07-28-2006 | On May 31, 2006, at approximately 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> ( CDT), with Unit 2 at approximately 100 percent power, Dresden Nuclear Power Station Engineering and Operations personnel reviewed the equipment history of the Unit 2 Reactor Steam Dome Pressure-Low Permissive Switch and concluded that previous failures of the switch to pass the Technical Specification Allowable Value in 2004, 2005 and 2006 might have incorrectly assumed that the failures occurred at the time of discovery. A further evaluation was conducted which provided firm evidence that the historical failures should have been classified as a failure to meet the Technical Specifications Allowable Value for a period that exceeded Allowed Outage Times. These events are being reported in accordance with 10 CFR 50.73(a)(2)(i)(B), "Any operation or condition which was prohibited by the plant's Technical Specifications.
The apparent cause of the switch failures was a knowledge-based awareness by technicians performing the calibration of the switches that using smaller step changes during calibration can result in improved accuracy of the setpoint. Corrective actions include training of technicians on the technique to be used in calibrating this switch and changes to the calibration procedure. |
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LER-2006-003, Unit 2 Reactor Steam Dome Pressure-Low Permissive Switch Determined To Have Been Historically InoperableDocket Number |
Event date: |
05-31-2006 |
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Report date: |
07-28-2006 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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2372006003R00 - NRC Website |
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Dresden Nuclear Power Station (DNPS) Unit 2 is a General Electric Company Boiling Water Reactor with a licensed maximum power level of 2957 megawatts thermal. The Energy Industry Identification System codes used in the text are identified as [XX].
A. Plant Conditions Prior to Event:
Unit: 02 � Event Date: 05-31-2006 Reactor Mode: 1 � Mode Name: Power Operation � Power Level: 100 percent Reactor Coolant System Pressure: 1000 psig
B. Description of Event:
On May 31, 2006, at approximately 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> (CDT), with Unit 2 at approximately 100 percent Reactor Steam Dome Pressure-Low permissive switch "B", PS 2-0263-52B [69]. The permissive switch has two internal micro switches. One micro switch is connected to the Core Spray System (CS) [BM] logic circuit and the other micro switch is connected to the Low Pressure Coolant Injection System (LPCI) [BO] logic circuit. The permissive switch's as-found setting of one or both micro switches had been below the Technical Specification (TS) Allowable Value during previous TS surveillance testing. The TS Allowable Value is less than or equal to 308.5 pounds per square inch gauge (psig) and the dates the surveillance tests were found below their required value were May 3, 2004, January 18, 2005, July 20, 2005, October 18, 2005, January 20, 2006 and April 19, 2006. At the time of each event, the failure cause could not be determined and was assumed to have occurred at the time of discovery.
On May 31, 2006, Engineering and Operations personnel concluded that previous failures of the permissive switch to pass the TS Allowable Value in 2004, 2005 and 2006 might have incorrectly assumed that the failures occurred at the time of discovery based on the failure history. A further evaluation was conducted which concluded that the cause of the permissive switch historic failures was the result of a knowledge-based awareness by technicians performing the calibration of the switches that using smaller step changes during calibration can result in improved accuracy of the setpoint. The TS surveillance failures were classified as failures to meet the TS Allowable Value for a period that exceeded the TS Allowed Outage Time based on the firm evidence provided in this evaluation.
These events are being reported in accordance with 10 CFR 50.73(a)(2)(i)(B), "Any operation or condition which was prohibited by the plant's Technical Specifications.
C. Cause of Event:
The apparent cause of the switch failures was a knowledge-based awareness by technicians performing the calibration of the switches that using smaller step changes during calibration can result in improved accuracy of the setpoint.
Reactor Steam Dome Pressure-Low permissive switch "B" has two micro switches (i.e., SW-1 and SW-2) inside, with both set at 336 psig. The permissive switch is a mechanical design with shoulders on cams activating the two micro switches at the setpoint. With both micro switches, SW-1 and SW- 2, having the same setpoint, the two micro switch mechanisms interact with each other. Therefore, adjustments to one micro switch may affect the setting of the other micro switch.
After each of the TS surveillance failures identified above, the micro switch appeared to operate as designed and was capable of being reset to the TS Allowable Value. Additionally, when permissive switches that failed the TS surveillance were tested by other facilities, the switches produced acceptable and repeatable results. As a result of this, the causes of the TS surveillance failures were indeterminate and were assumed to have occurred at time of discovery.
The evaluation conducted after May 31, 2006 focused on the possible causes of the historic failure rate. The evaluators reviewed the permissive switch manufacturer's recommendations contained in `ITT Barton Models 288A and 290A/B Differential Pressure Indicating Switches Installation and Operation Manual." The manufacturer advised in the manual that small step changes be used to calibrate and test the switch. Additionally, the manufacturer recommended smaller step changes be used if improved accuracy is needed. The use of small step changes and the rate at which pressure is changed, were left to the skill of the craft.
The DNPS evaluators reviewed the overall performance of DNPS technicians in calibrating various plant instruments and determined their performance to be satisfactory. DNPS technicians were requested to perform a calibration of the permissive switch specifically using the vendor recommended small step and rate changes. The permissive switch performed as designed and was capable of meeting TS surveillance requirements. The evaluation reviewed the training and the existing plant procedure, DIS 1500-01, "Reactor Low Pressure (350 PSIG) ECCS Permissive," used to calibrate the permissive switch. It was identified that both did not adequately address the vendor's recommendations for switch calibration to use small step and rate changes to calibrate and test the switch. DNPS's program incorrectly relied too heavily upon the skill of the craft for the calibration of these micro switches, which have unusual sensitivity to calibration technique. These deficiencies resulted in poor setpoint repeatability and the historic TS Allowable Value failures.
Additionally, the evaluation conducted after May 31, 2006, reviewed the cause of why the issue of repeat failures of the Unit 2 Reactor Steam Dome Pressure-Low permissive switch "B," was not evaluated previously. In May 2000, DNPS approved for site use procedure ER-AA-520, "Instrument Performance Trending," Revision 0. Additionally, in July 2002, DNPS approved for site use procedure ER-AA-2030, "Conduct of Plant Engineering Manual," Revision 0. The procedures implemented an instrument trending program for DNPS Engineering personnel that divided the responsibility of equipment trending between Design and Plant Engineering personnel. A review of the implementation of these procedures discovered that procedure responsibilities assigned to Plant Engineering personnel were not being implemented as required. This was the major contributor for the failure to perform an earlier evaluation of the repeat failures of the Unit 2 Reactor Steam Dome Pressure-Low permissive switch "B.
D. Safety Analysis:
The safety significance of the event is minimal. Unit 2 Reactor Steam Dome Pressure-Low permissive switch "A", PS 2-0263-52A, was operable and capable of permitting the safety function of the CS and LPCI to be performed when switch "B", PS 2-0263-52B, was assumed to be inoperable.
Additionally, Unit 2 Reactor Steam Dome Pressure-Low permissive switch "B" would have functioned to permit the operation of the CS and LPCI but at a lower pressure than allowed by TS and assumed in accident analyses (i.e., approximately 40 psig). Therefore, the consequences of this event had minimal impact on the health and safety of the public and reactor safety.
E. Corrective Actions:
The Unit 2 Reactor Steam Dome Pressure-Low permissive switch "B" calibration was performed and confirmed acceptable on June 2, 2006, prior to its scheduled quarterly test frequency.
The frequency of performing the quarterly TS Surveillance on Unit 2 Reactor Steam Dome Pressure- Low permissive switch "B" has been reduced to 31 days to confirm the actions being taken to correct the calibration issue.
A training package will be prepared for DNPS instrument technicians to provide enhanced training in calibrating the Reactor Steam Dome Pressure-Low permissive switch. The training will be implemented during the next instrument training cycle.
The apparent cause of the failure to adequately calibrate the Reactor Steam Dome Pressure-Low permissive switch will be reviewed with instrument maintenance personnel and the method to be used during the calibration will be re-enforced with the personnel.
Procedure DIS 1500-01 will be revised to include additional guidance on calibrating the Reactor Steam Dome Pressure-Low permissive switch.
A training package will be prepared for Plant Engineering personnel on their procedural responsibilities as described in procedure ER-AA-520. Additionally, all Plant System Manager and First Line Supervisors will review ER-AA-520 and ER-AA-2030, and affirm their understanding of procedural requirements for monitoring, trending and identification of recurring instrumentation problems.
F. Previous Occurrences:
A review of DNPS Licensee Event Reports (LERs) for the last three years identified six LERs associated with training or procedure issues.
of Instrument Sensing Lines." The LER identified inadequate procedure guidance in backfilling instrument sensing lines.
Subsequent Discovery Of Inoperability Of The Units 2 And 3 High Pressure Coolant Injection System." The LER identified inadequate procedure guidance for swapping the Main Turbine lube oil coolers.
Damper Failure To Close." The LER identified inadequate procedure guidance contained on an enclosed figure use to restore the system after a temporary modification.
The Standby Gas Treatment System For Units 2 And 3." The LER identified an inadequate leak rate test procedure that permitted a degraded Secondary Containment boundary to be undetected.
inadequate procedure direction for placing the detector in its penetration.
In Mode 2." The LER identified inadequate procedure controls for ensuring needed valve positions in Mode 2.
G. Component Failure Data:
NA
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05000305/LER-2006-010 | | | 05000456/LER-2006-001 | Unit 1 Reactor Coolant System Pressure Boundary Leakage Due To Inter-Granular Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000454/LER-2006-001 | Technical Specification Required Action Completion Time Exceeded for Inoperable Containment Isolation Valves Due to Untimely Operability Determination | | 05000423/LER-2006-001 | Loss Of Safety Function Of The Control Room Emergency Ventilation System | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000369/LER-2006-001 | Ice Condenser and Floor Cooling System Containment Isolation Valve inoperable longer than allowed by Technical Specification 3.6.3. | | 05000353/LER-2006-001 | HPCI Ramp Generator Signal Converter Failure | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000352/LER-2006-001 | Loss Of One Offsite Circuit Due To Invalid Actuation Of Fire Suppression System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2006-001 | | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | 05000316/LER-2006-001 | Failure to Comply with Technical Specification 3.6.2, Containment Air Locks | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2006-001 | Plant Shutdown Required by Technical Specification Action 3.6.5.B.1 | | 05000293/LER-2006-001 | | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000289/LER-2006-001 | | | 05000287/LER-2006-001 | Actuation of Emergency Generator due to Spurious Transformer Lockout | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000251/LER-2006-001 | Turkey Point Unit 4 05000251 1 OF 6 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2006-001 | Manual Reactor Trip Due to Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to Personnel Error | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2006-001 | Incorrect Wiring in the Remote Shutdown Panel Results in a Fire Protection Program Violation | | 05000413/LER-2006-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000368/LER-2006-001 | Completion of a Plant Shutdown Required by Technical Specifications Due to Loss of Motive Power to Certain Containment Isolation Valves as a Result of a Phase to Ground Short Circuit in a Motor Control Cubicle | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000306/LER-2006-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000298/LER-2006-001 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000286/LER-2006-001 | I | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000282/LER-2006-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000266/LER-2006-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000261/LER-2006-001 | Manual Reactor Trip Due to Failure of a Turbine Governor Valve Electro-Hydraulic Control Card | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000255/LER-2006-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000461/LER-2006-002 | Turbine Bypass Function Lost Due to Circuit Card Maintenance Frequency | | 05000458/LER-2006-002 | Loss of Safety Function of High Pressure Core Spray Due to Manual Deactivation | | 05000456/LER-2006-002 | Units 1 and 2 Entry into Limiting Condition for Operation 3.0.3 due to Main Control Room Ventilation Envelope Low Pressure | | 05000443/LER-2006-002 | Noncompliance with the Requirements of Technical Specification 6.8.1.2.a | | 05000387/LER-2006-002 | DMissed Technical Specification surveillance requirement | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000362/LER-2006-002 | Unit 3 Shutdown to Inspect Safety Injection Tank Spiral Wound Gaskets | | 05000336/LER-2006-002 | Manual Reactor Trip Due To Trip Of Both Feed Pumps Following A Loss Of Instrument Air | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000316/LER-2006-002 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2006-002 | Failure to Comply with Technical Specification Requirement 3.6.13, Divider Barrier Integrity | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2006-002 | | | 05000289/LER-2006-002 | | | 05000251/LER-2006-002 | Intermediate Range High Flux Trip Setpoint Exceeded Technical Specification Allowable Value | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2006-002 | Scaffold Built in the Containment Pool Swell Region | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000413/LER-2006-002 | Safe Shutdown Potentially Challenged by an External Flooding Event and Inadequate Design and Configuration Control | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000388/LER-2006-002 | Missed Technical Specification LCO 3.8.1 Entry for Unit 2 During Unit 1 ESS Bus Testing | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2006-002 | Main Steam Isolation Valve Failure to Close | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2006-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000301/LER-2006-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000286/LER-2006-002 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration September 13, 2006 Indian Point Unit No. 3 Docket No. 50-286 N L-06-084 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2006-002-00, "Manual Reactor Trip as a Result of Arcing Under the Main Generator Between Scaffolding and Phase A&B of the Isophase Bus Housing" Dear Sir: The attached Licensee Event Report (LER) 2006-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2006-02255. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Fred R. Dacimo Site Vice President Indian Point Energy Center Docket No. 50-286 NL-06-084 Page 2 of 2 Attachment: LER-2006-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007
(6-2004)
. Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. ■ 1. FACILITY NAME 2. DOCKET NUMBER I 3. PAGE
INDIAN POINT 3 05000-286 1 OF 6
4.TITLE: Manual Reactor Trip as a Result of Arcing Under the Main Generator Between
Scaffolding and Phase A&B of the Iso-phase Bus Housing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000282/LER-2006-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2006-002 | High Energy Line Breaks Outside Licensing Basis May Result in Loss of Safety Function | | 05000263/LER-2006-002 | | | 05000255/LER-2006-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2006-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000483/LER-2006-003 | Unexpected Inoperability of the Emergency Exhaust System due to Inoperable Pressure Boundary | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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