ML17266A086

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LER 79-020/03L-0 on 790614:auxiliary Feedwater Pump 1c Failed to Start Due to Failure of Steam Inlet Valve.Caused by Unknown Factor.Valve Operated Normally After Being Manually Cycled
ML17266A086
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 07/13/1979
From: SCHOPPMAN M A
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17206A915 List:
References
LER-79-020-03L, LER-79-20-3L, NUDOCS 7907250341
Download: ML17266A086 (1)


Text

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S ecification i 5 This was the seventh occurrence of the 1C Pump failing,to start and the second occurrence for which the root cause was unknown.(LER 335-77-33)~

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