05000237/LER-2004-004

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LER-2004-004,
Docket Number
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(B), System Actuation

10 CFR 50.73(a)(2)(iv)(A), System Actuation
2372004004R01 - NRC Website

Dresden Nuclear Power Station Unit 2 is a General Electric Company Boiling Water Reactor with a licensed maximum power level of 2957 megawatts thermal. The Energy Industry Identification System codes used in the text are identified as

A. Plant Conditions Prior to Event:

Unit: 02� Event Date: 4-28-2004� Event Time: 1536 CDT Reactor Mode: 1� Mode Name: Power Operation� Power Level: 66 percent Reactor Coolant System Pressure: 1000 psig

B. Description of Event:

On April 28, 2004, at 1536 hours0.0178 days <br />0.427 hours <br />0.00254 weeks <br />5.84448e-4 months <br /> (CDT), with Unit 2 at approximately 66 percent power in Mode 1, a manual scram was inserted by operations personnel due to the plant being in a region of the reactor's power to flow map that required an immediate scram. The power to flow condition was caused by the unexpected trip of the 2A Reactor Recirculation Pump [P] and the manual scram was in accordance with immediate operator actions specified in procedure DOA 202.01, "Recirculation (RECIRC) Pump Trip — One Or Both Pumps." There were no Electromatic or Safety Relief valve actuations and no Emergency Core Cooling System initiations. Primary Containment Isolation System Group 2 and 3 isolations occurred as expected due to normal reactor water level decrease following the scram. All control rods fully inserted and all other systems responded to the manual scram as expected.

An ENS call was made on April 28, 2004, at 1750 hours0.0203 days <br />0.486 hours <br />0.00289 weeks <br />6.65875e-4 months <br /> (CDT) for the above-described event. The assigned ENS event number was 40713.

This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B) of this section." The manual actuation of the reactor protection system is listed in 10 CFR 50.73(a)(2)(iv)(B).

C. Cause of Event:

The root cause of the trip of the 2A Reactor Recirculation pump and the manual scram was attributed to a lack of detailed rewinding and acceptance test requirements in the Exelon large motor standard that governed the rewind of the 2A Reactor Recirculation pump motor.

The 2A Reactor Recirculation pump motor was replaced during a refueling outage in the fall of 1999. The replacement motor was a rewound motor that used a different process for rewinding than was used during initial manufacture. The original manufacturing processed used a Vacuum Pressurization Impregnation (VPI) process.

This process first includes taping the electrical coils, series connections and leads with mica tape insulation. Then the motor stator is placed in a VPI tank where a vacuum is created to remove all voids, followed by pressurization and epoxy resin injection to completely saturate and seal the motor windings. The rewound motor used a B-Stage process. This process is used when it is not possible to use the VPI process. The VPI process could not be used to rewind the motor, as there was not a VPI vendor to work on a large contaminated motor. The B-Stage process uses mica tape impregnated with epoxy resin on the motor coils. The coils are heated in an oven allowing the epoxy resin to form a sealed bond from the inside out. The B-Stage process does not control how the series and lead connections are insulated. The individual motor shop process governs this insulation.

An inspection of the failed 2A Reactor Recirculation pump motor revealed that the winding failure initiated in the series connection end turn where the copper strands from the coil are brazed together. The joint that failed was "NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (7-2001) Dresden Nuclear Power Station Unit 2 05000237 NUMBER NUMBER melted in the failure, however, a nearby un-failed joint provided the likely configuration. The joints were brazed within a copper sleeve with strands extending outside the sleeves forming a relatively sharp corner. The insulating mica tape was applied directly over this corner. Wrapping the tape over the corner resulted in thinning of the tape, potentially damaging the tape layers during installation and resulting in a stressed region likely to be damaged during motor operation due to movement. The insulating mica tape appears to have been applied with a dry­ lapping process, with each layer applied directly over the other without a bonding agent. Applied over an irregular surface, this method can result in voids and allows relative movement of individual layers.

The series joint at the point of failure was at the top of the bend in the series connection. The bends were taped such that the bottom of the bend received full overlaps while the tops of the bends were half-lapped. The location of the failure at the top of the bend had the thinnest layering.

The rewinding of the 2A Reactor Recirculation pump motor was performed in accordance with the ComEd, "Large Motor Repair Standard 9894047.9159? The standard had a very detailed rewind and acceptance testing requirements for rewinding motors using the VPI process but did not have the same level of detail for the B-Stage process. The lack of detailed rewind and acceptance testing requirements in the standard allowed the motor vendor to provide minimum insulation at the series connection. When the motor rewind was complete, the stator had a wet High-Pot test performed before final assembly. The pre-test found that there were some inadequate seal spots at the series connections location. The series connections were repaired and the stator passed the next test.

D. Safety Analysis:

The safety significance of the Reactor Recirculation pump trip and the resulting manual scram event was minimal.

The transient response of the plant has been analyzed for the trip of one or two Reactor Recirculation pump and the results are contained in Chapter 15 of the Dresden Update Final Safety Analysis Report. The manual scram of the plant was in accordance with an approved pi.ocedure. There were no Electromatic or Safety Relief valve actuations and no Emergency Core Cooling System initiations. Primary Containment Isolation System Group 2 and 3 isolations occurred as expected due to normal reactor water level decrease following the scram. All control rods fully inserted and all other systems responded to the manual scram as expected.

Therefore, the consequences of this event had minimal impact on the health and safety of the public and reactor 'safety.

E. Corrective Actions:

The failed Reactor Recirculation pump motor was replaced.

The failed Reactor Recirculation pump motor was shipped on May 17, 2004, to a vendor's maintenance shop for evaluation. The vendor's evaluation report was received on August 9, 2004 Two outstanding purchase orders for the rewinding of two Dresden Reactor Recirculation pump motors were revised to include enhanced installation and testing requirements.

Exelon Nuclear Engineering Standard NES-EIC-40.01, "Large Motor (>2 kv) Repair Requirements," will be revised to incorporate B-Stage installation and testing requirements similar to the requirements for the VPI process.

NRC FORM 366A� U.S. NUCLEAR REGULATORY COMMISSION (7-2001) Dresden Nuclear Power Station Unit 2 05000237 NUMBER NUMBER

F. Previous Occurrences:

A review of Dresden Nuclear Power Station Licensee Event Reports (LERs) and operating experience over the previous five years did not find any similar occurrences associated with a failed Reactor Recirculation pump.

G. Component Failure Data:

General Electric 5770 HP Motor, Model 5K26376AG1