05000272/LER-1981-086, Forwards LER 81-086/03L-0.Detailed Event Analysis Encl

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Forwards LER 81-086/03L-0.Detailed Event Analysis Encl
ML20031D995
Person / Time
Site: Salem PSEG icon.png
Issue date: 10/02/1981
From: Midura H
Public Service Enterprise Group
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20031D996 List:
References
NUDOCS 8110140442
Download: ML20031D995 (3)


LER-1981-086, Forwards LER 81-086/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
2721981086R00 - NRC Website

text

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I LER O PSEG Public Service Electric and Gas Company P.O. Box 168 Hancocks Bridge, New Jersey 08038 Salem Generating Station October 2, 1981

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Q Mr.

R. C. Haynes g

Director of USNRC

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g'(J=

g Office of Inspection and Enforcement Region 1

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[E'.. OCT131%> I 631 Park Avenue King of Prussia, Pennsylvania 19406 4

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Dear Mr. Haynes:

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he LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-86/03L Pursuant to the requirements of Salem Generating Station Unit No.

1, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 81-86/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

& wy H.

J. Midura General Manager -

Salem Operations CC:

R.

A Uderitz General Manager - Nuclear Production Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies)

SPhl 8110140442 811002 J

PDR ADOCK 05000272 S

PDR The Energy People 9s 2is9 n2.sw i t e

Report Number:

81-86/03L Report Date:

10-2-81 Occurrence Date:

9-9-81 and 9-25-81 Facility:

Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 1

IDENTIFICATION OF OCCURRENCE:

i No. 11 Containment Fan Coil Unit - Inoperable.

This report was initiated by Incident Reports81-369 and 81-389.

CONDITIONS PRIOR TO OCCURREhCE:

9-9-81 Mode 1 - Rx Power 96% - Unit Load 1000 MWe 9-15-81 Mode 1 - Rx Power 95% - Unit Load 1040 MWe DESCRIPTION OF OCCURRENCE:

On two separate occasions, September 9, 1981 and September 25, 1981, No. 11 Containment Fan Coil Unit (CFCU) indicated a no service trater i

flow condition.

On both occasions No. 11 CFCU_was declared inoperable, and at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> and 1902 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.23711e-4 months <br />, respectively, action statement 3.6.2.3.a was entered.

This occurrence constituted operation in a degraded mode in accordance with technical specification 6.9.1.9.b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

On both occasions the cause of the no flow indication was the flow transmitter was plugged with silt.

ANALYSIS OF OCCURRENCE:

i Action statement 3.6.2.3.a requires:

With one group of containment cooling fans inoperable and both Containment Spray Systems operable, restore the inop-erable group of cooling fans to operable status within 7 days or be in at least hot standby within the next-6 hours and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />..

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l LER 81-86/03L -

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CORRECTIVE ACTION

I On each occasion the flow transmitter was blown down to remove the silt, and tested satisfactorily.

At 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br />, September 9,

1981, and 0210 hours0.00243 days <br />0.0583 hours <br />3.472222e-4 weeks <br />7.9905e-5 months <br />, September 26, 1981, No. 11 CFCU was declared operable and action statement 3.6.2.3.a was terminated.

A program is in effect to blow down all transmitters every two weeks.

However, this program is presently being recycluated in an effort to increase it's effectiveness.

FAILURE DATA:

Fischer and Porter Co.

Differential - Pressure Flow Transmitter l

Model 10B2495 jj

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1 Prepared By F.

Dickey r/,* <

(%V Mana'ger - Salem Generating Station j

SORC Meeting No.81-100 i

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