Similar Documents at Salem |
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LER-1981-072, Forwards LER 81-072/01T-0.Detailed Event Analysis Encl |
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GEk OPSEG
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1 Public Service Electric and Gas Con.; any 80 Park Plaz Newark, N.J. 07101 Prune 201/430-7000 August 27, 1981 Mr. Boyce H. Grier kp Director of USNRC Office of Inspection and Enforcement 1
Region 1
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I lU 631 Park Avenue
,N King of Prussia, Pennsylvania 19406 6
SEP 0 C 19815 73
Dear Mr. Grier:
Y2 D
LICENSE NO. DPR-70 i
DOCKET NC. 50-272 b
REPORTABLE OCCURRENCE 81-72/0lT Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 81-72/0lT.
This report is required within fourteen (14) days of the occurrence.
Sincerely yourc,
/[
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R. A. Uderit/
General Manager -
Nuclear Production CC:
Director, Office of Inspection and Enforcement (40 copies)
Director, Office of Management Information and Program Control
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(3 copies)
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8109040205 810827
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gDRADOCK 05000272 Ine enesyfDL,,
c2001 (400M) 1-81 L
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LER 81-72/0lT August 27, 1981 ANALYSIS OF OCCURRENCE:
Technical specification 3.6.2.3.a requires with:
One group of containment cooling fans inoperable and both Containment Spray Systems operable, restore the inoperable group of cooling fans to operable status within 7 days or be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Technical specification 3.6.2.3.b requires with:
Two groups of containment cooling fans inoperable, and both l
Containment Spray Systems operable, restore at least one group of cooling fans to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or i
be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Restore both groups of cooling fans to operable status within 7 days of initial loss or be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown withi.. Lha following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
CORRECTIVE ACTION
The fourth secondary cooling coil from the top on No. 14 CFCU and the bottom primary coil on No. 12 CFCU were isolated from the remainder of the coils by installing blank flange inserts between the service water inlet and outlet flanges.
As per engineering analysis, it is possible to isolate an individual cooler like this while retaining acceptable efficiency of the cooler.
These coolers will be replaced during the next scheduled outage; however, no supplementary report will be issued.
Action statement 3.6.2.3.a was terminated at 2125 hours0.0246 days <br />0.59 hours <br />0.00351 weeks <br />8.085625e-4 months <br /> on August 13,.981.
Action statement 3.6.2.3.b was terminated at 0510 hours0.0059 days <br />0.142 hours <br />8.43254e-4 weeks <br />1.94055e-4 months <br /> on August 14, 1981.
FAILURE DATA:
Westinghouse Coil Cooler Spin No. RCMECP Prepared By J.
Varga
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Manager - SalemiGenerating Station SORC Meeting No.
81-77
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Report Number:
81-72/0lT l
1 Report Date:
August 27, 1981 Occurrence Date:
8-13-81 Facility:
Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Containment Fan Coil Units (CFCU) - Servisa Water Leaks.
This report was initiated by Incident Reports81-327 and 81-328.
L CONDITIONS PRIOR TO OCCURRENCE:
t Mode 1 - Rx Power 95% - Unit Load 1030 MWe DESCRIPTION OF OCCURRENCE:
During the 0800-1600 shift on August 13, 1981, during a routine containment inspection, an operator discovered a service water leak of approximately 1 gallon per minute emanating from a pin point hole on the fourth secondary cooling coil from the top, on the No. 14 CFCU.
In accordance with NRC IE Bulletin 80-24, the NRC was notified i
of the service water leak by telephone with written notification made the following day.
No. 14 CFCU was removed from service and the service water isolated.
Action statement 3.6.2.3.a was entered at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br /> August 13, 1981, after declaring the CFCU inoperable due to service water isolation.
During the 1600-2400 shift on August 13, 1981, during a routine containment inspection, an operator discovered a service water leak.
of approximately.75 gallons per minute emanating from the bottom primary cooling coil on the No. 12 CFCU.
The NRC was again notified at 1923 hours0.0223 days <br />0.534 hours <br />0.00318 weeks <br />7.317015e-4 months <br /> and written notification was made the following day.
No. 12 CFCU was removed from service and the service water isolated.
I i
Action statement 3.6.2.3.b was entered at 1920 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.3056e-4 months <br /> on August 13, 1981, after declaring the CFCU inoperable since both No. 14 and 12 CFCU were inoperable.
These occurrences constituted operation in a degraded mode in accord-an.e with technical specification 6.9.1.9.b.
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f DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
l l
Equipment failure.
The fourth secondary cooling coil from the top on No. 14 CFCU had developed a pin point hole.
The bottom primary cooling coil on the No. 12 CFCU had developed a leak.
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| 05000311/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001-03, /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | | | 05000311/LER-1981-001-03, /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | | | 05000311/LER-1981-002, Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-002-03, /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | | | 05000272/LER-1981-002-03, /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | | | 05000272/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000311/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-003-03, Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | | | 05000272/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000272/LER-1981-003-03, /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | | | 05000311/LER-1981-004-04, /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | | | 05000311/LER-1981-004, Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000272/LER-1981-004-03, /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | | | 05000311/LER-1981-005-03, /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | | | 05000311/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-005-03, /03L-0:on 810128,during Routine Functional Test on Reactor Protection Sys,Safety Injection Signal Failed.Caused by Comparator Unit (Hagan Model 4111082-001) Failure. 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Caused by Worn Main Shaft Packing.Packing Replaced | /03L-0:on 810426,during Mode 3 Operations,Svc Water Pump 23 Declared Inoperable Due to Packing Leaks. Caused by Worn Main Shaft Packing.Packing Replaced | | | 05000311/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000272/LER-1981-010-03, /03L-0:on 810126,containment Fan Coil Unit 11 Declared Inoperable in Order to Replace Leaking Spool Piece in Svc Water Line.Due to Reactor Trip,Fan Coil Unit Had to Be Tested & Declared Operational | /03L-0:on 810126,containment Fan Coil Unit 11 Declared Inoperable in Order to Replace Leaking Spool Piece in Svc Water Line.Due to Reactor Trip,Fan Coil Unit Had to Be Tested & Declared Operational | | | 05000272/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000311/LER-1981-011-03, /03L-0:on 810427,during Routine Entry Into Containment,Containment Airlock Outer Door Would Not Close. Caused by Out of Alignment Linkage & Subsequent Roller Bearing Damage.Linkage Realigned & Roller Bearings Replaced | /03L-0:on 810427,during Routine Entry Into Containment,Containment Airlock Outer Door Would Not Close. Caused by Out of Alignment Linkage & Subsequent Roller Bearing Damage.Linkage Realigned & Roller Bearings Replaced | | | 05000311/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000272/LER-1981-011-03, /03L-0:on 810127,svc Water Line to Containment Fan Coil Unit 11 Found Leaking.Caused by Leaking Weld Connecting Spool Piece to Valve 11SW57.Weld Reworked & Spool Piece Replaced | /03L-0:on 810127,svc Water Line to Containment Fan Coil Unit 11 Found Leaking.Caused by Leaking Weld Connecting Spool Piece to Valve 11SW57.Weld Reworked & Spool Piece Replaced | | | 05000272/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000272/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000272/LER-1981-012-03, /03L-0:on 810204,fire Pump 2 in Fire Suppression Water Sys Declared Inoperable for Maint on Leaking Inlet Cooling Water Line.Caused by Leaking Corrugated Stainless Steel Hose Connecting Common Cooling Water Piping | /03L-0:on 810204,fire Pump 2 in Fire Suppression Water Sys Declared Inoperable for Maint on Leaking Inlet Cooling Water Line.Caused by Leaking Corrugated Stainless Steel Hose Connecting Common Cooling Water Piping | | | 05000311/LER-1981-012-03, /03L-0:on 810427,during Surveillance Procedure Sp(O) 4.6.1.3 on Containment Air Lock,Leak Rate Exceeded Tech Specs.Caused by Inability of Inner Door Seals to Maintain Test Pressure.Seals Replaced | /03L-0:on 810427,during Surveillance Procedure Sp(O) 4.6.1.3 on Containment Air Lock,Leak Rate Exceeded Tech Specs.Caused by Inability of Inner Door Seals to Maintain Test Pressure.Seals Replaced | | | 05000311/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000311/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000311/LER-1981-013-03, /03L-0:on 810501,during Scheduled Type B & C Leakage Tests,Leak Rate Was Greater than Max Range of Volumetric Test Equipment.Caused by Use of Limited Range Equipment.Valves Adjusted & Airlock Door Seals Reworked | /03L-0:on 810501,during Scheduled Type B & C Leakage Tests,Leak Rate Was Greater than Max Range of Volumetric Test Equipment.Caused by Use of Limited Range Equipment.Valves Adjusted & Airlock Door Seals Reworked | | | 05000272/LER-1981-013-03, /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable Due to Leak in Pump Oil Cooler.Oil Cooler Replaced | /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable Due to Leak in Pump Oil Cooler.Oil Cooler Replaced | |
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