ML17326A542

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LER 80-007/03L-0:on 800129,during Surveillance Test, Containment Isolation Valve NCR-252 Did Not Close Fully. Cause Unknown.New Diaphragm Placed in Valve Operator.Valve Restroked & Timed Before Returning to Svc
ML17326A542
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 02/28/1980
From: RISCHLING J
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A539 List:
References
LER-80-007-03L, LER-80-7-3L, NUDOCS 8003040543
Download: ML17326A542 (1)


Text

1 IP 4 1 4~tP 1 1\I (7.77)~0 7 8 CON'T[oaf 7 8 LICENSEE EVENT REPORT Q1 IPLEASE PRINT OR TYPE A L REQUIRED INFORhlATIONI 6 ZQE 0 0 0 0 0 0 0 0 0 0 0QEO 1 1 1 Q~ps 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CONTROL BLOCK: I M I D C C 9 LICENSEE CODE~LQB 0 5 0 0 0 3 QO 1 2 9 8 0 Q 60 61 DOCKET NUMBER EVENT DATE 74 75 RFPPR1'ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 DURING NORMAL OPERATION WHILE PERFORMI A SURVEILLANCE TEST, CONTAINMENT QB ISOLATION VALVE NCRL252 (PRIMARY WATER TO THE PRESSURIZER RELIEF TANK)DID NOT 4 CLOSE FULLY.THIS VIOLATED T.S.3.6.3.1.AN UPSTREAM MANUAL ISOLATION VALVE WAS SHUT UNTIL NCR-252 WAS RETURNED TO SERVICE.~07~OB 7 8~OB 7 8 9 80 SYSTEM CAUSE CAUSF.COMP VAI VE CODE'.COPE,.SUBCODE COMPONENTCODE SUBCODE SUBCODE~5D Q11~E Q12~X Q>>V A L V E X Q4~F Q>>LJZI, Q78 9 10 11 12 13 18 19'0 SEQUENTIAL OCCURRENCE

'EPORT REVISION LF RIRO EVENT YEAR REPORT NO.CODE.TYPE NO.Q17 REPoRT~so~~oo~w~03~L~~0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRlhIE CONIP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS+22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER

~XQ78~ZQ18~ZQER~ZQ21 0 0 0'Q23~NQ24'NQEE G 2 5 5 pss 33 34 35 36 37~40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS+27 AN INSPECTION OF THE VALVE INTERNKS AND VALVE OPERATOR FAILED TO REVEAL ANY CAUSE FOR THE VALVE'NOT CLOSING I-ULL'(;A NEll DIAPHRAGM WAS PLACED IN THE VALVE OPERATOR AS A PRECAUI'IONARY MEASURE.NCR-252 WAS 1HEN RESTROKED AND TIMED AS RE(UIRED BY T.S.4.6.3.1.1.

PRIOR TO BEING RETURNED TO SERVICE.NO FURTHER ACTION IS PLANNED, 4 SINCE NO ADDITIONAL PROBLEMS HAVE BEEN ENCOUNTERED WITH THIS VALVE.CE3 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q 8 Z Q33~ZQ34 NA7 8 9 10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 7~00 0 Q37~ZP38 NA LOCATION OF RELEASE Q 45 7 8 EI 9 11 12 13 PERSONNEL INJURIES NUMBER OESCRIPTIONQ41

~00 O Q48 NA 7 8 9 FACILITY~30 h'IETHOD OF STATUS Ts POWER OTHER STATUS~DISCOVERY~DISCOVERY DESCRIPTION 1 5~EQ28~09 0 Qs NA~BP31 SURVEILLANCE TEST 9 10 12 13 44 45 46 80 80 80 80 7 8 8 O 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Z Q4.NA 9 10 PUBLICITY ISSUED DESCRIPTION

~L~JQ44 NA 9, 10 NAME QF PREPARER Jack Rischl in$0y g ss ss 80 80 NRC USE ONLY~4 a 2 80 a 0 tL