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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station ML20148K4161997-05-31031 May 1997 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20141B9631997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Pilgrim Nuclear Power Station ML20137T5631997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Pilgrim Nuclear Power Station ML20136G7791997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Pilgrim Nuclear Power Station ML20138K5811997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Pilgrim Nuclear Power Station ML20133G5831996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Pilgrim Nuclear Power Station BECO-96-106, Monthly Operating Rept for Nov 1996 for Pilgrim Nuclear Power Station1996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-097, Monthly Operating Rept for Oct 1996 for Pilgrim Nuclear Power Station1996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Pilgrim Nuclear Power Station ML20128N2611996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-083, Monthly Operating Rept for Pilgrim Nuclear Power Station for Aug 1996 Ltr1996-08-31031 August 1996 Monthly Operating Rept for Pilgrim Nuclear Power Station for Aug 1996 Ltr ML20116L0841996-07-31031 July 1996 Monthly Operating Rept for Jul 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-066, Monthly Operating Rept for June 1996 for Pilgrim Nuclear Power Station1996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-056, Monthly Operating Rept for May 1996 for Pilgrim Nuclear Power Station1996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Pilgrim Nuclear Power Station ML20117E0961996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-034, Monthly Operating Rept for Mar 1996 for Pilgrim Nuclear Power Station1996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-023, Monthly Operating Rept for Feb 1996 for Pilgrim Nuclear Power Station1996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-008, Monthly Operating Rept for Jan 1996 for Pilgrim Nuclear Power Station1996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Pilgrim Nuclear Power Station BECO-LTR-96-004, Monthly Operating Rept for Dec 1995 for Pilgrim Nuclear Power Station1995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Pilgrim Nuclear Power Station ML20095E7351995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Pilgrim Nuclear Power Station Unit 1 BECO-LTR-95-116, Monthly Operating Rept for Oct 1995 for Pilgrim Nuclear Power Station1995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Pilgrim Nuclear Power Station ML20093F5221995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Pilgrim Nuclear Power Station BECO-LTR-95-097, Monthly Operating Rept for Aug 1995 for Pilgrim Nuclear Power Station1995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Pilgrim Nuclear Power Station BECO-LTR-95-081, Monthly Operating Rept for July 1995 for Pilgrim Nuclear Power Station1995-07-31031 July 1995 Monthly Operating Rept for July 1995 for Pilgrim Nuclear Power Station BECO-LTR-95-071, Monthly Operating Rept for June 1995 for Pilgrim Nuclear Power Plant1995-06-30030 June 1995 Monthly Operating Rept for June 1995 for Pilgrim Nuclear Power Plant 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20153D3901998-09-22022 September 1998 Safety Evaluation Granting 970707 Request to Use Guidance in GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water Sys Piping for Pilgrim Nuclear Power Station ML20197C5011998-09-0404 September 1998 Rev 12C,Pages 4 & 5 to Pilgrim Nuclear Power Station Colr ML20197C5471998-08-31031 August 1998 Rev 12C to Pilgrim Nuclear Power Station Colr ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237E2251998-08-26026 August 1998 Suppl & Revs to SE for Amend 173 for Pigrim Nuclear Power Station ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236U8201998-07-13013 July 1998 Rev 12B to Pilgrim Nuclear Power Station COLR (Cycle 12) ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20207B7601998-03-31031 March 1998 Final Rept, Pilgrim Nuclear Power Station Site-Specific Offsite Radiological Emergency Preparedenss Prompt Alert & Notification System Quality Assurance Verification, Prepared for FEMA ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20216J3741998-03-19019 March 1998 Safety Evaluation Accepting Licensee Request to Evaluate Elevated Tailpipe Temp on Safety Relief Valve SRV 203-3B ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20236M8511997-12-31031 December 1997 1997 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station ML20202D5761997-11-0808 November 1997 1997 Evaluated Exercise BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217D6431997-10-0101 October 1997 Safety Evaluation Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Class 3 SSW Piping for Pilgrim ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station 1999-09-08
[Table view] |
Text
{
. :. y BOSTON EDISON Pilgr# Nuclear Pov.or station Rocky Ril Road Plymouth, Massachusetts 02360
- E. Thomas Boulette, PhD Vee President Nuclear Operanons and Stanon Duecto.
November 12, 1992 BECo Ltr. #92-127 U.S Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555 sicense No. DPR-35 D_ocket No. 50-293
Subject:
October 1992 Monthly Report in accordance with PNPS Technical Specification 6.9.A.2, a copy of the-Operational Status Summary for Pilgrim Nuclear Power Station is attached for your information and planning. Should you have any questions concerning this report please contact me directly, hflot tbJ C LY E. Thomas Boulette WJM/bal Attachment cc: Mr. Thomas T. Martin Regional Administrator, Region 1 U.S. Nuclear Regulatory Commission 475 Allendale Rd.
King of Prussia,.PA 19406 Mr. R. B. Eaton Div. of Reactor Projects I/II Office of NRR - USNRC One White Flint North - Mail Stop 14D1 11555 Rockville Pike Rockville, MD 20852 Senior Resident Inspector 170019 9211170227 921o31
/ l PDR ADOCK 05000293 '
R PDR l
OPERATING DATA REPORT DOCKET NO. 50-293 __
DATE. _ November 12. 1992 COMPLETED BY W. Munro TELEPHONE (508) 747-5474 _
OPERATING _ STATUS Notes
- 1. Unit Name Pilarim 1
- 2. Reporting Period October 1992
- 3. .nsed Thermal Power (MWt) 1998
- 4. nameplate Rating (Gross MWe) 678
- 5. Design Electrical Rating (Net MWe) 655
- 6. Maximum Dependable Capacity (Gross MWe) 6 16 ,
- 7. Maximum Dependable Capacity (Net MWe) 670 __
- 8. If thanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
None
- 9. Power Level To Which Restricted, If Any (Net MWe) __ None
- 10. Reasons for Restrictions, If Any N/A This Month Yr-to-Date f_quiul ative
- 11. Hours In Reporting Period 745.0 7320.0 174408.0
- 12. Number Of Hours Reactor Was Critical 562.8 6760.4 105121.0
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 -0.0
- 14. Hours Generator On-Line 557.7 6703.2 10120511
- 15. Unit Reserve Shutdown-Hours 0.0 0.0 Q10
- 16. Gross Thermal Energy Genereted(MWH) 1096680.0 13115040.0 176819520.0-
-17. Gross Electrical Energy Generated (MWH) 377760.0 4520220.0 .59726634.0
- 18. Net Electrical Erergy Generated (MWH) 363483 _4351042.0 57401990.0
- 19. Unit Service Factor 74.9 91.6 58.0-
- 20. Unit- Availability Factor ..
74.9- 91.6 58.0
- 21. Unit Capacity Factor. (Using MDC Net) 72.8 88.7 -49.1
- 22. Unit Capacity Factor.(Using DER Net) 74.5: 90.7 '50.2-
- 23. Unit Forced Outage Rate 0.0 6.0 12.2
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date,-and Duration of Each):
Refuelino 0utane #9 startina 4-3-93 for a duration of 58 days
- 25. If Shut Down At End Of Report Period, Estimated Date of Startup 11-22-92 r
4 e AVERAGE DAILY UNIT POWER LEVEL DOCKET N0, 50-293 UNIT Pilarim i DATE November 12, 1992 COMPLETED BY W. Munro TELEPHONE [5_08) 747!5474 MONTil October 199&
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 569 17 663 2 662 18 663 . _ _ _ _
3 661 19 663 4 661 20 661 5 661 21 662 6 662 22 662 7 663 23 609 8 663 24 60 9 661 25 0 10 662 26 0 11 664 27 0 12 664 28 0 13 661 29 ___
0 14 663 30 0 15 663 31 0 16 662 This format lists the average daily unit power level in MWe-Net for each day in the reporting month, computed to the nearest whole megawatt.
. --, - - - - - _ - - . .- .- - - -- - - . . - - ~ .
BOSTON EDISON C0iiPANY >
PILGRIM NUCLEAR POWER STATION-4 DOCKET NO. 50-?93 Operational Summary for October 1992 The unit started the reporting period at approximately 64 percent core-thermal power (CTP). Following maintenance on 'C' Reactor Feed Pump, the pump was started and power ascension commenced. At.approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> the unit attained 100 percent CTP._ This power level was essentially maintained until October 23 when at approximately 2036 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.74698e-4 months <br /> a controlled shutdown was initiated to facilitate the planned Midcycle Maintenance and Surveillance Outage. During power reduction, a planned backwash of the m, a condenser was accomplished at approximately 50 percent (CTP). Following backwashing of the Main Condenser, power was increased temporarily to apprcximately 65 percent CTP to perform a thermal backwash. At approximately 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on October 24 power reduction continued, and at 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br /> the turbine generator was tripped off line. All control rods were inserted at 1006 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.82783e-4 months <br />, and the mode switch was placed in SHUTDOWN position at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br />.
The unit ended the reporting period in cold shutdown condition with midcycle maintenance-activities underway. Startup from the midcycle outage is scheduled for November 22, 1992.
Weekly control rod exercises were performed on October a, 10 and 17, 1992. Minor power reductions occurred on October 9 and 10 while performing reactivity manipulations for training purposes.
Safety Relief Valve Challenges Month of October 1992 Requirement: NUREG-0737 T.A.P. II.K.3.3 There were no safety relief valve challenges during this reporting period.
An SRV challenge is defined as anytime an SRV has received a signal to operate via reactor pressure, auto signal -(ADS) or control switch -(manual). Ref. BEco ltr. #81-01 dated-01/05/81.
, . - . - - . -. . = - .-
. ~
- REFUELING INFORMATION :
- The following refunling information is included.in the-Monthly Report as requested in an
- NRC~ letter to BECo,_ dated. January 18, 1978:
for your convenience, the information supplied has been enumerated so that each number Ecorresponds to equivalent notation utilized in the reqqcst.
- 1. The name of this facility is Pilgrim Nuclear Power Station, Docket Number 50-293.
- 2. Scheduled date for next refueling shutdown: April 3, 1993
- 3. Scheduled date for restart following next refueling: May 30, 1993
- 4. Due to their similarity, requests 4, 5, & 6 are responded to collectively under #6.
- 5. See #6.
- 6. The new fuel loaded during the 1991 refueling outage was of the same design as'-
loaded in the previous outage and consisted of 168 assemblies.
- 7. (a) There are 580 fuel assemblies in the core.
(b) There are 1489 fuel assemblies in the spent fuel pool.
- 8. (a) The station is presently licensed to store 2320 spent fuel assemblies. The- ,
actual usable spent fuel storage capacity is 2320 fuel assemblies.
(b) The planned spent fuel storage capacity is 2320 fuel assemblies.
- 9. With present spent fuel in storage, the-spent fuel pool.now has the capacity to-accommodate an additional 831 fuel assemblies.
I e -
MONTH ' October, 1992
PILGRIM NUCLEAR POWER STATION :,
MAJOR SAFETY RELATED MAINTENANCE
. SYSTEM COMPONENT MALFUNCTION CAUSE MAINTENANCE CORRECTIVE ACTION TO ASSOCIAIED PREVENT RECURRENCE- -LER-Reactor Reactor' Vessel. False high Water level Correct leakage Refer to Associated LER Vessel' water level reactor vessel purturbations at fittings etc. LER. 92-013-00 (RV) control, inst- water level . (spiking) in for Instrument (To be rumentation signal causing- the 'B' refer- Rack C-2206 issued) reference: leg. automatic act- ence leg of'the (Rack B).
'B condensing' uation of the reactor vessel Measure instru-
, chamber.128. Mai Steam - water level in- ment' bypass System / Group 1 strumentation. valve leakage portien of the. on Racks C-2205 Primary Conta- and C-2206.
inment Isola- Confirm accuracy ion ControlL of resistance ,
-System (PCIS). . temperature devices PR92-9203 (RTDs) previously installed per Temp- ;
orary Modification 91-44.
Sal t - Pump P208E SSW P208E .
.Under invest- Replaced.seven Bid specific- N/A
- Service pump failed igation.. .(7) spider ations sent surveillance . bearings, inst-
- Water to'various (SSW) Test Procedure alled rebuilt vendors to 8.5.3.2.(Oper- bowl and two-(2) investigate abili ty ' Test,' intermediate vibration
-due to.. low columns which- problems and
- discharge were'out of- limited pump
. fl ow. . ~ tolerance, and a. life.-
PR92-9184 new pump motor.'.
lMidcycle Maintenance outage commenced October 24, 1992:and maintenance:' activity-is being accomplished in ,
.accordance.with' outage. schedule.. >
^
' UNIT SHUTDOWNS AND POWER REDUCTIONS -DOCKET NO. 50-293 -
4 RAME PILGRIM 1 . . .
DATE November 12,1 .992' E, COMPLETED.BY W. MUNRO. .
TELEPHONE 508 747-8474..
REPORT MONTH October,1992 - ---
^
METHOD OF LICENSE CAUSE.& CORRECTI T DURATION SHUTTING EVENT SYSTEM COMPONENT ACTION TO PREVENTi NO. DATE TYPEl (HOURS) REASON DOWN' REACTOR REPORT # CODE 4 CODE 5 RECURRENCE ~
'06 10/24/92 'S 187'.3 B 1 N/A N/A N/A Shutdown for Mid--
cycle Outage.:.
'i
)
1 2 2 3 4&5-F-Forced .A-Equip Failure F-Admin 1-Manual Exhibit F & HL "
, S-Sched B-Main or Test" G-Oper Error 2-Manual Scram Instructions for C-Refueling- ..
_ H-Other 3-Auto Scram Preparations of' D-Regul atory . Restriction. 4-Continued Data Entry Sheet Ee0perator Training- 5-Reduced Load . Licensee Event Report ~
U .&; License Examination- 9-Other -(LER). File (NUREG-1022)'
q-' $ w = w e g % w 'm, -q