ML17331A743

From kanterella
Revision as of 08:28, 6 July 2018 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
LER 80-038/03L-0:on 801224,testing of Main Feedwater Check Valves Not Performed as Required Per Inservice Insp Program in Preparation for Startup.Caused by Misinterpreted Checkoff Sheet.Temporary Change Sheet Initiated
ML17331A743
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/23/1981
From: STEPHENS T R
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17319A927 List:
References
LER-80-038-03L, LER-80-38-3L, NUDOCS 8106090488
Download: ML17331A743 (1)


Text

NRC Cv6RhT 366, U.S.NUCLEAR REGULATORY COMMISSION 0 73)LICENSEE EVENT REPORT CONTROL BLOCK: Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6~oi M I D C C 2 Q2 0 P Q4 QE~Qs 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T KK soURGE~LQ<<'O O>>6 Q>>QB 0 1 8 1 Qe 7 8 60 61 DOCKET NUMBER 68 69EVENT DATE 74~75 REPbRT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO IN PREPARATION FOR START UP THE TESTING OF'W-118-1 2 3 4 AS RE VIREO BY THE IS I PROGRAM WHILE IN h10DE 3 WAS NOT DONE.(T.S.4.0.5)THE (4)MAIN FEEDWATER CHECK VALVES NOT BEING TESTED HAD NO EFFECT ON THE HEALTH AND SAFETY OF THE PUBLIC o 6 IN AS MUCH AS THERE ARE MOTOR OPERATED AND AIR OPERATED VALVES UPSTREAM OF THESE~o 6 VALVES THAT WOULD STOP REVERSE FLOW.i~O7~OB 7 8 9 80 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~o,e~CN Q11 0 Q12~Z Q13 Z Z Z Z Z Z Q4~ZQEE~Z QER 9 10 11 12 , 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LE R)RO EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPQRT~0~~7~ILJ~~IILII~~~[gJ 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT.

NPRDR PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS O22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER

~GQER~ZQTE~ZQ23 I 2 IQ 0 N Q23~NQ24~ZQEs Z 9 9 9 QEs 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE FACT THAT THESE VALVES WERE NOT TESTED WAS MASKED BY THE FACT THAT SIGN OFFS FOR OTHER MODE TESTS ALSO APPEARED ON THE SAME CHECKOFF SHEET.A TEMPORARY CHANGE SHEET WAS WRITTEN TO SEPARATE THE TEST AS TO THEIR MODE RE UIREMENTS.

OTHER 3 PROCEDURES ARE BEING REVIEWED FOR SIMILIAR PROBLEMS.PUBLICITY ISSUED DESCRIPTION Q O~NQ44 B7.6609'6H'P NA 8 9 FACILITY STATUS%POWER OTHER STATUS~ls C Q23~10 0 Qss NA 7 8 9 10 12 13 44 ACTIVITY CONTENT RELEbSED OF RELEASE AMOUNT OF ACTIVITY Q 6~Q33~~Q34 7 8 9 10 44 PERSONNEL EXPOSURES 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41

~TR~00 0 Q43 NA 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION Z Q42 NA 7 8 9 10 80 80 80 80 80 80 NRC USE ONLY 80 ss 0 Q 68 69 EsunEEEE;.

sss/4 f4/NIR 5'5 9'0/METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32'~AQ31 COMPLETED TEST DATA REVIEW 45 46 LOCATION OF RELEASE Q NA 45