while Returning RHR Loop a to ECCS Lineup,Reactor Protection Sys Actuation Occurred.Caused by Simultaneous Opening of Valves RHR-V-6A & RHR-V-4A,causing Reactor Pressure Vessel Water Level Decrease |
- on 850507,while Returning RHR Loop a to ECCS Lineup,Reactor Protection Sys Actuation Occurred.Caused by Simultaneous Opening of Valves RHR-V-6A & RHR-V-4A,causing Reactor Pressure Vessel Water Level Decrease
| | | 05000397/LER-1985-031, :on 850508,during Surveillance of Main Steam Line Hi Radiation,Reactor Protection Sys a & B Placed Simultaneously in Trip Condition.Caused by Spurious Noise Spikes.Surveillance Procedures Modified |
- on 850508,during Surveillance of Main Steam Line Hi Radiation,Reactor Protection Sys a & B Placed Simultaneously in Trip Condition.Caused by Spurious Noise Spikes.Surveillance Procedures Modified
| | | 05000397/LER-1985-032, :on 850418,required 18-month Surveillance Tests Found Not Performed on Some Output Signals from Reactor Vessel Water Level lo-lo Instruments.Level 2 & High Drywell Procedures Deficient from 831220-850419 |
- on 850418,required 18-month Surveillance Tests Found Not Performed on Some Output Signals from Reactor Vessel Water Level lo-lo Instruments.Level 2 & High Drywell Procedures Deficient from 831220-850419
| 10 CFR 50.73(a)(2)(1) | | 05000397/LER-1985-033, :on 850525,noise Spike in Intermediate Range Monitor Channels Resulted in Reactor Protection Sys Actuation.Caused by Movement of Intermediate Range Monitor by Water Spray.Caution Signs to Be Put in Area |
- on 850525,noise Spike in Intermediate Range Monitor Channels Resulted in Reactor Protection Sys Actuation.Caused by Movement of Intermediate Range Monitor by Water Spray.Caution Signs to Be Put in Area
| | | 05000397/LER-1985-034, :on 850525,inadvertent ESF Injection to Reactor Pressure Vessel Occurred During Cold Shutdown.Caused by Faulty Logic seal-in Lamp Indication.Procedural Changes Made to Identify Logic Status More Positively |
- on 850525,inadvertent ESF Injection to Reactor Pressure Vessel Occurred During Cold Shutdown.Caused by Faulty Logic seal-in Lamp Indication.Procedural Changes Made to Identify Logic Status More Positively
| | | 05000397/LER-1985-035, :on 850531,diesel Fuel Oil Supply Line on Engine 1 Developed Leak & Diesel Manually Shut Down by Operator.Caused by Broken Copper Tubing in Fuel Line.Faulty Line Replaced & Other Fuel Oil Lines Inspected |
- on 850531,diesel Fuel Oil Supply Line on Engine 1 Developed Leak & Diesel Manually Shut Down by Operator.Caused by Broken Copper Tubing in Fuel Line.Faulty Line Replaced & Other Fuel Oil Lines Inspected
| | | 05000397/LER-1985-036, :on 850601,control Room Emergency Filtration Unit Started.Caused by First Trip Not Being Reset After Testing.Step to Verify Reset Status Independent of Operator Action Added |
- on 850601,control Room Emergency Filtration Unit Started.Caused by First Trip Not Being Reset After Testing.Step to Verify Reset Status Independent of Operator Action Added
| | | 05000397/LER-1985-037, :on 850609,two Circuit Breakers Discovered Inoperable During Scheduled Maint Outage of 4160-volt safety-related Switchgear.Caused by Failure of Spot Welded Pivot Pin.Part 21 Related |
- on 850609,two Circuit Breakers Discovered Inoperable During Scheduled Maint Outage of 4160-volt safety-related Switchgear.Caused by Failure of Spot Welded Pivot Pin.Part 21 Related
| | | 05000397/LER-1985-038, :on 850607,insp of Itt General Hydromotor Valve Actuators Revealed 11 Missing Stiffner Plates.Caused by Removal of Plates During Const.Stiffner Plates Reinstalled |
- on 850607,insp of Itt General Hydromotor Valve Actuators Revealed 11 Missing Stiffner Plates.Caused by Removal of Plates During Const.Stiffner Plates Reinstalled
| | | 05000397/LER-1985-039, :on 850606,normal Tech Spec Change Request Initiated Re Fuse Size Listing Due to Discovery of Errors in Listing.On 850614,util Notified of Need for NRC Approval Before Resuming Operation.Approval Obtained |
- on 850606,normal Tech Spec Change Request Initiated Re Fuse Size Listing Due to Discovery of Errors in Listing.On 850614,util Notified of Need for NRC Approval Before Resuming Operation.Approval Obtained
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000397/LER-1985-040, :on 850606,two Reactor Protection Sys Actuations Occurred.Caused by Reactor Recirculation Sys Pump 1B Testing Evolution.Temporary Reactor Recirculation Sys Pump 1B Testing Procedure Canceled |
- on 850606,two Reactor Protection Sys Actuations Occurred.Caused by Reactor Recirculation Sys Pump 1B Testing Evolution.Temporary Reactor Recirculation Sys Pump 1B Testing Procedure Canceled
| | | 05000397/LER-1985-041, :on 850618,Channel B Logic Input to Main Turbine & Feedwater Turbine B Did Not Respond.Caused by Cable Not Reconnected Following Replacement & Rerouting During Startup Test Program.Cable Terminated |
- on 850618,Channel B Logic Input to Main Turbine & Feedwater Turbine B Did Not Respond.Caused by Cable Not Reconnected Following Replacement & Rerouting During Startup Test Program.Cable Terminated
| | | 05000397/LER-1985-042, :on 850621,primary Containment Valve in Traversing in-core Probe Purge Line Identified to Be in Noncompliance W/License Commitments.Redesign Prepared & Implemented.Further Investigation Underway |
- on 850621,primary Containment Valve in Traversing in-core Probe Purge Line Identified to Be in Noncompliance W/License Commitments.Redesign Prepared & Implemented.Further Investigation Underway
| | | 05000397/LER-1985-043, :on 850619,during Fire Barrier Surveillance, Connection Box,Conduit & Two Cables Found W/Missing Thermolag Fire Protective Coating.Barriers Not Installed During Initial Const.Fire Watch Established |
- on 850619,during Fire Barrier Surveillance, Connection Box,Conduit & Two Cables Found W/Missing Thermolag Fire Protective Coating.Barriers Not Installed During Initial Const.Fire Watch Established
| | | 05000397/LER-1985-044, :on 850628,fuel Oil Intended for Use in Auxiliary Boilers Inadvertently Added to Standby Diesel Generator Fuel Oil Storage Tanks.Caused by Personnel Error. Storage Tanks Sampled & Analyzed |
- on 850628,fuel Oil Intended for Use in Auxiliary Boilers Inadvertently Added to Standby Diesel Generator Fuel Oil Storage Tanks.Caused by Personnel Error. Storage Tanks Sampled & Analyzed
| | | 05000397/LER-1985-045, :on 850625,automatic Reactor Water Cleanup Sys Isolation Occurred While Repressurizing Demineralizer B After Completion of Backwash & Precoat.Caused by Air in Sensing Lines of Flow Instrumentation |
- on 850625,automatic Reactor Water Cleanup Sys Isolation Occurred While Repressurizing Demineralizer B After Completion of Backwash & Precoat.Caused by Air in Sensing Lines of Flow Instrumentation
| | | 05000397/LER-1985-046, :on 850629,reactor Manually Scrammed & Main Turbine Manually Tripped.Caused by Fire in Reactor Feedwater Pump 1B While Remaining Pump Secured for Maint.Fire Extinguished,Plant Shut Down & Pump Repaired |
- on 850629,reactor Manually Scrammed & Main Turbine Manually Tripped.Caused by Fire in Reactor Feedwater Pump 1B While Remaining Pump Secured for Maint.Fire Extinguished,Plant Shut Down & Pump Repaired
| | | 05000397/LER-1985-047, :on 850701,discovered That One Reactor Protection Sys Relay for Turbine Throttle Valve Not Energized When Open.Scram Occurred During Valve Reset.Caused by Limit Switch Failure.Switches Recalibr |
- on 850701,discovered That One Reactor Protection Sys Relay for Turbine Throttle Valve Not Energized When Open.Scram Occurred During Valve Reset.Caused by Limit Switch Failure.Switches Recalibr
| | | 05000397/LER-1985-048, :on 850702,discovered Suppression Pool Not Adequately Refilled After Recent Mod.Cause Unstated.Level Transmitters Vented,Refilled & Recalibr.Pool Level Restored to Normal Levels |
- on 850702,discovered Suppression Pool Not Adequately Refilled After Recent Mod.Cause Unstated.Level Transmitters Vented,Refilled & Recalibr.Pool Level Restored to Normal Levels
| | | 05000397/LER-1985-049, :on 850720,core Pressure Drop Baseline Data Not Obtained While Increasing Power Above 50% Rated Core Thermal Power in Single Recirculation Loop Operation.Power Reduced to Thermal Power Limit for Data |
- on 850720,core Pressure Drop Baseline Data Not Obtained While Increasing Power Above 50% Rated Core Thermal Power in Single Recirculation Loop Operation.Power Reduced to Thermal Power Limit for Data
| | | 05000397/LER-1985-050, :on 850723,during 18-month Surveillance on Cable Spreading Room pre-action Fire Protection Sprinkler, Solenoid Valve Controlling Flow to Sprinkler Header Did Not Open.Cause Unstated.Valve Repaired |
- on 850723,during 18-month Surveillance on Cable Spreading Room pre-action Fire Protection Sprinkler, Solenoid Valve Controlling Flow to Sprinkler Header Did Not Open.Cause Unstated.Valve Repaired
| | | 05000397/LER-1985-051, :on 850722,incorrect Values for Single Loop Operation Used in Aprm,Reactor Protection Sys Thermal Power Trip Calibr Procedure.Caused by Failure to Perform Calibr W/ Latest Approved Procedure.Values Reset |
- on 850722,incorrect Values for Single Loop Operation Used in Aprm,Reactor Protection Sys Thermal Power Trip Calibr Procedure.Caused by Failure to Perform Calibr W/ Latest Approved Procedure.Values Reset
| | | 05000397/LER-1985-052, :on 850801,discovered Procedure Deviation Issued on 850608 Incorrectly Changed Containment Isolation Valve Closure Time.Procedure Mod Issued |
- on 850801,discovered Procedure Deviation Issued on 850608 Incorrectly Changed Containment Isolation Valve Closure Time.Procedure Mod Issued
| | | 05000397/LER-1985-053, :on 850804,reactor Scram Occurred During Instrument Surveillance of ATWS Recirculation Pump Trip Feature.Caused by Faulty Instrument Isolation Valve.Valve Replaced & Training Program Implemented |
- on 850804,reactor Scram Occurred During Instrument Surveillance of ATWS Recirculation Pump Trip Feature.Caused by Faulty Instrument Isolation Valve.Valve Replaced & Training Program Implemented
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