06-05-2006 | On April 8, 2006, at 0105, with Unit 1 in Mode 3 prior to cooldown for a refueling outage, during Main Steam Isolation Valve (MSN) and Bypass Valves Cold Shutdown Valves Inservice Test, the Unit 1 downstream MSIV's failed to fully stroke closed. The A valve closed approximately 70%, and valves B and C did not move from the full-open position. On April 8, 2006, at 0700, after some cooldown, the A valve was found 90% closed, and would not move open or closed; the B valve was found 75% open, and was closed by repeated mechanical agitation; the C valve was found full open, and was closed by a single application of mechanical agitation. On April 9, 2006, at 1200, following completion of cooldown, all three valves would stroke both open and closed from the Main Control Room. This event was caused by inadequate preventive maintenance on shaft load bearing components, improper valve assembly, omission of relevant information in the procedure and turbulence in the downstream valves resulting in a more severe duty condition than in the upstream valves. The shafts and all load-bearing components in contact with the shafts of the downstream valves have been replaced, and the quarterly partial stroke test has been re-established. Preventive maintenance ( PM) for replacement of the shafts and load-bearing components in contact with the shafts will be established on Unit 1 and Unit 2 by August 1, 2006. Applicable Operations procedures have been revised. Applicable Maintenance procedures will be revised by August 1, 2006. Unit 2 valves have been partial stroke tested satisfactorily to verify that the stem will move.
An engineering review to consider possible design changes to reduce the severity of the service conditions in the downstream valves will be completed by March 15, 2007.
5NRC FORM 366 (6-2004) PRINTED ON RECYCLED PAPER |
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Westinghouse -- Pressurized Water Reactor Energy Industry Identification Codes are identified in the text as [XX]
Description of Event
On April 8, 2006, at 0105, with Unit 1 in Mode 3 prior to cooldown for a refueling outage, during Main Steam [SB] Isolation Valve (MSIV) and Bypass Valves Cold Shutdown Valves Inservice Test, the Unit 1 downstream MSIV's failed to fully stroke closed. The A valve closed approximately 70%, and valves B and C did not move from the open position. On April 8, 2006, at 0700, after some cooldown, the A valve was found 90% closed, and would not move open or closed with mechanical agitation or from the Main Control Room; the B valve was found 75% open, and was closed by repeated mechanical agitation; the C valve was found full open, and was closed by a single application of mechanical agitation. On April 9, 2006, at 1200, following completion of cooldown, all three valves would stroke both open and closed from the Main Control Room.
Cause of Event
Upon disassembly, the A valve shaft was found to have gouges under the packing follower location, and a crack initiated at a disc arm keyway. The B valve shaft was found to have wear marks under the packing follower location and an open circumferential crack that had initiated at a disc arm keyway. The keyway design results in a stress riser in the keyways. The C valve shaft was found to have deposition of packing material graphite bonded to the shaft in the packing region. The shafts and associated load bearing components of all three valves were found to have wear marks.
The shaft load bearing components had no defined criteria for replacement. Accumulation of wear allowed shaft clearances and roughness of components in contact with the shaft to increase over the years. This possibly allowed development of interference between the packing follower and shaft, as other shaft clearances increased while packing clearance remained tight due to packing replacement during each outage.
The thrust bearing on the shaft of downstream MSIV B was installed backwards. This coupled the shaft to the spacer on the opposite-actuator side of the valve disk assembly, causing increased wear rates in the bearing until axial clearances were lost, and thus increased drag resistance to shaft rotation. Relevant information (such as thrust bearing orientation and acceptance criteria for inspection of components subject to wear) was not specified in the procedure.
This event is unique to the downstream valves. The upstream valves are not subjected to high turbulence agitating the valve discs, which causes increased wear of load bearing components and cyclic tortional loads on the shaft. Due to less turbulence agitation, the upstream valves have not experienced the high-cycle fatigue that the downstream valves have experienced.
Safety Assessment The safety and health of the public were unaffected by this event.
The upstream valves were not affected by this event. Therefore, at least one train of Main Steam Line Isolation remained operable throughout this event. This event does not represent a Safety System Functional Failure.
Following cooldown, all three MSIV's stroked fully open and closed from the Main Control Room. All tests were conducted on the downstream valves without assistance of steam flow. It is the engineering judgment of the plant and the valve manufacturer that even though there may have been some binding in the full open position, had the valves been called upon to close under accident conditions with choke flow, they would have closed in the event of a steamline break downstream of the MSIV's.
The Unit 2 valves are operable at this time. The downstream Unit 2 MSIV's (farthest from containment) were inspected during the last Unit 2 outage, including penetrant testing. No cracks were identified in the shafts. The MSIV's were reassembled and satisfactorily tested and additionally were stroked in Hot Standby conditions. All of the Unit 2 MSIV's were partial stroke tested on April 24, 2006 and all stroked satisfactorily. In the event that a closure of the valves was necessary, movement into the steam flowpath would provide additional motive force to close the valves to assist the mechanical closure mechanisms.
Corrective Action The Maintenance procedure for MSIV overhaul will be revised by August 1, 2006. The Operations MSIV cold shutdown surveillance test procedure (STP) has been revised.
The quarterly partial stroke test procedure has been re-established for Units 1 and 2. The test cylinder used at Farley Nuclear Plant during partial stroke testing does not allow the disc to enter the flow stream, and therefore does not present the risks associated with partial stroke testing that the industry is currently experiencing.
All load-bearing components in contact with the shaft have been replaced on Unit 1 downstream valves including new shafts with radius design keyways.
Preventive maintenance (PM) for replacement of the shafts and load-bearing components in contact with the shafts will be established on Unit 1 and Unit 2 by August 1, 2006 Both upstream and downstream Unit 1 valves have been successfully tested at cold and hot shutdown conditions.
An engineering review to consider possible design changes to reduce the severity of the service conditions in the downstream valves will be completed by March 15, 2007.
Additional Information
The following LER's have been submitted in the past two years on Technical Specification violations:
Failure Troubleshooting
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05000305/LER-2006-010 | | | 05000456/LER-2006-001 | Unit 1 Reactor Coolant System Pressure Boundary Leakage Due To Inter-Granular Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000454/LER-2006-001 | Technical Specification Required Action Completion Time Exceeded for Inoperable Containment Isolation Valves Due to Untimely Operability Determination | | 05000423/LER-2006-001 | Loss Of Safety Function Of The Control Room Emergency Ventilation System | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000369/LER-2006-001 | Ice Condenser and Floor Cooling System Containment Isolation Valve inoperable longer than allowed by Technical Specification 3.6.3. | | 05000353/LER-2006-001 | HPCI Ramp Generator Signal Converter Failure | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000352/LER-2006-001 | Loss Of One Offsite Circuit Due To Invalid Actuation Of Fire Suppression System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2006-001 | | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | 05000316/LER-2006-001 | Failure to Comply with Technical Specification 3.6.2, Containment Air Locks | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2006-001 | Plant Shutdown Required by Technical Specification Action 3.6.5.B.1 | | 05000293/LER-2006-001 | | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000289/LER-2006-001 | | | 05000287/LER-2006-001 | Actuation of Emergency Generator due to Spurious Transformer Lockout | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000251/LER-2006-001 | Turkey Point Unit 4 05000251 1 OF 6 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2006-001 | Manual Reactor Trip Due to Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to Personnel Error | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2006-001 | Incorrect Wiring in the Remote Shutdown Panel Results in a Fire Protection Program Violation | | 05000413/LER-2006-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000368/LER-2006-001 | Completion of a Plant Shutdown Required by Technical Specifications Due to Loss of Motive Power to Certain Containment Isolation Valves as a Result of a Phase to Ground Short Circuit in a Motor Control Cubicle | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000306/LER-2006-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000298/LER-2006-001 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000286/LER-2006-001 | I | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000282/LER-2006-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000266/LER-2006-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000261/LER-2006-001 | Manual Reactor Trip Due to Failure of a Turbine Governor Valve Electro-Hydraulic Control Card | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000255/LER-2006-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000461/LER-2006-002 | Turbine Bypass Function Lost Due to Circuit Card Maintenance Frequency | | 05000458/LER-2006-002 | Loss of Safety Function of High Pressure Core Spray Due to Manual Deactivation | | 05000456/LER-2006-002 | Units 1 and 2 Entry into Limiting Condition for Operation 3.0.3 due to Main Control Room Ventilation Envelope Low Pressure | | 05000443/LER-2006-002 | Noncompliance with the Requirements of Technical Specification 6.8.1.2.a | | 05000387/LER-2006-002 | DMissed Technical Specification surveillance requirement | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000362/LER-2006-002 | Unit 3 Shutdown to Inspect Safety Injection Tank Spiral Wound Gaskets | | 05000336/LER-2006-002 | Manual Reactor Trip Due To Trip Of Both Feed Pumps Following A Loss Of Instrument Air | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000316/LER-2006-002 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2006-002 | Failure to Comply with Technical Specification Requirement 3.6.13, Divider Barrier Integrity | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2006-002 | | | 05000289/LER-2006-002 | | | 05000251/LER-2006-002 | Intermediate Range High Flux Trip Setpoint Exceeded Technical Specification Allowable Value | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2006-002 | Scaffold Built in the Containment Pool Swell Region | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000413/LER-2006-002 | Safe Shutdown Potentially Challenged by an External Flooding Event and Inadequate Design and Configuration Control | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000388/LER-2006-002 | Missed Technical Specification LCO 3.8.1 Entry for Unit 2 During Unit 1 ESS Bus Testing | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2006-002 | Main Steam Isolation Valve Failure to Close | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2006-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000301/LER-2006-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000286/LER-2006-002 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration September 13, 2006 Indian Point Unit No. 3 Docket No. 50-286 N L-06-084 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2006-002-00, "Manual Reactor Trip as a Result of Arcing Under the Main Generator Between Scaffolding and Phase A&B of the Isophase Bus Housing" Dear Sir: The attached Licensee Event Report (LER) 2006-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2006-02255. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Fred R. Dacimo Site Vice President Indian Point Energy Center Docket No. 50-286 NL-06-084 Page 2 of 2 Attachment: LER-2006-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007
(6-2004)
. Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. ■ 1. FACILITY NAME 2. DOCKET NUMBER I 3. PAGE
INDIAN POINT 3 05000-286 1 OF 6
4.TITLE: Manual Reactor Trip as a Result of Arcing Under the Main Generator Between
Scaffolding and Phase A&B of the Iso-phase Bus Housing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000282/LER-2006-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2006-002 | High Energy Line Breaks Outside Licensing Basis May Result in Loss of Safety Function | | 05000263/LER-2006-002 | | | 05000255/LER-2006-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2006-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000483/LER-2006-003 | Unexpected Inoperability of the Emergency Exhaust System due to Inoperable Pressure Boundary | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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