05000293/LER-2003-003, Regarding Automatic Scram Resulting from Load Rejection at Full Power Due to Transformer Fault

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Regarding Automatic Scram Resulting from Load Rejection at Full Power Due to Transformer Fault
ML032180736
Person / Time
Site: Pilgrim
Issue date: 07/29/2003
From: Balduzzi M
Entergy Nuclear Operations
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
2.03.089 LER 03-003-00
Download: ML032180736 (7)


LER-2003-003, Regarding Automatic Scram Resulting from Load Rejection at Full Power Due to Transformer Fault
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(1)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function
2932003003R00 - NRC Website

text

Entergy Entergy Nuclear Operations, Inc.

Pilgrim Nuclear Power Station 600 Rocky Hill Road Plymouth, MA 02360 Michael A. Balduzzi Site Vice President July 29, 2003 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 Subject Entergy Nuclear Operations, Inc.

Pilgrim Nuclear Power Station Docket No. 50-293 License No. DPR-35 Licensee Event Report 2003-003-00 Letter Number:

2.03.089

Dear Sir:

The enclosed Licensee Event Report (LER) 2003-003-00, 'Automatic Scram Resulting from Load Rejection at Full Power due to Transformer Fault," is submitted in accordance with 10 CFR 50.73 This letter contains no commitments.

Please feel free to contact me if there are any questions regarding this subject.

Sincerely, i/

> g/,Z, Michael A. Balduzzi DWE/dd cc:

Mr. Hubert J. Miller Regional Administrator, Region 1 U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. Travis Tate Project Manager Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission 1 White Flint North Mail Stop: 0-8B-1 11555 Rockville Pike Rockville, MD 20555-001 Senior NRC Resident Inspector INPO Records IC__

1.

NRC Form 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104

, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection.

FACILITY NAME (1)

DOCKET NUMBER (2)

PAGE(3)

PILGRIM NUCLEAR POWER STATION 05000-293 1 of 6 TITLE (4)

Automatic Scram Resulting from Load Rejection at Full Power due to Transformer Fault EVENT DATE (5[

LER NUMBER (6)

REPORT DATE OTHER FACILITIES INVOLVED 8)

MONTH DAY EAR YAR ISEQUENTAL NUMBER IRxEVISION FACaurY NAME DOCKET NumBER Mot~m DAY YEAR YE AR NUMBER MONTH DAY YEAR N/A 05000 FACauY NAME DOCKET NUMBER 06 01 2003 2003 003 00 07 29 2003 N/A 05000 OPERATING THIS REPORT IS SUBMlTrED PURSUANT TO THE REQUIREMENTS OF 10 CFR: (Check on or more) (11)

MIODE (9)

N 20.2201(b) 22.2203(a)(3)(1) 50.73(a)(2)(1)(C) 50.73(a)(2)(vii)

POWER 1

22.2202(d) 20.2203(a)(3)(1i) 50.73(a)(2)(i1)(A) 50.73(a)(2)(vlil)(A)

LEVEL (1) 100 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(3)(1)0)(A) 50.73(a)(2)(1ii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(ii) 50.36(3)(1)(ii)(A)

X 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)ofl)

=

50.36(c)(2)

=

50.73(a)(2)(v)(A)

=

73.71(aX4) 20 2203(a)(2)(Xv) 50.46(a)(3)(_i) 50.73(a)(2)(.)

v)(B)

I_ 73.71(aX) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)

OTHER 20.2203(a)(2)(v) 50.73(a)(2W)(B) 50.73(a)(2)(v)(D)

Specify in Abstract below or in NRC Form 366A LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER (include Area Code)

Bryan Ford - Licensing Manager 508-830-8403 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

REPORTABLE l

I REPORTABLE

CAUSE

SYSTEM COMPONENT IMANUFACTURERl TORTABL I-P CAUSE SYSTEM COMPONENT MANUFACTURER RTOEPIX X

EA XMFR W120 V

I tC0:OEN TO SUPPLEMENTAL REPORT EXPECTED (141)

EXPECTED MONTH DAY YEAR YES I

X I NO I

SUBMISSION

(

QlyescompleteEXPECTEDSUBMISSIONDATE) l DATE(15) l ABSTRACT (Limit to 1400 spaces i.e., apprordmately 15 singe-spaced typewritten fines) (16)

On June 1, 2003 an unplanned automatic scram occurred while at 100% reactor power. The scram was the result of a load rejection. Automatic responses included the insertion of all withdrawn control rods, transfer of the source of electrical power for Pilgrim's 4.16 kV auxiliary power distribution system (APDS),

closure of the turbine steam control and stop valves, trip of the turbine, opening of the turbine steam bypass valves, and opening of main steam relief valves for pressure relief.

The direct cause of the scram was the automatic closing of the turbine control valves. The direct cause of the event was an electrical fault in the unit auxiliary transformer (UAT) that was powering the APDS at the time of the event. The fault was the result of the failure of a conductor within the low voltage portion of the UAT (X-winding).

Corrective actions taken included a temporary alteration for powering the APDS during power operation.

Corrective actions planned include the repair or replacement of the unit auxiliary transformer.

The event posed no threat to public health and safety.

NRC FORM 366

NRC Forw 366A U.S. NUCLEAR REGULATORY COMMISSION

' NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKETNUMBER 2 LER NUMBER 6 PAG l

SEQUENTIAL l REVISION l YEAR I NUMBER l NUMBER PILGRIM NUCLEAR POWER STATION 05000293 2003 003 00 2o EXT (if more space Is required, use additional copies of NRC Form 366A) (17)

BACKGROUND The preferred offsite power source for Pilgrim Station is the 345 kV transmission lines 342 and/or 355 via the Startup Transformer. The secondary offsite power source is the 23 kV distribution system via the Shutdown Transformer.

During power operation when the Main Transformer is energized by the Main Generator, the Pilgrim Station 4.16 kV auxiliary power distribution system (APDS) is normally powered from the Unit Auxiliary Transformer.

The APDS provides power to nonsafety-related and safety related loads. The nonsafety-related electrical loads are powered from 4.16 kV Buses Al through A4 and the respective 480 volt load centers and motor control centers. The safety-related electrical loads are powered from 4.16 kV Buses AS and/or A6 and the respective 480 volt load centers and motor control centers.-

During plant shut down conditions when the 345 kV transmission lines are energized, the APDS is powered from the 345 kV transmission system by the Startup Transformer via the respective 345 kV switchyard circuit breakers. During plant shut down conditions when the 345 kV lines are not energized, the safety-related 4.16 kV Buses (A5/A6), and respective load centers and motor control centers, are designed to be powered by the respective emergency diesel generator (EDG 'A'/EDG 'B') or the 23 kV distribution system via the Shutdown Transformer (Buses A5 and/or A6) or the Station Blackout Diesel Generator (Bus AS or Bus A6).

Just prior to the event the following conditions existed. The preferred and secondary offsite power sources were energized, the switchyard ringbus was intact, the EDGs and the Station Blackout Diesel Generator were in standby service. The Main Transformer was energized by the Main Generator with the APDS being powered from the Main Transformer via the Unit Auxiliary Transformer (UAT). The reactor was operating at 100% power (1998 MWt) with the reactor mode selector switch in the RUN position. The reactor vessel pressure was normal, about 1035 psig, with the reactor water at the saturation temperature for that pressure. The reactor water level was normal, at about +26" (narrow range).

EVENT DESCRIPTION

On June 1, 2003 at about 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br />, an unplanned automatic reactor protection system scram signal and scram occurred while at 100% reactor power (1998 MWt). The scram signal resulted in the automatic insertion of the control rods that were in a withdrawn position at the time of the event. The reactor core display panel and the plant computer (EPIC) call-rods function indicated all control rods were fully inserted.

The scram signal was initiated by the closing of the turbine steam control valves. The closing of the turbine steam stop valves also resulted in an automatic scram signalU.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

SEQUENTIAL REVISION YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000293 2003 003 00 3of 6 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

The event was initiated by a trip of the unit auxiliary transformer (UAT) differential relay that resulted in a trip of the main generator lockout relay. The trip of the lockout relay included the automatic transfer of the source of 4.16 kV power for the APDS from the UAT to the Startup Transformer, automatic opening of the 345 kV switchyard circuit breakers that connect the main transformer to the switchyard, automatic opening of the main generator field breaker, and automatic trip of the master trip solenoid (MTS-1) that is part of the turbine mechanical-hydraulic control system.

The trip of MTS-1 included the automatic closing of the turbine steam control valves and stop valves.

Collectively, the three turbine steam bypass valves have a capacity for diverting 25% of the rated main steam flow to the main condenser. The steam flow from the reactor vessel exceeded the capacity of the bypass valves and the consequence was the expected, relatively rapid increase in the reactor vesselmain steam pressure.

The reactor vessel pressure increase and insertion of the control rods each contributed to a decrease in the reactor water void fraction (shrink). The decrease in the void fraction resulted in a decrease in the reactor water level. The reactor water level decreased to about -10" (narrow range). The decrease in reactor water level, to less than the low water level setting of about +12" (narrow range), resulted in the expected automatic actuation of the Primary Containment Isolation Control System [(PCIS Groups 2 (Sampling System) and 6 (Reactor Water Cleanup System)] and Reactor Building Isolation Control System (RBIS).

Meanwhile, the pressure increase resulting from the closing of the turbine steam valves (control valves and stop valves) resulted in the automatic opening of three of the four main steam relief valves for the pressure relief function. Post trip review verified each relief valve that actuated demonstrated a normal opening and reseat within the valves' specification and that the response of all four relief valves was in accordance with design.

After the main steam relief valves closed, the turbine steam bypass valves provided the reactor/main steam pressure control function.

The operation of the bypass valves resulted in a gradual decrease in the reactor vessel pressure and consequent increase in the reactor water void fraction (swell). The maximum reactor water level that occurred was about +52". The high pressure coolant injection (HPCI) system turbine control system received a trip signal as a result of the high water level condition. The HPCI high water level trip function is nonsafety-related, functions to protect the HPCI turbine from water, and can be manually reset when the reactor water level is less than the trip setting or Is automatically reset if a reactor water low-low level condition occurs.

The high water level condition also resulted in an automatic close signal to the normally closed reactor core isolation cooling (RCIC) system turbine steam supply valve. The high water level closing function for the valve is nonsafety-related, functions to protect the RCIC turbine from water. The valve can be manually opened when the reactor water level is less than the high water level setting or is automatically opened if a reactor water low-low level condition occurs. The RCIC turbine steam supply valve remained closed as designed.

NRC Farm 366A U.S. NUCLEAR REGULATORY COMMISSION NRC Formn 366A U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKETNUMBER 2 LER NUMBER (6l PAG SEQUENTIAL REVISION YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000 293 2003 003 0

4c TEXT (If more space Is required, use aditonal copies of NRC Form 366A) (17)

Control room licensed operator response to the event included the following. The full insertion of the control rods was verified. The PCIS and RBIS actuations were verified. A reactor water level band of 20" to 40" was established by 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br />.

The HPCI turbine high water level trip was manually reset at 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br />.

The NRC Operations Center was notified of the event In accordance with 10 CFR 50.72 at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on June 1, 2003.

CAUSE

The direct cause of the scram was the automatic closing of the turbine control valves. The closing of the turbine control valves (and stop valves) was the result of the automatic actuation of the turbine master trip solenoid (MTS-1). The trip of MTS-1 was the result of the automatic trip of the generator lockout relay. The trip of the lockout relay was the result of the automatic trip of the UAT differential relay. The trip of the differential relay was the result of an electrical fault in the UAT.

The direct cause of the event was the failure of the conductor that connects to the phase A' of the UAT (X-winding). The failure was internal to the transformer. The UAT phase 'A' winding powers the phase

'A' portion of Pilgrim's 4.16 kV APDS. The UAT was installed during original plant construction (C. 1970).

The UAT is a three phase, oil-cooled, 60 Hz, type SL power transformer manufactured by the Westinghouse Electric Corporation. The nameplate data is as follows: Serial Number RCR-23161, Class OANFANFDA, Insuldur insulation, L. Spec. 874190, (primary) 23000 volts Delta winding (H winding),

(secondary) 4160/2400 volts Wye winding (X-winding, Y-winding), 5-position load tap changer. Tap number 4 was the working tap position at the time of the fault.

CORRECTIVE ACTION

Corrective actions taken included the following:

The Pilgrim Station electrical system was aligned such that the APDS is powered from the Startup Transformer during power operation, pending repair or replacement of the Unit Auxiliary Transformer.

The Unit Auxiliary Transformer was disconnected and shipped offsite for evaluation and repair or replacement.

Corrective actions planned include the following:

Repair or replacement of the Unit Auxiliary Transformer.

Review of a vendor evaluation to establish additional actions necessary for early detection to eliminate the potential of a future failure of the UAT.

NRC Form-366A U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER 2 LER NUMBER 6 PAGE 3 SEQUENTIAL REVISION YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 2003 003 00 5 of 6 TEXT (If more space Is required, use additional copies of NRC Form 366A) (17)

SAFETY CONSEQUENCES

The event posed no threat to public health and safety.

The maximum reactor power experienced during the event was about 101% and decayed as expected.

The plant systems responded as designed to the transient. The preferred and secondary sources of offsite power remained energized. The EDGs and Station Blackout Diesel Generator remained available during the event. The Core Standby Cooling Systems (HPCI System, Automatic Depressurization System, Residual Heat Removal System, Core Spray System) and the RCIC System remained available during the event to provide makeup water or core cooling if necessary.

The maximum reactor pressure that occurred was less than the Technical Specification limit including tolerance for the relief valves and safety valves. The response of the main steam relief valves was in accordance with design. The opening or one or more relief valves is an expected occurrence resulting from a load rejection at 100% power.

The minimum reactor water level that occurred was about -10" (narrow range). The level was above the low-low water level (about -46") for automatic actuation of the Core Standby Cooling Systems and

- automatic actuation of the Group I portion of the PCIS. The level was also above the level (about -127")

corresponding to the top of the active fuel zone.

REPORTABILITY

This report was submitted in accordance with 10 CFR 50.73(a)2)(iv) because the actuation of the RPS was not planned.

SIMILARITY TO PREVIOUS EVENTS A review was conducted of Pilgrim Station Ucensee Event Reports (LERs) submitted since 1984. The review identified previous scrams resulting from load rejections but identified no previous events that were caused by the Unit Auxiliary Transformer. The review Identified two similar LERs. LER 89-010-00 reported a failure (fault) of one of the feeder cables that connect the Startup Transformer to the APDS; the failure occurred while shut down when the SUT was powering the APDS and was caused by cable jacket damage during original construction installation (c. 1970). LER 97-004-01 reported a failure (fault) of the Main Transformer that occurred while the transformer was powering the APDS, in a backfeed configuration, while shut down; the failure was caused by a degraded transformer winding condition or static electrification.U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER 2 LER NUMBER (6)

PAGE (3) l I

I SEQUENTIAL REVISION 1 YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 2003 003 00 6 of 6 TEXT (If more space Is required, use additional copies of NRC Form 366A) (17)

ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for the report are as follows:

COMPONENTS CODES Circuit Breaker, AC 52 Relay, Differential, Protective 87 Relay, Locking-Out 86 Solenoid (MTS-1)

SOL Transformer (UAT)

XMFR Valve (Control, Stop, Bypass)

V Valve, Relief (RV-203-3A/B/CID)

RV SYSTEMS Engineered Safety Features Actuation EA (RPS, PCIS, RBIS)

High Pressure Coolant Injection BJ Main Generator Output EL Main Steam SB Medium Voltage Power EA Switchyard FK Turbine Steam Bypass Control Jil