ML17221A444

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LER 87-006-00:on 870917,discovered That Test of Emergency Diesel Generator Automatic Load Sequence Relays Incomplete. Caused by Personnel Error.Personnel Immediately Performed Required Surveillance Test Per procedure.W/871016 Ltr
ML17221A444
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 10/16/1987
From: MENDOZA V N, WOODY C O
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
L-87-417, LER-87-006-03, LER-87-6-3, NUDOCS 8710220113
Download: ML17221A444 (5)


Text

REGULATINFORMATIONDISTRIBUTIOYSTEM<RIDS)ACCESSIONNBRFACIL:50-389AUTH.NAMEMENDOZAIV.N.WOODY'.O.RECIP.NAME8710220113DOC.DATE:87/10/ibNOTARIZED:NOSt.LuciePlantiUnit2iFloridaPoeerhLightCo.AUTHORAFFILIATIONFloridaPower5LightCo.FloridaPoeer5LightCo.RECIPIENT'AFFILIATIONDOCKET¹05000389

SUBJECT:

LER87-00b-00:on870917'estof2ASc2Bemergency'ieselgeneratorautomaticloadsequencerelaysincomplete.Causedbgpersonnelerror.Personnelimmed.iatelgperformedrequiredsurveillancetestinaccordanceUj/procedure.W/8710ibltr.DISTRIBUTIONCODE:IESRDCOPIESRECEIVED:LTRIENCLgSIZE:TITLE:50.73LicenseeEventReport<LER)iIncidentRptietc.NOTES:RECIPIENTIDCODE/NAMEPD2-2LATOURIGNYiEINTERNAL:ACRSMICHELSONAEOD/DOAAEOD/DSP/ROABARM/DCTS/DABNRR/DEST/ADSNRR/DEST/ELBNRR/DEST/MEBNRR/DEST/PSBNRR/DEST/SGBNRR/DLPG/GABNRR/DREP/RABSIB02RESTELFQRDIJRGN2FILE01EXTERNAL:EGLGGRQHiMLPDRNSICHARRISIJCOPIESLTTRENCL111111122111011111111111111111551111*RECIPIENTIDCODE/NAMEPD2-2PDACRSMOELLERAEQD/DSP/NASAEOD/DSP/TPAB.DEDRQNRR/DEST/CEBNRR/DEBT/ICSBNRR/DEST/MTBNRR/DEST/RSBNRR/DLPG/HFBNRR/DOEA/EABNRR/DREP/RPBNRR/PMAS/ILRBRESDEPYGIRES/DE/EIB'STLOBBYWARDNRC'PDRNSICMAYS.GCOPIESLTTRENCL1122111'111:111111111122"11.111'1111TOTALNUMBEROFCOPIESREQUIRED:LTTR45ENCL44 NRCForm344(403)LICENSEEEVENTREPORT(LER)V.S.NUCLEARREGULATORYCOMMISSIONAPPROVEDOMBNO.3150010CEXPIRES,'i3)i45FACILITYNAME(I)ST.LUCIEUNIT2DOCKE'TNUMBER12)PAGEI3i03891OF03MISSEDSURVEILLANCEONTHE2AAND2BEMERGENCYDIESELGENERATORAUTOMATICLOADSEUENCERELAYSDUETOACOGNITIVEPERSONNELERROR.EVENTDATE(5)LERNUMBER(4)REPORTDATE(7)OTHERFACILITIESINVOLVED(SIMONTHOAYYEARYEARei>.;SEQUENTIALy'-NUMSERSrTNUMSERMONTHDAYR4Vt)KINYEARFACILITYNAMESN/ADOCKETNVMBERISI0500009178787060010168705000OPERATINOMOOK(~I~OWERL'EYEL1020402(4)20A04(e)Ill(0204444)Ii)I4I20A04(~l(1)(SI)2040441(11(lvl204044)llI(v)20404(el50.34IclI)I50.34(cl(1)X50.73(el(2)(II50.73(el(2)(4)50.73(el(2)((BILICENSEECONTACTFORTHISLER(12)50.73(~l(2)(wI50.73(~II2I(v)50.73(e)(2)(vnl50,73Ie)LT)4iil)(Al50.73(~I(2)Ivi)i~)I4I50.73I~)(2IIxlTHISREPORTISSUBMITTEDPURSUANTT0THKREQUIREMENTSOF10CFR(I;fCneceoneormoreOftnefollowing/(1173.71(4)73.71(~IOTHER(SpecifyinapstisctOelOwentrinTert,iVRCperm3544INAMEV.N.Mendoza,ShiftTechnicalAdvisorTELEPHONENUssBERAREACODE305465-:3550COMPLETEONELINKFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEM'COMPONENTNANANAMANUFAC.TVRERNANAc:)Prrrst2wgSYSTKMCOMPONENTMANUFAC.TVRERREPORTABLETONPRDSw'vSUPPLEMENTALREPORTEXPECTEDlle)YESfffyet,CemptetetXptCTEDSVSetfSSIOefOATtfNOABSTRACT(Limittotc00tpeces.f.e..epprosimeNryRfteentingie.specstvpewrNNnfinest(14)EXPECTEDSUBMISSIONDATE(15IMONTNDAYYEARNAAt1900onSeptember17,1987,itwasdeterminedthatthe12monthtestofthe2Aand2BEmergencyDieselGenerator(EDG)automaticloadsequencerelayswasincomplete.Areviewofthesurveillanceprocedure,performedonMay4,1987,indicatedthatonlythecomponentsonthe4160volt2A3and2B3busesweretestedandthatthetestdidnotincludethecomponentsonthe4160volt.2ABbusandthe480voltloadcenters(LC).Therootcauseoftheeventwasacognitivepersonnelerrorbyutilitypersonnelimplementingthemaintenancesurveillanceprocedureandthequalitycontrolpersonnelreviewingtheplantworkorderandthemaintenancesurveillanceprocedureforcompletenessandcompliancetothesurveillancerequirements.'Forcorrectiveactions,theelectricalmaintenancepersonnelimmediately-performedtherequiredsurveillancetestinaccordancewiththeapprovedprocedure.PlantManagementhasre-emphasizedtheimportanceofadequatereviewofplantworkordersandsurveillanceprocedures.Inaddition,thesurveillanceprocedurewasrevisedforclarity.8710@201138710~16389PDRADOCK050$NRCForm344iS43s NRt!Form3EEAO.831LICENSEEEVENTREPORT(LERITEXTCONTINUATIONU.S.NUCLEARRECULATORYCOMMISSIONAPPROUEOOMSNO.3(50-0(0<EXPIRES:8/31/88FACILITYNAME(I)ST.LUCIEUNIT2OOCKETNUMBER(2)YEARLERNUMSER(8)N).SEQUENTIALNUMBERREvrsroNNUMBERPACE(3)TEXT///moree/reooierequired,ueeeddr(r'orre/HRCForrrr3SSA'e/l)2)0500038987006-0'2OF03DESCRIPTIONOPTHEEVENTAtapproximately'1730onSeptember17;1987,operationspersonnel.werenotified~thatanFPLQualityAssuranceaudithaddeterminedthetwelvemonthtestofthe2Aand2Bemergencydieselgenerator(EDG)(EIISSEK)automaticloadsequencerelaysperformedonMay4,1987wasincomplete.Thisprocedurerequiredthatallcomponentsonthethe4160Vbusesandthe480Vloadcenters(LC)betestedforproperloadsequencerelaytiming.Duringthereview,itwasdiscoveredthatonlythecomponentsonthe4160volt2A3and2B3busesweretested.At1900onSeptember17,1987,effortswerestarted"toperformtherequiredsurveillanceteststocomplywiththeTechnicalSpecificationrequirements.By0600onSeptember18,1987,allthecomponentsonthe2AEDG(Train"A")weresatisfactorilytestedandby1453onSeptember18,1987,allofthe2Aand,2BEDGcomponentsweresatisfactorilytested.AlltherelaystestedwerefoundtobewithinthetolerancerequirementsoftheTechnicalSpecifications.St.LucieUnit82remainedatMode1,100%power,throughoutthistimeperiod.rCAUSEOPTHEEVENTTherootcauseoftheeventwasacognitivepersonnelerrorbyutilitymaintenanceandqualitycontrolpersonnelresponsibleforreviewingtheplantworkorder(PWO)toensurecompleteimplementationandcompliancewiththerequirementsofthesurveillanceprocedures.Thecopyoftheprocedureusedbythejourneymanhadhandwrittendirectionsonthe'tepsof,the.procedure.indicatingwheretostart,andwheretostop.'heseinstructionsonlycoveredthe4160volt2A3and2B3components.Consequently,'160volt2ABbusandthe480VLCportionsoftheprocedurewereneverperformed.Thereviewof.thePWOdidnotrevealthisomission.ANALYSISOPTHEEVENTTechnicalSpecifications4.8.1.1.2.drequiresthatwhileoperatinginModes1,2,3,and4eachdieselgeneratorshallbedemonstratedoperablebyverifyingthatatleastonceper12monthstheautomaticloadsequencetimersareoperablewiththeintervalbetweeneachloadblockwithinplus/minusonesecondofitsdesigninterval.SincetheSt.LucieUnitN2wasoperatinginMode'1whentheeventwasdiscovered,thisreportisbeingsubmittedunder10CFR50.73(a)(2)(i)(B),anyoperationorconditionprohibitedbytechnicalspecificat'ionsasdefinedingenericletter87-09.Thelast'urveillancefortheEDG.12-monthtest'ftheautomaticloadsequencerelayswassatisfactorilyperformedinMay1986.ThissurveillanceprocedurewascompletedonSeptember18,1987,approximately18.5dayspastthemaximumallowableextensionof25%ofthetestingintervalafterthesurveillancewas'dueandapproximately22hoursafterthediscoveryofthecondition.Allcomponentstestedsatisfactorily,thusthehealthandsafetyofthegeneralpublicwerenotaffectedbythisevent.NRCFORM3BBA(94)3)

NRCFoehn3ddA(94)3ILICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONAPPROVEOOMBNO.3)9)W)04EXPIRES:8/31/88FACILITYNAME(I)DOCKETNUMBERl3)YEARLERNUMBER(8)SEOVENTIALNVMSSAK'IKIOAEV/SIONNVMSSAPAGE(3IST.LUCIEUNIT2TEXTIII///o/osPscois/odw'red,//sosddio'o/MIHRC%%d////3dSA'4/(17)osooo38987006003OF03CORRECTIVEACTIONS1.AfterOperationspersonnelwerenotifiedofthemissedsurveillancecondition,therequiredsurveillancewasimmediatelyperformedandwasdeemedsatisfactory.2.PlantManagementhasre-emphasizedtoplantpersonneltheimportanceofcompletingalltechnicalspecificationsurveillancesinatimelymannerasrequired.3.TheplantTxainingDepartmentwillevaluatethisitemtodetermineappropriatetrainingrequirementsandmethods..4.ThepersonnelresponsibleforpreparationandreviewoftheabovePWOhave*beencounselledontheimportanceofattentiontodetailinensuringTechnicalSpecificationsurveillancerequirementsaremet.5.Thesurveillanceprocedurewasrevisedforclarity.ADDITIONALINFORMATIONFailedcomponentinformation:Nocomponentorsystemfailuresoccuredduringthisevent.Previous.similarevent:ThemostrecentsimilareventonUnitII2wasamissedsurveillancesubmi.ttedunderLER$389-86-014.N/ICFORMSddA(94)3)

P.OX14000,JUNOBEAC<.,k.C;.gQ<0~pe.iOBcRi(,1~8(L<7OI7-IOCFR50.73U.S.NuclearRegulatoryCommissionAttn:DocumentControIDeskWashington,D.C.20555GentIemen:Re:St.LucieUnit2DocketNo.50-389ReportableEvent:87-06DateofEvent:Septemberl7,l987MissedSurveillanceonEmergencyDieselGeneratorAutoLoadSeuenceRelasTheattachedLicenseeEventReportisbeingsubmittedpursuanttotherequirmentsofIOCFR50.73.a.toprovidenotificationonthesubjectevent.Verytrulyyours,iI'p,i;o,E~C.0.Wo'odyGroupVicePresidentNuclearEnergyCOW/GRM/gpAttachmentcc:J.NelsonGrace,RegionalAdministrator,RegionII,USNRCSeniorResidentInspector,USNRC,St.LuciePlantGRMI/030/IanFPLGroupcompany