ML20214V454

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SALP Rept 50-352/86-99 for Feb 1986 - Jan 1987.Meeting Will Be Scheduled to Discuss Assessment & Util Plans to Ensure Improved or Continued Emphasis on Activities Having Positive Effect on Performance
ML20214V454
Person / Time
Site: Limerick Constellation icon.png
Issue date: 06/05/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20214V419 List:
References
50-352-86-99, NUDOCS 8706120105
Download: ML20214V454 (62)


See also: IR 05000352/1986099

Text

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ENCLOSURE

SALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NO. 50-352/86-99

PHILADELPHIA ELECTRIC COMPANY

LIMERICK GENERATING STATION

UNIT 1

ASSESSMENT PERIOD: FEBRUARY 1, 1986 - JANUARY 31, 1987

BOARD MEETING DATE: MARCH 17, 1987

8706120105 870605 ~

PDR ADOCK 05000352

G PDR

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TABLE OF CONTENTS

Page

I. INTRODUCTION ...... ................. 1

A. Purpose and Overview . . . . . ............ 1

B. SALP Board Members . . . . . . . . . . . . . . . . . . 1

C. Background . . . . . . . . . . . . . . . . . . . . . . 2

.

II. CRITERIA . .. . .... ................. 5

III. SUMMARY OF RESULTS .. ........ ......... 6

A. Facility Performance . . . . . . ........... 6

B. Overall Facility Evaluation ............. 6

IV. PERFORMANCE ANALYSES. . . . . . . . . . . . . . . . . . . . 8

A. Plant Operations . . . . . . . . . . . ....... 8

B. Radiological Controls ................ 12

C. Maintenance ... .................. 17

D. Surveillance . . . . . . . . . . . . . ........ 21

E. Engineering Support. ................ 25

F. Emergency Preparednesss ............... 28

G. Security and Safeguards ............... 30

H. Training and Qualification Effectivenesss ...... 34

I. Licensing Activities . . . ............. 37

J. Assurance of Quality ................ 41

V. SUPPORTING DATA AND SUMMARIES . . . . . . . . . . . . . . . 44

A. Investigation and Allegation Review ......... 44

B. Escalated Enforcement Actions ............ 44

C. Management Conferences . . . . . . . . ....... 44

D. Licensee Event Reports . . . . . ........... 45

E. Licensing Activities . . . . . . . . . . . . . . . . . 47

Tables and Figures

Table 1 - Licensee Event Reports .................. 48

Table 2 - Inspection Hours Summary ................. 54

Table 3 - Enforcement Summary . ................... 55

Table 4 - Inspection Activities . . .. ............. 57

Table 5 - Unplanned Automatic Trips and Shutdowns . . ........ 59

Figure 1 - Number of Days Shutdown ................. 60

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I. INTRODUCTION

A. Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an

integrated NRC staff effort to collect the available observations and

data on a periodic basis and to evaluate licensee performance based

upon this information. SALP is supplemental to normal regulatory

processes used to ensure compliance to NRC rules and regulations.

SALP is intended to be sufficiently diagnostic to provide a rational

basis for allocating NRC resources and to provide meaningful guidance

to the licensee's management to promote quality and safety of plant

construction and operation.

~

An NRC SALP Board, composed of the staff members listed below, met

on March 17, 1987 to review the collection of performance observa-

,

tions and data to assess the licensee performance in accordance

with the guidance in NRC Manual Chapter 0516, " Systematic Assessment

of Licensee Performance." A summary of the guidance and evaluation

criteria is provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at the Limerick Generating Station Unit i for the

period February 1,1986 through January 31, 1987. The summary

findings and totals reflect a 12-month assessment period.

B. SALP Board

Board Chairman '

.

W. F. Kane, Director, Division of Reactor Projects (DRP), ,

i

Members

i L. H. Bettenhausen, Acting Director, Division of Reactor Safety

! (DRS)

i R. M. Gallo, Chief, Projects Branch 2, DRP

!

C. J. Cowgill, Acting Chief, Reactor Projects Section 2A

J. R. Johnson, Acting Chief, Operations Branch, DRS

M. Shanbaky, Acting Chief, Emergency Preparedness and Radiological -

Protection Branch, DRSS

E. M. Kelly, Senior Resident Inspector

W. R. Butler, Chief, BWR Project Directorate No. 4

R. E. Martin, Licensing Project Manager, NRR

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Other Attendees'

S. D. Kucharski, Resident Inspector

J. H. Williams, Project Engineer.

L. Scholl, Reactor Engineer

F. Hebdon, AE00

R. Bailey, Physical Security Inspector

R. Keimig, Chief, Safeguards Section

W. Pasciak, Chief, Effluent Radiation Protection Section

T. Dragoun, Senior Radiation Specialist

J. Sweeney, Consultant

C. Background

1. Licensee Activities

The startup test program was completed, and commercial operation

was declared on February 1,1986, following performance of the

100-hour warranty run on January 23-28, 1986. The plant oper-

ated at full rated power through most of the assessment period

at a capacity factor of approximately 82%.

The one unplanned scram from power during the period occurred

on February 10, 1986'from 99.8% power on a high flux signal.

.

The high flux was the result of a pressure increase from tur-

bine control valve closure due to a momentary ground created

in the main turbine presture control system by a test engineer

who had been collecting turbine operating data. Following

reactor startup on February 11, the plant operated at full

rated power through May 2, 1986. A planned shutdown was

commenced on May 2, 1986, and a six-week scheduled outage

l was begun to perform surveillance testing. An unplanned

scram signal on low reactor vessel level occurred during the

i

subsequent cooldown (with manual level control using a single

i- feedwater pump) with all rods already inserted. The outage

l was completed within the scheduled time frame,.and major work

included replacement of all 14 main steam safety valves, over-

, haul of all 4 emergency diesels, and extensive surveillance

' testing. ,

Y

i Tbe plant aphieved full rated power operation on June 21, 1986

and operated until July 4, 1986 when the plant was shut down

, dde to an iicrease in unidentified drywell leakage. In

1

ad;11 tion to= replacing LPCI valve packing, a recirculation pump

i seal was replaced and on July 13 the plant returned to full

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power operaflon.

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Full power operation continued from July 1986 for a record 198

days until a controlled shutdown was begun on January 27, 1987

and a manual scram from 27% power was performed to repair

three valves found later to be contributing to the high

unidentified drywell leakage.

Plant load drops from full power were performed on several

occasions at the end of the assessment period. Control rod

pattern changes for the remaining rod groups still inserted in

the core were made to extend core life. End-of-cycle coastdown

began at the end of the period, as target burnup was reached and

all control rods were fully withdrawn. New fuel arrived onsite

on January 21-23, 1987. A license amendment to extend core life

by allowing increased core flow and partial feedwater heating

was submitted to the NRC on November 16, 1986 and was approved

i

shortly following the end of the assessment period.

Detailed preplanning was undertaken during the assessment

period in preparation for the initial refueling scheduled to

last 11 weeks and expected to begin in May 1987. The refueling

will involve a full core offload, approximately 80 system modi-

fications, and extensive testing and maintenance activities.

Organizational changes at the station level occurred through-

out the assessment period, including promotion of a new station

manager in April 1986. The licensee announced changes in

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November 1986 in PECO senior management associated with nuclear

programs. The Senior Vice President for Nuclear Power and the

Vice President (VP) for Electric Production retired, and J. S.

Kemper was appointed to a new position of Senior VP with three

new VPs reporting to him, effective on November 24, 1986.

Annual emergency preparedness exercises were held on April 3,

1986 and January 15, 1987.

i

Startup commenced on January 30, 1987 after being shut down

for 4 days to repair valve packing leaks, and power ascension

! to rated conditions was underway at the end of the assessment

l

,

period.

2. Inspection Activities

Two NRC resident inspectors were assigned to the site during

the assessment period. The total NRC inspection hours for the

12 month assessment period was 2781 hours0.0322 days <br />0.773 hours <br />0.0046 weeks <br />0.00106 months <br />. Distribution of

these hours for each functional area is depicted in Table 2.

During this assessment period, the first year of commercial

operations was covered. NRC teams evaluated two emergency

preparedness exercises, conducted on April 3, 1986 and January

15, 1987.

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A summary of enforcement activities is provided in Table 3,

followed by inspection activities in Table 4.

This report also includes assessment of " Training and Qualifi- *

cation Effectiveness" and " Assurance of Quality" as separate

functional areas. Although these topics are assessed in other

functional areas through their use as evaluation criteria, these

two areas are summarized separately to provide a synopsis. For

example, quality assurance effectiveness was assessed on a

day-to-day basis by the resident inspector and as an integral

part of specialist inspections. Although quality work is the

responsibility of every employee, one of the management tools

to measure this effectiveness is reliance on quality assurance

inspections and audits, Other major factors that influence

quality, such as involvement of first-line supervision, safety

1

committees, and worker attitudes, are discussed in each func-

tional area.

,

'

Engineering support was evaluated as a separate functional

area for the first time during this assessment period. Fire

Protection is assessed as part of Operations, as in the last

assessment, since there was only one programmatic inspection

in this area. Security continued to receive increased inspec-

tion effort, as in the previous period,.because of identified

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weaknesses.

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II. CRITERIA

Licensee performance is assessed in selected functional areas. Each

functional area represents areas significant to nuclear safety and the

environment, and are normal programmatic areas. The following evaluation

criteria were used as appropriate to assess each functional area.

1. Management involvement and control in assuring quality

2. Approach to resolution of technical issues from a safety standpoint

3. Responsiveness to NRC initiatives

4. Enforcement history

5. Reporting and analysis of operational events.

6. Staffing (including management)

7. Training effectiveness and qualification

Based upon the SALP Board assessment each functional area evaluated is

classified into one of these performance categories. The definitions of

these performance categories are:

Category 1. Reduced NRC attention may be appropriate. Licensee manage-

ment attention and involvement are aggressive and oriented toward nuclear

safety; licensee resources are ample and effectively used so that a high

level of performance with respect to operational safety is being achieved.

Category 2. NRC attention should be maintained at normal levels. Licen-

see management attention and involvement are evident and concerned with

nuclear safety; licensee resources are adequate and reasonably effective

such that satisfactory performance with respect to operational safety is

being achieved.

Category 3. Both NRC and licensee attention should be increased. Licensee

management attention or involvement is acceptable and considers nuclear

safety, but weaknesses are evident; licensee resources appear strained or

not effectively used so that minimally satisfactory performance with

respect to operational safety is being achieved.

The SALP Board has also categorized the performance trend over the

course of the SALP assessment period. The SALP trend categories are:

Improving: Licensee performance was determined to be improving near the

close of the assessment period.

Declining: Licensee performance was determined to be declining near the

close of the assessment period.

A trend is assigned only when a definite trend of performance is

discernible, and the SALP Board believes that continuation of the trend

may result in a change of performance level.

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III. SUMMARY OF RESULTS

A. Facility Performance

Functional Category Category

Area Last Period This Period

(12/1/84 - 1/31/86) (2/1/86 - 1/31/87)

A. Plant

Operations 1 1

B. Radiological

Controls 2 1

C. Maintenance 2 1

D. Surveillance 2 1

Not

E. Engineering Support Evaluated 1

F. Emergency

Preparedness 1 1

G. Security and

Safeguards 3 2

H. Training & Quali-

fication Effective-

ness 2 1

I. Licensing Activities 1 2

J. Assurance of Quality 1 1

1

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B. Overall Facility Evaluation

The SALP Board assessment confirmed a strong orientation toward

safe plant operation and found significant management, staffing, and

performance strengths in plant operations, maintenance, surveillance,

and emergency preparedness. Other functional areas, while rated

Category 1 on the strength of performance during the period, were

found to be so because of strong station management. Radiological

controls and engineering support are examples of functional areas

where strong corporate support will be necessary to sustain Category

1 performance. In most functional areas the licensee exhibited an

ability to predict problems by taking a proactive approach to

critically self-evaluate performance and institute effective

corrective actions to prevent problems from occurring.

Control room activities were observed to be at a consistently high

quality level. The conduct of business in the control room was

professional and improved over previous assessments. Operator

attitudes toward plant safety and cooperation with the NRC were

excellent.

Security exhibited poor performance in past assessments, necessi-

tating many program changes during the current assessment period.

Program improvements included increased oversight and direction of

the security contract force, as well as increased licensee manage-

ment involvement and enhanced training program enhancements. These

changes indicate to us the licensee's intent to develop and implement

a high quality security program. However, many of the changes

occurred late in the assessment period and their effectiveness has

not yet been assessed. Therefore, high management attention to the

program must continue to ensure that this level of effort is maintained.

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IV. PERFORMANCE ANALYSIS

A. Plant Operations (974 hours0.0113 days <br />0.271 hours <br />0.00161 weeks <br />3.70607e-4 months <br />; 35%)

1. Analysis

This area was rated as Category 1 during the previous assess-

ment period, concluding that staffing was at full complement,

control room activities were fully supported by technical

, personnel and strong management involvement, with demonstrated

ability to implement effective corrective action and perform

critical self evaluations. Areas needing improvement were

coordination between operators, on-shift communication, and an

increased recognition of Technical Specification requirements

under changing plant conditions. Operator license examination

failures during the previous period also reflected a recurrent

weakness in supervising refueling operations.

Plant operations and activities were monitored by the resi-

dent and region-based inspectors during this assessment period.

Station management continues to be visible in control room

activities, particularly during major plant evolutions. Technical

specifications and license conditions have been adhered to

consistently. Operators are cognizant of safety system status,

alarmed conditions, and equipment problems. Shift supervision

has responded with conservative decisions on operability when

, equipment problems arise.

There were two unplanned scrams during the assessment period.

The only scram from power occurred at the beginning of the

assessment period due to data collection that was not adequately

controlled, and has not been a recurrent problem. The second

scram occurred due to reactor vessel water level oscillations

with all rods inserted and the reactor in a shutdown condition.

1

In contrast, nine unplanned scrams occurred during the last

assessment period. The licensee is an active member of the BWR

Owners Group Scram Frequency Reduction Committee that convenes

quarterly to discuss root causes of scrams and successful

preventive measures. Good practices recommended or already

implemented at Limerick include: head sets for communication

between I&C technicians, test engineers and operators during

surveillances; adjustment of the main steam line high radiation

setpoint; protective cages around instrumentation racks and

reduction in the number of continuously lighted control room

annunciators. The result has been a marked reduction in

unplanned scrams.

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Control room routines were maintained at a high level. New

access controls were instituted during the period that were

effective in limiting non-essential personnel and noise, and

improved the conduct of business in the control room to correct

a chronic past problem. Improved access controls were notable

since Unit 2 control panels were under construction during the

last half of the period. Operator performance reflected high

morale and a cooperative attitude. Formalized shift turnover

procedures were implemented during the assessment period, and

turnovers have been crisp and professional. Operators have

found plant problems because of attention to detail in turn-

overs, such as a reactor water cleanup pump which had tripped

but was not annunciated, and a self-identified violation

involving chilled water isolation valves that had not been

properly isolated.

The plant operating review committee (PORC) has continued to

effectively keep safe plant operation as the highest priority,

and plant management regularly convenes the PORC when signifi-

cant issues arise. The closeout of the startup test program was

carried out with the same high quality as the conduct of the

program rated as Category 1 in the previous assessment. Staf-

fing levels and a tracking method were maintained such that the

PORC was able to assure that open test exceptions carried into

the operational phase were closed out or periodically reviewed

for status with technically adequate action plans for each open

test exception.

Licensed operator staffing has been maintained at a high level

to support safe reactor operation. Staffing for both units is

essentially in place; this allows for extra licensed expertise

in the control room to better handle collateral duties such as

the fire brigade, equipment blocking and release for mainte-

nance, and startups and shutdowns. Less use of overtime

occurred as compared with the last assessment period when the

plant was in a power ascension test program. Plant management

communicates effectively with shift supervision and control

room staff through daily meetings, as well as an end of the

week planning session for weekend activities. Shift technical

advisors (STAS) determine the scope of appropriate post

maintenance testing; and assist in event reportability, recon-

struction and emergency response. A new position of technical

assistant on shift (TAOS) was created at the end of the period

to allow the STA to remain in the control room with the shift

superintendent. The TAOS has assumed computer display and

offsite dose calculation responsibilities.

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Licensed training programs were accredited by INP0 in October

1986. One set of license examinations was given during the

, current assessment period; a total of 4 senior reactor opera-

<

tors, three reactor operator candidates and an instructor

certification were examined, and all pass,ed

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Fire protection was assessed as part of resident inspections

and one inspection by a region based fire protection specialist.

Deficiencies from the previous assessment for brigade members

who missed quarterly meetings and semi annual drills were

resolved by training makeup sessions. However, licensee manage-

ment does not appear to be thoroughly involved in activities

affecting the quality of the fire protection program, as evi-

i denced by the relatively large number of licensee event reports

(LERs) in this area and in particular the number of LERs issued

i

because of degraded fire barriers. It appears that, with proper

training and increased management involvement, some of the fire

protection related events could have been avoided. Additional

management attention is warranted in staffing, since the Fire

Protection Assistant position (left vacant a year ago) has not

1 been permanently filled. The position has been temporarily

filled by a technician who does not have State certification as

a fire brigade instructor. Also, the corporate Fire Protection

Engineer rarely visits the plant to review the program, or more

importantly, to monitor Unit 2 construction activities as they

may affect Unit 1.

Marked improvements were made in reducing the number of

unnecessary control room annunciator alarms, with a daily

, average of five or less nuisance alarms by the end of the

assessment period. Green plastic covers are used to identify

expected alarming conditions, and other colored markings for

which heightened response via alarm response procedures is

i necessary. Operators were responsive to, knowledgeable of the

'

cause of, and aggressively investigated equipment conditions

causing alarms.

! The licensee's performance is exemplary with respect to

! reportable events. Of the 50 prompt notification events

reported under 10 CFR 50.72, all were correctly identified

{ and properly analyzed. The high percentage of licensee event

reports (LERs) resulting from follow-up of the 10 CFR 50.72

reports indicates a thorough and careful reporting policy.

There also were few subsequent revisions of the LERs. None of

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the events reported was of unusual safety significance, and no

l events or problems specific to Limerick were considered

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significant. All of these considerations suggest that

corrective actions are effective.

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The plant was critical for 7365 hours0.0852 days <br />2.046 hours <br />0.0122 weeks <br />0.0028 months <br /> during the reporting

period and experienced an average of 0.14 unplanned scrams

with rod motion per 1000 critical hours. This scram frequency

indicates a well operated and maintained plant.

In summary, the quality of operations was evident throughout

the assessment period. A notable exception was fire protection

program activities, particularly barrier control, staffing and

corporate involvement. The number of reportable events

attributable to operator error was significantly reduced, and

the overall scram rate was extremely low.

2. Conclusion

1

Category 1

3. Board Recommendations

None,

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B. Radiological Controls (301 hours0.00348 days <br />0.0836 hours <br />4.976852e-4 weeks <br />1.145305e-4 months <br />; 10.8%)

1. Analysis

Overview

In the previous assessment period this area was rated as

Category 2. One minor weakness had been noted regarding

ineffective communication of h"alth physics (HP) control

requirements to the work groups. This weakness has been

recognized by the consistent efforts of the HP group to

improve communications at all levels, including timely

issuance of event reports for radiological incidents.

During this period there were several months of full power

operation and a 6-week outage which provided the opportunity

to assess the radiological controls program under other than

routine operational conditions. A total of six specialist

inspections were performed: two in radiation protection; two

in radwaste management and environmental monitoring; and two

in chemistry controls.

Radiation Protection

Low plant radiation levels and the lack of significant

contamination have allowed station management and HP super-

vision to focus attention on the nore hazardous work such

as neutron dete.ctor and recircula. ion pump seal replacements,

resulting in excellent control of work and low personnel

exposures. Total 1986 station exposure was approximately 70

man-rem, within the site management goal, due in part to the

onsite Senior Health Physicist who has been aggressive in

seeking cooperation and support from other site departments.

The HP department is fully staffed with permanent, qualified,

and dedicated personnel. A new director of corporate programs

was appointed at the end of the assessment period. Contract

personnel play major roles in the respiratory protection and

general employee training programs. No negative impact on the

quality of these programs has been noted due to good licensee

oversight of and qualification programs for the contract

personnel.

Corporate support was not evident in plant radiological control

activities, and is clearly lacking in programs to maintain per-

sonnel exposure levels as-low-as-reasonably-achievable (ALARA).

This issue is discussed further in Section IV.J, Assurance of

Quality. Regarding the ALARA program, there are no corporate

implementing procedures, as well as a lack of formal partici-

pation (from a site focus on work packages) by the Engineering

and Maintenance Departments. ALARA goals set by the site HP

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group are achievable and establish a level of excellence;

however, these goals do not receive formal corporate sanction

or involvement. HP procedures assign responsibility to the

site ALARA group to revise modifications to incorporate ALARA

considerations. However, the site HP ALARA group is unquali-

fied and undermanned for this task which is more appropriately

a responsibility of licensee corporate engineering departments.

Nonetheless, the oversight of plant activities by onsite ALARA

engineers and HP has been excellent.

Outaga work was effectively controlled due to clear and well

stated radiation work procedures, and the use of experienced

lead HP technicians and similarly experienced work crews.

Although radiological hazards are generally low, the tech-

nicians in charge of work took conservative precautions to

prevent workers from becoming lax in regard to radiation

protection. An overall positive attitude across all site

work groups has been reflected by their adherence to routine

HP controls. Sensitive automatic personnel friskers installed

at the power block main access passageway provide control of

very low levels of radioactive materials. However, the excel-

lent control afforded by this equipment is complicated by the

abnormally high level of naturally occurring radioactive

material (radon) found in the geographic area of the site.

There was a concern identified by the NRC during the May 1986

outage that heat stress of the workers, with primary containment

spot coolers secured, might compromise radiological controls.

The licensee responded with a comprehensive heat stress control

program expected to be administered during the 1987 refueling

outage.

The respiratory protection program reflects a conservative

approach to the control of intakes by workers with good proce-

dures and a sizeable force of well-trained contractors.

A well organized training program continues to make a positive

contribution to the effectiveness of the HP program. General

employee training and respiratory protection instructors must

complete a rigorous qualification program. The content and

presentation of training for workers is tightly controlled by

the corporate Nuclear Training Manual.

Audit programs appear to be effective in identification of

program weaknesses. Several problems with the control of high

radiation exclusion areas found during an NRC inspection had

been identified by the licensee one month earlier, and were

appropriately corrected by the end of the assessment period.

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Radioactive Waste Management and Environmental Monitoring

Program controls in processing and classification of radwaste

were well managed. Significant organizational improvements

were instituted at the end of the assessment period, including

a change to a separate line organization from the previous

matrix organization. A Radwaste Manual was' developed to

describe the conduct of operations, position responsibilities

and program requirements. Management directed oversight /

approval of all radwaste discharges, review of performance

indicators associated with the water balance program, and a

published goal / commitment to become a "zero-release" (i.e.,

no radioactive liquid discharges) plant. Staffing was complete,-

with minimal reliance on contractor personnel. The non-licensed

operator training program, which applies to radwaste operators,

received INP0 accreditation during this assessment period.

Technical support was also in place to identify radwaste equip-

ment problems, establish unique priorities for work requests and

identify equipment improvements. Continued radwaste program

improvements to minimize dry active waste include plans for a

super-compaction facility shared between the Peach Bottom and

Limerick stations.

An inspection of the licensee's radiological environmental

monitoring found consistent application of the program. Quality

assurance of the environmental thermoluminescent dosimetry (TLD)

-measurements is supported by two well-recognized comparison

programs. No administrative offsite dose limits were approached,

and radioactive waste shipments have been in compliance with the

state requirements of South Carolina and Washington.

Chemistry Controls

The licensee has developed and is implementing a site-specific

water chemistry control program which follows EPRI and industry

consensus standards. The onsite effort represents a significant

improvement in resin controls, limiting chlorides, better trend-

ing of solids and conductivity, and overall water quality since

the last assessment. Review of plant chemistry performance and

trends is routinely performed by station management.

Technical support to the station for resolution of post

accident sampling system (PASS) reliability was not coordinated

until identified and highlighted by the NRC. The licensee had

not been able to satisfactorily complete surveillance tests to

demonstrate PASS operation throughout the assessment period due

to recurring component failures. By the end of the assessment

period, licensee management directed the appropriate resources

and had developed a thorough corrective action plan, including

completing the surveillances and initiating system modifications,

f

.

.

15

The licensee's capability to analyze non radiological chemical

parameters in various plant systems was reviewed. The results

of the standard measurements comparison showed six out of four-

teen disagreements. The disagreements occurred in the metal

analysis area and were caused by poor attention to calibration

and a lack of appropriate measurement control charts. Another

problem was related to the licensee setting an arbitrary ten-

percent control value rather than a statistically useful con-

trol value. The problem of control charts was identified in

an inspection during the previous assessment period. These

problems could have been avoided with more attention to quality

control details at the site or with better corporate involve-

ment, in addition to a more timely followup of identified

problems.

Personnel performance in chemistry was very good, even with

roughly half of the licensee's staff (at the Support Chemist

and ANSI technician level) as contractors. The licensee

received INP0 accreditation for their chemistry training

program. Permar.ent (licensee) chemistry staffing is nearing

final goals and should improve upon completion of the required

training and qualification. QA surveillances at the beginning

of the assessment period identified significant weaknesses in

the plant chemical control programs which have been

subsequently strengthened.

Summary

Low radiation and contamination levels have allowed management

focus on and excellent control of radiological work, resulting

in low personnel exposures. Effective qualification and train-

ing programs have allowed for good oversight of contractors and

positive attitudes among site work groups with respect to HP

controls. While audit programs are identifying some program

weaknesses, appropriate corporate support and involvement with

radiological and ALARA programs was not evident. Moreover, site

radiological controls and ALARA oversight were effective, in

spite of the absence of corporate sanctions, because of strong

station HP group management.

!

i

Radwaste program improvements continued to be implemented

throughout the assessment period, as were chemistry practices,

although increased corporate direction or assistance in those

, areas was warranted by virtue of problems experienced with

4

laboratory QC and PASS reliability.

!

l

I

i

b.

_ _ _ _ _ _ _ _ _ __ _ _

,.

.

-

16

2. Conclusion

Category 1

3. Board Recommendations

Licensee: See Section IV.J, Assurance of Quality

NRC: Continue the routine inspection program, considering

expected increased challenges associated with the 1987 refueling

outage.

. . . . . . . . . . __--

.

-

17

C. Maintenance (362 hours0.00419 days <br />0.101 hours <br />5.98545e-4 weeks <br />1.37741e-4 months <br />; 13%)

1. Analysis

This area was rated Category 2 during the last assessment

period. No concerns were identified during that assessment,

and, overall, maintenance programs were judged to be function-

ing well.

The resident inspectors reviewed routine plant maintenance

during the present assessment, and there was one programmatic

inspection by a region-based specialist. Mainter;ince activi-

ties were more extensive than in the previous period, as craft

supported two outages; one a six week surveillance test outage

and the other a one-week recirculation pump seal and packing

replacement outage.

Careful and well-controlled maintenance programs have resulted

in quality work during the assessment period. Program chal-

1enges have been met by maintenance personnel as indicated

by a lack of equipment deficiencies and excellent plant reli-

ability and availability. There were no scrams attributable

to this area, nor was there a backlog of safety related

corrective maintenance. No examples occurred of recurrent

failures involving rework or excessively drawn-out job

schedules. Maintenance supervision demonstrated effective

work planning, responded capably to contingencies, and main-

tained an adequately staffed craft organization.

Maintenance was well-managed during the assessment period.

Maintenance craft accumulate the largest percentage of the

station's radiation exposure, and thus ALARA is a principal

goal within the Maintenance Division. The ALARA goal was

ambitiously set and slightly exceeded due, in part, to a

large number of unanticipated reactor water cleanup system

pump repairs. However, a vendor representative was consulted

and, by eventually improving operating and maintenance proce-

dures, no additional pump seal failures were experienced during

the last quarter of the assessment period. Other targeted

management goals included minimizing the use of contractors and

eliminating excessive craft overtime. A new onsite maintenance

supervisor was appointed at the end of the assessment period

who has applied valuable quality control (QC) and maintenance

experience to that position.

Significant demands for maintenance were met during the assess-

ment period as evidenced by performance during the six-week

mint-outage and major equipment repairs, including: the

replacement of a recirculation pump seal, the replacement of

all 14 main steam safety relief valves; the overhaul of all

four emergency diesel generator engines; and, rework of

.___-_________ _ _ _ _

.

-

18

feedwater check valves and the main steam isolation valves

(MSIV's). Generic information was factored into maintenance

programs to promptly surface safety concerns, and effective

vendor interface controls were evident in these major repairs.

Maintenance work has been extensive during the assessment

period. Over 3500 preventive and corrective maintenance

activities were completed, and with essentially no backlog of

outstanding safety related corrective maintenance. Work is

centered about a computerized program for history and mainte-

nance planning (CHAMPS) that is also used to track maintenance,

equipment history, failure trends, and scheduling of resources.

A computer generated maintenance request form (MRF) has proved

to be an efficient means of interfacing between plant staff,

quality control, maintenance planning, and operations. Routine

work is coordinated through a series of meetings during the day.

The meetings serve not only to effect proper interface among

organizations on site, but also improvements in scheduling and

maintenance craft morale. Work controls have been effective,

particularly with respect to post-job critiques and work

planning. Accurate appraisals of actual versus estimated job

hours have been provided through the use of CHAMPS. Job dur-

ation has been optimized by responsive health physics coverage,

turnover of equipment, and effective engineering support.

Accurate job planning has enabled effective utilization of craft

resources.

i

Maintenance Division senior management have extensive experience

in nuclear maintenance. The Division, which consists of over

1100 personnel, has doubled in size in the past six years and is

currently organized such that a significant mobile resour:e of

craft are available on short notice for maintenance contingen-

cies and outages. As of the end of the assessment period, site

maintenance was comprised of approximately 120 craft and 20

technical personnel. Competent maintenance engineering support

was evidenced by complex and difficult in place repairs to a

high pressure coolant injection (HPCI) isolation valve which

were technically well conceived. The licensee has also recog-

nized the need to plan for future growth within craft ranks by

the addition of 29 entry-level Helpers currently in an on-the-

job training progression.

Well-developed maintenance procedures have been prepared using a

unique procedure writer's guideline. Maintenance procedures

have been found to be sufficiently detailed, particularly in

those cases of complex maintenance such as MSIV refurbishments,

diesel overhauls, and safety relief valve replacements. Lessons

learned have been factored into procedures based on plant

experience, such as the recirculation pump seal replacement and

control rod drive overhauls, as have Peach Bottom experiences.

The absence of any scrams attributable to maintenance activities

reflects, in part, carefully developed procedures.

. _- . ._. _ _ _ _ _ _ _ _ _ _ __ - - _ _ . - - _ - . _ _ - _ - -

_ _ _ _ _ _ _ _ _

.

4

-

19

3

i

i

Craft training programs were accredited by INPO during the

'

assessment period. Training initiatives'have included pur-

chase of a plastic recirculation pump seal training aid and

plans to purchase a spare MSIV. A dedicated training facility

!

' at Barbados Island (a decommissioned fossil station) is

equipped with Limitorque valves and other plant equipment for

"

hands-on training. The instructor to student ratio is excel-

lent, at approximately I to 4. Formal classroom and on-the-job

training are a part of a craftsman's progression to journeyman.

Specialty training has also been provided whert necessary, as

for example with refuel floor, snubber rebuilding, pump seals

and control rod drive work.

'

Housekeeping was maintained at a consistently high quality

level through persistent management attention, establishment

'

of administrative controls including a housekeeping committee,

!. and the effective use of a contract cleanup crew. As a result,

i

there existed few hazards to fire, equipment and personnel

safety during the assessment period. The licensee assured a

continued level of good housekeeping, even with more difficult

i

conditions dictated by refueling outage preparations, by use

l of a plant area concept accountable within the maintenance

organization.

Quality audits and surveillances have given extensive coverage

4

to maintenance activities. QC is involved in all safety-related

, maintenance via the MRF processing system. Quality trending

j reports during this assessment have analyzed findings over a

3 two year period, assessing maintenance errors as a declining

, trend. The majority of quality findings in maintenance are

a

related to the control of heavy loads at Limerick, and manage-

ment accordingly initiated training to address the deficiencies.

t

! In summary, maintenance programs were challenged more fre-

, quently during the current assessment period, and proved to be

t

a strength as evidenced by a lack of equipment problems caused

by maintenance, excellent plant reliability, and the lack of

, rework. Safety-related work was properly prioritized and

i planned. Efficient supervision of qualified craft resulted in

! effectively implemented procedures. No instances were identi- '

I fied where maintenance caused equipment or system inoperability.

Consistently good engineering support was evidenced by well-

planned and executed major repairs. Control of the removal

j from and return to service of safety related systems (including

post-maintenance testing) was a consistent program strength,

i

'

l

!

- _ - - . .-

<

.

-

20

2. Conclusions

Category 1

3. Board Recommendations

None

.

.

21

D. Surveillance (429 hours0.00497 days <br />0.119 hours <br />7.093254e-4 weeks <br />1.632345e-4 months <br />; 15.4%)

1. Analysis

Surveillance was rated Category 2 during the previous

assessment. Concerns were expressed with management of

troubleshooting activities, controls on valve positions

and independent verifications.

Test programs were reviewed by resident and region-based

inspectors during the present assessment period. Specialist

inspections covered the surveillance test and calibration

control program, and containment local leak rate testing

during the six week May 1986 mini outage.

A well-managed surveillance test program was conducted during

the assessment period. This is evidenced by the 40% fewer

LERs than last assessment period, the fewer number of missed

surveillances, and the absence of emergency core cooling system

(ECCS) actuations and reactor scrams caused by testing. One

unplanned scram was caused by improperly controlled trouble-

shooting at the beginning of the period. Tighter management

controls on troubleshooting, including the requirement for a

troubleshooting control form approved by shift supervision,

prevented similar problems for the remainder of the period.

There were few unplanned actuations of safety systems

(9 reportable events or 16% of all LERs, principally inad-

vertent isolations) caused by test errors. Scheduling and

control of surveillance testing has been excellent and there

have been very few missed or late tests (of the 16,000 sur-

veillance tests run annually). Routine testing is scheduled

so as to minimize impact on plant operations. Complex testing

has also been rescheduled for dayshift during the week when

plant management is more immediately available should signifi-

cant problems arise.

The program has been successful in uncovering equipment prob-

lems, such as the residual heat removal (RHR) service water pump

flow blockage. Questionable test results receive proper super-

visory attention. Evaluation of test results and anomalies

have resulted in accurate identification of root cause, and the

licensee has made conservative decisions with regard to system

operability when test results were marginal.

The licensee maintains useful surveillance records enabling

effective trending of test results when equipment problems

were noted. Examples where test data were effectively

utilized included the reactor protection system (RPS) power

supply breakers and the containment purge system isolation

valves, both the subject of 10 CFR Part 21 reports during the

period. The licensee was also able to reconstruct accurate

s

..

. 22

,

~

test records to appraise potentially adverse trends on operation.

This was evident in an average power range monitor (APRM) noise

event involving an unexplained half-scram signal wherein a study

of past testing helped to confirm proper RPS response in spite

of seemingly anomalous results.

The licensee conducts thorough and effective testing of systems,

using procedures containing sound technical detail. Technicians

are well-trained and qualified, and good communications has been

established with licensed operators. Technicians have (in all

cases) suspended testing, and informed control room supervisicn

prior to resumption of testing, when erroneous system responses

have occurred. This practice has enabled prompt assessment of

root cause for equipment malfunctions and timely reconstruction

of sequences of events. In most reportable events during this

period involving test technician errors, the licensee's staff

comprehensively determined root cause, and this has been a

factor in reducing repetitive occurences and improving proce-

dural inadequacies. Test procedures are developed to the point

that, with improvements in human factors, incorporation of

vendor recommendations and embodied precautions, high confidence

in test procedures has been reached. The sub-PORC concept has

assured that procedures remain technically sound by better

attention to procedural detail on the part of responsible

engineers and work groups prior to presentation to the

full review committee.

There have been instances where communications between test

and control room personnel have led to violations (identified

by the licensee), but these have been corrected and have not

been recurrent. In response to one reportable event during

the assessment period, the licensee provided timers in the

control room that better administratively control the two-

hour limit associated with channel functional testing.

There have been fewer reportable events associated with test-

ing as compared with the last period, and the majority of these '

events have involved either fire protection or toxic gas detec-

tion systems. Reportable events in the fire protection area

were due to doors that were propped open and improperly con-

trolled, missing barriers and seals, and surveillances that

were missed due to poor communications. Moreover, there were

a relatively high number of reportable events (see causal anal-

ysis discussed in Section V.D.2.b) attributable to chlorine or

toxic gas detector design deficiencies. As a result, the

licensee has expended a considerable effort in maintaining these

state-of-the-art systems. New chlorine electrolyte probes were

installed at the beginning of the period to improve the reli-

ability of a previous system involving a tape which broke

frequently (and the source of numerous events). The licensee

continued to address toxic gas detector design problems at the

,

-

w

..

. 23

end of.the assessment period by increasing test surveillance

intervals and vendor / engineering involvement.

Previous problems associated with the temporary procedure con-

trol (TPC) process have been corrected. PORC review has been

effective in maintaining test procedure changes to a minimum.

Administrative processes to troubleshoot or to utilize TPCs,

when necessary, are not cumbersome and have also contributed to

procedure improvement. Previously experienced problems asso-

ciated with instrument valve manipulations have been eliminated

by the creation of a valving school and by restricting root

valve manipulations to instrumentation and control (I&C) tech-

nicians, as only one instance occurred curing the period in

which mispositioning an instrument root valve caused a report-

able event. The licensee also has substantial capability in

the area of performance data gathering and trend analysis, such

' as with the vibration monitoring program, chemistry database

, _

management system and emergency diesel engine testing.

The licensee reported a number of self-identified violations

involving testing. With the excaption of fire protection

barriers and doors, none of the test discrepancies were

repetitive or indicative of a larger breakdown and attest to

the licensee's continued ability to self-identify and correct

problems. An effective concept for correcting the cause of

test errors has been the use of roundtable discussions between

I&C technicians and engineers. For example, a drywell airlock

door leak rate test was six weeks overdue, but was discovered

because the licensee had not had a large backlog of overdue

surveillance tests and was adequately staffed to review test

schedules and find these isolated examples. A retest of the

airlock was promptly performed, scheduling program errors were

corrected, and the event was accurately reported. The licen-

see's program (STARS) for scheduling and. tracking surveillances

assists in assuring that tests are performed on schedule. The

coordination of the test program, across all disciplines, is

very strong due, in part, to the importance placed on the pro- '

gram by licensee personnel and the assignment of an engineer as

a dedicated surveillance test coordinator.

In summary, surveillance testing has been successful in reli-

ably confirming operability and uncovering equipment problems.

The program is extensive yet well centrolled, and personnel

are qualified and conservatively conduct testing. Staff and

shift supervision are appropriately involved, engineering eval-

uations are solicited when necessary, and staffing is adequate

to support test schedules. Testing is integrated into day-to-

day operations of the plant without unduly affecting reactor

operation. The relatively few instances of missed surveillances

are not a programmatic concern in an otherwise excellent test

program.

.

x

.

.-

24

2. Conclusion

Category 1

3. Board Recommendations

None

n'

'

.

. 25

E. Engineering Support (61 hours7.060185e-4 days <br />0.0169 hours <br />1.008598e-4 weeks <br />2.32105e-5 months <br />; 2.2%)

1. Analysis

This area has not been rated in previous assessments. During

this assessment period the resident and specialist inspectors

reviewed the plant modification and design change process, and '

assessed engineering support for plant operations, maintenance

activities, and the upcoming initial refueling outage. j

Corporate engineering and design support has been previously

noted to be strong, and the company is highly engineering-

oriented. Engineering issues have been effectively dealt with ,

during this assessment, such as safety relief valve setpoint I

drifts and safety evaluations to support continued plant oper-  !

ation such as for the extension of the reactor core isolation

cooling (RCIC) system high energy line break boundary. One I

unplanned scram was attributed to a design limitation in

feedwater level control and, as a result, the licensee is

considering installation of additional startup level control

valves.

Plant modifications have been implemented throughout the

assessment period, with minimal impact on plant operations.

Detailed preplanning and design was performed for the large

number of modifications planned for the first refueling out-

age scheduled in May 1987. The most extensive modification

for the outage involves tie-in of the standby gas treatment

system to the refueling floor volume, a license condition

required to be implemented prior to moving irradiated fuel.

Over 85% of the modification was completed as of the end of

the assessment period, well in advance of the outage, and is

typical of design changes which are completed such that there

are more pre-engineered modification packages than there are

opportunities or staff to install them.

Major modifications are performed by an experienced onsite

Construction Division staff, consisting of approximately 65

permanently assigned craft personnel that are supplemented by

contractors to support outage activities. The construction

superintendent has been onsite at Limerick for 9 years and has

had previous experience at Peach Bottom. The group performs

extensive advance planning and utilizes the concept of a

Construction Job Memorandum to summarize work scope for field

personnel. The group has been successful in coordinating

among the licensee's matrixed organizations with minimal

impact on plant operations, and has as a goal to levelize

manpower during the upcoming refueling outage, accomplishing

as much work in advance as practicable. Walkdowns of systems,

and effective communications among work groups including daily

participation in planning (TRIPOD) meetings, have served to

-- - - . - . _ _ _ - -- . - _ _ - - -

.

.. 26

accomplish this goal. Design changes were implemented without

extending the critical path schedule during the May 1986 outage,

and have been practically integrated-into the projected schedule

for the refueling outage.

Safety evaluations associated with system changes are suf-

ficiently detailed, giving evidence of the strong corporate

engineering resources from which the licensee can draw for

design support. A Field Engineering group is also available

for electrical design and modifications. This group has con-

sistently provided expertise to solve safety system problems.

Examples included: various relay and logic problems; the

reactor protection system (RPS) power supply breakers that were

modified to more reliably open to protect the hydraulic control

unit scram solenoids; and, the average power range monitors

noise event that produced an unexplained half-scram signal and

detailed questions relating to proper RPS' response. This group

is also responsible for Limitorque motor-operated valve (MOVATS)

testing and troubleshooting, as well as reactor protection

system inverter operation and safety-related breaker design and

maintenance.

Engineering problems were experienced during the assessment

period as evidenced by Unit 1/2 interface contamination

incidents. The configuration of isolation devices in these

piping systems cross-connecting common unit systems were such

that internal contamination was allowed to migrate in several

instances to the radiologically uncontrolled Unit 2 side of

the piping systems. The licensee assembled a group to investi-

gate the short term and long term actions necessary to ensure

that Unit 1/2 interfaces are maintained isolated. Also, in

response to NRC concerns near the end of the assessment period,

corporate engineering developed a plan to address chronic PASS

reliability problems that had not been appropriately recognized

and brought to licensee management's attention.

There was a large number of LERs attributable to chlorine or

toxic gas detector design deficiencies, and the licensee has

.

expended considerable effort in these state-of-the-art systems.

l New chlorine electrolyte probes were installed at the beginning

of the period to improve the reliability of a previous system

j involving a tape which broke frequently (the source of numerous

LERs). The licensee continued to react to these design problems

at the end of the assessment period by increasing vendor and

l engineering involvement.

'

An item of concern involved the generation of new computer- 1

l drafted process and instrument drawings (P& ids) which were found

l near the end of the assessment period to contain a substantial

number of errors. In response, the licensee undertook

immediate review of the drawings, red-lined copies in the

,

.

.

. 27

control room and emergency response facilities, and undertook a

program to permanently correct the drawings. No operational

safety problems were identified as a result of these drawing

errors. Engineering design controls and quality program effec-

tiveness were being reviewed by the licensee at the end of the

assessment period to preclude similar future errors.

As noted in the last SALP report, the Technical Engineering

group continues to be a valuable source of engineering knowledge

in the operation and test of plant systems. Further, the way in

which onsite programs are organized (i.e., the matrix organi-

zation) integrates engineers into all site activities. For

instance, the plant engineer-maintenance has a staff which

provides engineering support for Unit 1 maintenance. In

parallel, the Maintenance Division has a self-contained engi-

neering group. Both groups of engineers constitute a source

of engineering support for Unit 1 maintenance which is separate

and distinct from corporate design engineers. This is a typical

organizational structure of the licensee and is indicative of

strong engineering within the company.

The licensee updated the " Level 1" portion of the probabilistic

risk assessment (PRA) in September 1986, modifying system fault

trees to reflect as- built system designs and revising accident

sequence event trees to include: consideration of the emergency

operating procedures; an updated station battery life estimate;

and, a changed MSIV closure setpoint. The result of the update

was a reduction by a factor of 3 in the calculated core damage

frequency, and additional insights into initiating events. The

licensee plans to use the current PRA as an analytical tool for

cost / benefit analysis on design changes, evaluating changes to

the technical specifications, and providing a prioritization

method for an integrated living schedule for licensing actions.

In summary, the licensee is strongly oriented toward engineering

and has effective engineering support integral to all disci-

plines in addition to the historically strong corporate design

engineering function. Engineering activities of the assassment

period were escalated, particularly in the second half, as

extensive planning and implementation of modifications for the

first refueling outage were underway.

2. Conclusion

Category 1

3. Board Recommendations

,

None

,

!

.. _ . _ _ . _

i

.

.

28

1

1

F. Emergency Preparedness (326 hours0.00377 days <br />0.0906 hours <br />5.390212e-4 weeks <br />1.24043e-4 months <br />; 11.7%)

1. Analysis

Licensee performance in this area was rated as Category 1,

(consistent) during the previous assessment period based

principally upon support and guidance by the licensee's

corporate staff, as well as the licensee's own initiatives

in emergency preparedness.

During the current assessment period, there were three region-

based inspections that observed two emergency exercises and a

remedial medical drill.

Performance during the annual exercises has reflected success-

ful planning and management of emergency preparedness (EP),

and demonstrates the licensee's ability to respond. Response

personnel were knowledgeable in their duties and in use of

implementing procedures; an indication of an effective train-

ing program. In both exercises, the Emergency Director and

Emergency Coordinator provided conservative, decisive technical

support to operators in mitigation of degrading scenario events.

Decision-making by key licensee responders; effective command

and control of the emergency facilities and organization;

accurate protective measures for workers and protective action

recommendations for the public; and, timely notifications to

offsite authorities are all program strengths. Although minor

exercise deficiencies were identified, the licensee corrected '

these by providing additional training in areas in which

improvement was needed. Senior licensee staff and management

were present at both exercise critiques.

The Station Manager has emphasized training, cooperation, and

the importance given to emergency response. The corporate staff

provides strong direction for the program, supports scenario

development, and maintains current status on the state of off-

site preparedness. The site Planning Coordinator has effectively

maintained EP procedures and integrated changes into the EP

'

training program which have been identified through drills and

exercises. Implementing procedures have been improved based on

feedback from drill evaluations and this process has improved

the overall state of emergency preparedness at Limerick.

Emergency planners have successfully coordinated with all

matrix organizations, working towards solving problems such as

crowd control in the Operations Support Center (OSC) and radio

communications. A problem noted during the assessment period

involved coordination between corporate security and site

operations regarding the assessment of bomb threats and the

declaration of an unusual event. However, steps were in effect

at the end of the period to effectively resolve this issue with

,

.

.

29

all parties concerned. During a bomb threat that occurred in

December 1986, control room supervisors were knowledgeable of

emergency and security plan details, and decisive in initiating

searches and recognizing appropriate emergency action levels.

The dedicated emergency response facilities have been maintained

in an adequate state of readiness through the period. Communi-

cations and computer-based assessment equipment availability are

given a high priority. The licensee also conducts quarterly

training exercises, which has been reflected in the strong

leadership evident by senior staff participation in the

Emergency Director position.

In summary, the license has maintained a high state of emer-

gency preparedness. Personnel have displayed evidence of good

training, attitude, and dedication to this functon. Emergency

preparedness activities are well integrated in day-to-day plant

activities, and are part of the routine PORC agenda. Strong

corporate direction of the onsite programs and offsite functions

has resulted in a program which has matured over past assessment

periods.

2. Conclusion

Category 1

3. Board Recommendations

None

_ _ . .

.

. 30

G. Security and Safeguards (328 hours0.0038 days <br />0.0911 hours <br />5.42328e-4 weeks <br />1.24804e-4 months <br />; 11.8%)

1. Analysis:

During the previous SALP, Category 3 concerns were identified

for weak management oversight of contractor activities, and

a lack of willingness to address long-standing program

shortcomings. As a result of escalated enforcement at the

end of the previous period, the licensee initiated aggressive

actions during this SALP period to address those concerns and

to improve the program overall.

During this assessment period, three routine, unannounced

physical protection inspections were conducted by a regional-

based inspector. Routine resident inspections were performed

throughout the assessment period.

The licensee and the security force contractor have aggressively

pursued a planned course of action to identify the root causes

of their previously identified poor performance. To improve the

overall performance of the security organization, the licensee

developed and implemented several significant changes.

Senior corporate officials affirmed their support for and

intent to implement an effective security program at both of

its nuclear generating stations by initiating a reorganization

of corporate responsibilities. The Manager of Nuclear Support

was given the responsibility to establish a security organiza-

tion that would be headed by a Director. The role of the

Director of Nuclear Security was defined, and assigned respon-

sibility for the management and oversight of the PECO nuclear

security program. A technical analyst was assigned to assist

the Director.

In conjunction with this change, the licensee allocated large

capital expenditures and authorized eight shift security assis-

tant supervisor positions to provide 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> oversight of the

contract security force, three of which were filled at the end

of the assessment period. The responsibilities of these super- ,

visors include assuring that the contractor properly implements

the licensee's security program and that the security force

maintains a high level of performance. In addition to the PECo

supervisors, the licensee's senior onsite security representa-

tive, the Nuclear Security Specialist, was also assigned a

staff of four technical assistants. These technical assistants

are responsible to monitor key aspects of the security program

on a day-to-day basis. The development and implementation of

this expanded PECo oversight organization, along with the

corporate changes, is evidence that the licensee is attempting

to implement a sound security program that goes beyond minimum

.

. 31

compliance with NRC requirements. However, these changes are

very recent, and, therefore, their impact on the program has

not yet been assessed by NRC.

Additionally, to instill in the security force personnel a

strong sense of purpose and a clear understanding of their

roles and responsibilities, the security force contractor made

changes to its supervisory staff, implemented numerous human

factors improvements and refined the training program.

To combat earlier problems of low morale and job dissatisfaction

in the security force, the contractor addressed employee con-

cerns regarding pay, benefits and human factors. Overtime hours

were substantially reduced and additional personnel were hired

to meet Unit 2 security duties previously assigned to members of

the Unit 1 security force. As a result of continued support of

the security program by the plant manager and other plant func-

tional groups, as well as the improvements made to the program,

the morale of security force personnel appears to have improved,

as demonstrated by a professional and dedicated demeanor.

The licensee also required its contractor to refine the train-

ing program. Two noteworthy refinements are the development

of a training program curriculum to define the purpose and

performance objectives of the program, and the initiation of

routine random testing of security force performance and

qualification criteria. The results appear to be effective,

as evidenced by the greater awareness of duties and a more

responsible attitude displayed by security force personnel.

The licensee's training program is carried out by individuals

who are experienced and assigned to security training only.

Training facilities have adequate classroom space. Lesson

plans are fairly well developed, generally thorough, and kept

current through feedback from supervisors and quality assurance,

and from the on-the-job performance testing. Random testing is

a significant program enhancement that has improved the perform-

ance and self-confidence of security force members. Security

procedures and instructions were recently revised to be more

clear and concise, which should enable members of the security

force to improve their performance.

Overall, the licensee, and its contractor appear to be addres-

sing the major security program shortcomings experienced in the

past. The licensee's efforts in this regard are significant but

management attention must continue at the current level.

Security management continued to be actively involved in

industry and NRC initiatives dealing with nuclear security

programs. This provides evidence of support for the secur-

ity program at a high level in the licensee's organization.

Management personnel also exhibited a clear understanding

..

.

32

and conservative approach to technical security issues as

evidenced by their handling of security matters that evolved

as a result of the resumption of Unit 2 construction. The

licensee's approach to resolution of those matters was

noteworthy. A very clear and comprehensive plan was devel-

oped, integrated with other plant functional and construction

groups and subsequently reviewed on-site with NRC representa-

tives before being implemented. This approach was extremely

effective in preventing numerous problems that are usually

encountered under such circumstances.

The licensee submitted four security event reports pursuant

to 10 CFR 73.71(c) during the assessment period. One report

concerned the misidentification of a vital area door; another

concerned a minor delay in response to an alarm because of a

miscommunication; the third identified the discovery of a

weapon during the search of a vehicle prior to entering ti.9

plant protected area; and the fourth reported a non-credible

bomb threat. In all cases, the licensee's compensatory

measures were timely and appropriate. The reports to NRC

were prompt, clear, and thorough. These reports have shown

considerable improvement during the assessment period.

Inspector reviews of the security incident files found that

the NRC-approved security plan was being properly implemented.

The lack of systems and equipment-related event reports during

this period is noteworthy, and evidence of increased licensee

attention to preventive maintenance and surveillance testing.

During the assessment period, the licensee submitted two

revisions to the Security Plan under the provisions of 10

CFR 50.54(p) and provided its response to the August 4,1986

Miscellaneous Amendments to 10 CFR 73.55 codified by the NRC.

The licensee's corporate security staff is responsible for

ensuring that Plans are current, and for coordinating changes

when required. The staff is very effective in carrying out

this responsibility. They often communicate and review Plan

changes with regional licensing personnel to ensure a clear

understanding and, when the Plan changes are submitted to NRC,

they are of good quality, indicative of a thorough review and

good understanding of NRC security performance objectives.

In summary, the licensee has implemented many program changes

and pursued many program improvements during this assessment

period. Increases in program oversight and direction, manage-

ment involvement and support, and enhancement in the training

program all served to demonstrate the licensee's desire to

develop and implement a high quality security program with a

well qualified and dedicated, professional force. However,

many of those changes occurred late in the period and the

effectiveness of the changes has not been assessed. Therefore,

-___ -_ - __ _ _ _ _ _ - _ _ - _ _ _ .

.

.

33

high level management attention to the program must continue

to ensure that the current level of effort to improve the

program is maintained.

2. Conclusions

Category 2

3. Board Recommendations

Licensee: Continue to evaluate the effectiveness and impact

of security program changes.

NRC: Maintain existing inspection effort.

I

i

_ . _

_ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

. 34

H. Training and Qualification Effectiveness

1. Analysis

The various aspects of this functional area have been considered

and discussed as an integral part of the other functional areas

and the respective inspection hours have been included.in each

one. Consequently, this discussion is a synopsis of the assess-

ments related to training conducted in other areas. Training

effectiveness has been measured primarily by the observed per-

formance of licensee personnel and, to a lesser degree, as a

review of program adequacy. This discussion addresses three

principal areas: licensed operator training, non-licensed

staff training, and the status of INP0 training accreditation.

,

During the previous assessment period, training and qualifi-

l cations effectiveness was considered as a separate functional

area for the first time and rated Category 2. Training and

qualification effectiveness continues to be an evaluation

criterion for each functional area. The previous assessment

recommended refresher training in refueling operations and

core alterations in preparation for the first refueling outage,

as well as increased emphasis on Technical Specifications for

licensed personnel. The current assessment is based on resident

I

and specialist observations as well as two specific inspections

of nonlicensed and maintenance training programs.

Fire protection training was assessed as part of one inspection

by a region based fire protection specialist. Deficiencies from

the previous assessment for brigade members who missed quarterly

meetings and semi annual drills were resolved by training makeup

sessions. However, licensee management does not appear to be

thoroughly involved in activities affecting the quality of the

fire protection program, as evidenced by the relatively large

number of licensee event reports (LERs) in this area and in

particular the number of LERs issued because of degraded

barriers. It appears that, with proper training and increased

management involvement, some of the events could have been

avoided.

During the current assessment period license examinations were

given to four senior reactor operator (SRO) candidates, three

reactor operator (RO) candidates and an instructor certifica-

tion, which all passed. Emergency procedure use continued to be

a licensee strength, as was knowledge of specific systems in

written exams. Knowledge of technical specifications was also a

notable strength which is an improvement from last year. One

generic weakness observed during the conduct of the exams was ,

difficulty in the location of control room indications (not )

currently installed on the simulator) during oral exams.

Simulator upgrades, which include a better panel mimic of

.

- - - - - - _ _ _ _ _ . . _ _ _ _ _ _ . _ _ _

, .-_ _ _ _ _ _ _ _ _ _ _ -

.

. 35

l

isolation logic and setpoints, process monitors, and a complete

remote shutdown panel, are scheduled to be completed by October

1988. Other weaknesses identified in individual exams included

SR0 ability to predict automatic depressurization system response

when blowdown was in progress and suppression pool temperature

limits as related to net positive suction head for emergency

core cooling system pumps. Reactor operator weaknesses involved

correlating reactor vessel level with intermediate range neutron

monitor detector response, and power response during a loss of

feedwater transient. Internal coordination of license appli-

cations has significantly improved due to centralized corporate

oversight.

The effectiveness of plant operator and test technician train- 1

ing programs was reflected in the absence of reactor scrams

and the low number of safety system actuations attributable to

those groups. I&C technicians are well-trained and qualified,

and good communications has been established with licensed

operators. Technicians have (in all cases) suspended testing,

and informed control' room supervision prior to resumption of

testing, when erroneous system responses have occurred. In most

reportable events during this period involving test technician

errors, the licensee's staff comprehensively determined root

cause, and this has been a factor in reducing repetitive

occurrences. An effective concept for correcting the cause of

test errors has been roundtable discussions between I&C tech-

nicians and engineers. For example, previous problems with

instrument valve manipulations have been corrected by the

creation of a valving school and by restricting root valve

manipulations to I&C technicians. Only one instance occurred

during the period in which mispositioning an instrument root

valve caused a reportable event.

The licensee reported 21 events attributable to personnel

errors. However, with the exception of fire protection

barriers and doors, none were repetitive or indicative of

a larger breakdown and attest to the licensee's continued

ability to self-identify and correct problems.

A well-organized and controlled radiological training program

continues to make a positive contribution to the effectiveness

of the HP program. This is evident by the low station personnel

exposure history to date, and by the excellent attitude of all

site work groups adhering to HP controls. Instructors involved

in general employee training and respiratory protection training

must complete a rigorous qualification program. The content and

presentation of training for workers is tightly controlled by

the corporate Nuclear Training Manual.

t

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

. 36

Craft training programs were accredited by INPO during the

assessment period. The Limerick Training Center and Barbados

Training Center support the non-licensed training activities

very well. Contractor support is also_ enlisted for training.

Training initiatives have included purchase of a plastic

recirculation pump seal training aid and plans to purchase a

spare MSIV. The maintenance training facility at Barbados, a

decommissioned fossil station is equipped with Limitorque

valves, a spare reactor water cleanup pump, and other actual

plant equipment for hands-on training. Formal classroom and

on-the-job training are a part of a maintenance craftsman's

progression to the journeyman rate. Specialty training has

also been provided where necessary, as for example with refuel

floor activities, snubber rebuilding, pump seals and control

rod drive rebuilds.

In summary, management has promoted a positive attitude in all

areas toward the importance of training. The licensee achieved

INPO accreditation of all of its ten training programs on

Octooer 30, 1986, two months ahead of a self-imposed schedule

set during the previous assessment period.

2. Conclusion

Category 1

3. Board Recommendations:

None

.

!

!

,

. 37

I. Licensing Activities

1. Analysis

This area was rated as Category 1 during the previous assess-

ment period based on issues associated predominantly with

issuance of the full power license and completion of the

Startup Test Program. The previous assessment concluded that

management involvement was apparent and very productive, that

a high degree of licensee responsiveness was exhibited, that

corporate staffing levels were stable and that reportable event

frequencies had improved significantly. An area of potential

weakness was noted in the maintenance of oversight to ensure

that forthcoming scheduler requirements were recognized and

were responded to in a timely manner.

This assessment is based principally on the licensee's

performance in support of three amendments to the operating

license, the review of nine other technical issues and five

petitions concerning licensee actions submitted by intervenors

pursuant to 10 CFR 2.206.

The licensee has continued to demonstrate strengths in the

areas of its approach to problems from a safety standpoint,

the qualifications and level of staffing and in the declining

frequency of reportable events. However, several areas have

not experienced the highest level of performance. These areas

are: (1) the timeliness of licensee applications for NRC staff

action relative to the requested action date; (2) the provision

of adequate technical analyses to support the licensee's pro-

posed no significant hazards consideration (NSHC) determinations;

and, (3) the coordination of plant activities and communications

with the NRC staff.

Management involvement in assuring quality is apparent in the

areas of strength noted above. However, several weaknesses in

licensing activities have developed in the assessment period

which call for further management involvement. One of these

areas, which was also noted in the previous assessment, is the

timeliness of licensee applications for NRC staff action

relative to the requested action date. An apparent lack of

sufficient advance planning and preparation has resulted in the

majority of the requests for action being submitted only a short

time before the needed action date. This concern applies to

the subject of license amendment nos. 1, 2 and 3 and to the

amendment applications concerning the standby gas treatment

system service to the refueling floor and to the allowable

control room air inleakage rate. For example, two of these

issues were included in the initial operating license yet the

responsive license amendment application was submitted only a

few months prior to the needed action date. This concern was

.

. 38

discussed with the licensee in a meeting on October 1, 1986

wherein the staff emphasized the importance of submitting

applications, for which the need can be foreseen, in a timely

manner so that the necessary actions can be completed without

unduly impacting plant availability. The effort by the licensee

in this meeting to project the anticipated filing date for

requests for staff action and the date such action is needed is

commendable. However, three of the four items for which NRC

staff action was requested by a specific time experienced delays

in the projected filing date of two or more months. This area

will continue to be monitored by the staff and a more formalized

scheduling process may be explored if the present less formal

process remains unsatisfactory.

It should also be noted that, while some applications for

action have been untimely, the absence of any requests for

emergency changes to the technical specifications speaks

well of the licensee's past efforts to develop the technical

specifications and the licensee's practices in managing the

operation of the plant.

An additional area of weakness concerns the generalized nature

of the licensee's analyses in its initial proposals of no

significant hazards consideration (NSHC) determination. This

area was not very active in the previous assessment which

included only partial consideration of license amendment nos.

I and 2. However, the much greater degree of activity in this

assessment period, which included the remaining consideration

of amendment nos. I and 2 as well as seven other amendment

applications, indicates that an enhanced level of management

involvement over that apparent in the assessment period is

warranted. Most of the nine license amendment applications

considered in the rating period were initially inadequate in

their analysis of one or more of the three factors of 10 CFR

50.92. The deficiencies consisted of discussions which were

overly simplified and ambiguous to support the assertion that

each of the three factors were met, resulting in a more

extensive NRC staff effort to develop the NSHC Federal Register

notice which extends the time required to process applications.

This issue has been addressed by NRC Generic Letter 86-03, by

letters to the licensee dated May 20, 1986 and February 19,

1987, and in extensive discussions with the licensee's staff

including a meeting on October 1, 1986. The licensee's

performance appeared to be on a clearly improving trend at

the end of the rating period.

A high level of continuing management involvement is also

necessary to ensure that plant activities remain coordinated

with licensee corporate staff activities. Although not typical

of the Itcensee's performance, there was one issue in this area

'

..

. 39

which received attention during the assessment period. Spe-

cifically, this concerned the licensee amendment no. 1 Technical

Specification changes to permit an extension of the surveillance '

interval for instrumentation line excess flow check valves. The

extension permitted postponement of testing until an outage on

the basis that it was undesirable to conduct such testing during

power operations. However, the licensee later began testing

some of the valves before the commencement of the outage, seem-

ingly in at least partial conflict with the basis for the

request for the extension. The conflict appears to have been

due in part to a lack of good communications between plant

staff and corporate licensing personnel. The staff addressed

this issue in a letter dated August 5, 1986 to the licensee

noting that although the issue may not constitute a legal

violation, it represented a departure from the highest stand-

ards of communications expected from licensees. The staff

identified no further need for corrective action by the

licensee in response to this specific event and there have

been no similar recurrences during the assessment period.

A principal licensee strength is its approach to issues from

a safety standpoint. The licensee's proposals have been

technically sound, have reflected acceptable margins of safety

and have contained few errors in technical-information. This

strength was apparent in the application for revision of the

Technical Specification limits on feedwater temperature and

core flow, which was accompanied by a safety analysis that was

extensive in scope and systematic in its approach, and in the

SGTS fan capacity issue wherein the licensee recognized the need

for greater fan capacity and modified the design accordingly.

Strengths are apparent in the licensee's responsiveness in that

the channels of communication between the staff and the licensee

continue to be very effective. The licensee is very responsive

in arranging the appropriate resources for conferences and

meetings. A weakness is also apparent in this area in that the

problem of timely submittal of requests for staff action is one

which continues from the last assessment period and one which

has shown no improvement during this assessment period.

Changes have been adopted in the licensee's corporate organi-

zation, including the licensing staff that interfaces with NRR.

The corporate changes include bringing the Engineering and

Research, the Nuclear Operations and the Electric Production

groups under a single Senior Vice President. These changes

also include some reorganization at the plant staff level.

The licensee characterizes these changes as being in response

to a need to provide more responsive control, because of growth

and specialization and to bring the Peach Bottom and Limerick

plants under a common organization. The current licensing

staff for Unit 1 is gaining further licensing experience and

,

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

___

.

. 40

is increasing in effectiveness. The licensee's staff coordin-

ates an effective response to NRC requests for information.

There is a visible effort to improve effectiveness and all

communications are handled in a professional manner. Based on

the recent implementation of these changes there is an insuf-

ficient basis to conclude whether they will be effective in

alleviating the weakness noted above.

In summary, for the present assessment period, the licensee's

performance in the areas of technical responses to safety

issues, responsiveness to staff communications and staffing

levels cor.tinues at the high level previously experienced

while the frequence of reportable events has improved markedly.

However, the timeliness of submittals, the adequacy of NSHC

determinations, and the adequacy of corporate and plant staff

coordination on actions before the NRC staff need continuing

attention to improve the past level of performance or to main-

tain the improving trend achievec by te end of the assessment

period.

2. Conclusions

Rating: Category 2

3. Board Recommendations

NRC: Conduct a meeting with the licensee to discuss progress

in resolving the three areas of concern, namely the timeliness

of submittals, the adequacy of NSHC determinations and licensee

plant / corporate staff communications.

,

,

__ _ _ _ _ _ _ _ _ . - _ _ .

-- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _

.

.

41

J. Assurance of Quality

1. Analysis

Management involvement and control in assuring quality was

initially considered as a separate functional area in the

previous SALP, in addition to being one of the evaluation

criteria in the other functional areas. The previous

assessment rated this area as Category 1. This discussion

is a synopsis of the assessments relating to the assurance

of quality for activities in other functional areas. The

area was evaluated by both resident and region-based inspec-

tors and is based, in part, on one specific inspection of

QA/QC programs and Independent Safety Engineering Group

(ISEG) activities.

In assessing how the licensee assures quality, the SALP

Board has considered various attributes normally considered

key contributors to the assurance of quality. Among the

attributes considered are implementation of management goals,

planning and control of routine activities, worker enthusiasm

and attitudes, management involvement, staffing, and training.

Licensee management addresses these attributes in diverse

ways. An operational excellence program was institued during

the assessment period that, while formally completed, estab-

lished the desired attitude across all work groups to carefully

consider safety and qualit9, apply attention to detail, involve

supervision and critically self-evaluate. Those traits have

been evident in the attitudes and performance of personnel at

Limerick.

The Plant Operating Review Committee (PORC) was convened on

over 100 occasions during the assessment period, and has been

instrumental in maintaining safe reactor operation as a priority.

The group has clearly insisted on procedures, safety evaluations

in support of modifications, and well considered approaches to

solving station problems. A tracking system is used that

clearly assigns accountability to resolve open issues, such as

test exceptions remaining from the startup test program. The

group has consistently remanded items to their orginator when

less than expected quality was presented. The expectations

for quality in the many issues presented to the PORC have been

high.

As discussed in Section IV.A, the fire protection program war-

rants additional management attention with regard to staffing,

since the Fire Protection Assistant position (left vacant a

year ago) has not been permanently filled. The position has

been temporarily filled by a technician who does not have State

certification as a fire brigade instructor. Also, the corporate

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

. 42

Fire Protection Engineer rarely visits the plant to get a feel-

ing for the program, but more importantly to closely monitor

construction activities as they may present a fire hazard for

Unit 1.

Also, as discussed in Section IV.B, corporate support was not

evident in plant radiological control activities during the

period. An otherwise excellent corporate radiation protection

manual appears to be generally ignored at site and corporate

levels, and corporate involvement is clearly lacking in the

ALARA program. ALARA goals set by the site are achievable,

and establish a level of excellence; however, these goals

do not receive formal corporate sanction or involvement.

Nonetheless, the oversight of plant activities by onsite

ALARA engineers and HP has been excellent.

The Independent Safety Engineering Group (ISEG) has been

active in feeding back experience to operational practices,

while independently assessing significant potential problems.

A Nuclear Safety Section Supervisor chairs the licensee's i

Operational Experience Assessment Committee (0EAC) at monthly

'

meetings, and the scope of industry-wide experience reviewed

and the quality of OEAC recommendations is excellent. ISEG

investigations have provided valuable lessons learned, such

as tagging both ends of long leads associated with temporary

circuit alterations. The ISEG moderates the newly established

Plant Incident Review Committee, utilizing shift supervision

to successfully determine the root of operational problems

such as the drywell chilled water isolation valve violation.

The ISEG has studied reportable events, particularly in the

area of personnel error. In response to an LER at the end of

the assessment period, the ISEG is undertaking a review of

the use and replacement of fuses in safety related circuits.

Investigation of reportable events were thorough, and recom-

mendations made by ISEG were well received by licensee

management. The ISEG has also been involved with a study of

the reliability of the main feedwater system in concert with

corporate engineering, important in light of its role as a PRA

accident initiator. The ISEG is a contributor to quarterly

meetings of a BWR Owner's Group on scram reduction, and in

a new Human Performance Evaluation System (HPES) used to

evaluate causal factors in personnel errors and explore the

man-machine interface. The experience of ISEG members has

been diverse and useful. ,

QA/QC involvement in performing audits and surveillance has

helped to keep quality in the forefront of areas such as opera-

tions startup testing, maintenance, surveillance, non-licensed i

training and fire protection. A visible QA/QC organization is

evident. The personnel assigned to these areas were found to

.

. 43

be knowledgeable of the QA program as it is applied to opera-

tional activities such as maintenance and testing. QA/QC

groups include contract support personnel, and the licensee

has provided complete training for contractors prior to per-

forming their nev function to assure a smooth transition. QA

and QC have been utilized by licensee management to solve

various quality problems during the assessment period. These

problems have included control room communications breakdowns,

vendor access screening, the control of safeguards information

and security barrier breaches. At the end of the assessment

period the licensee was proposing more active involvement by

QC in monitoring test activities and performing independent

verifications.

Meetings were held onsite to discuss the licensee's use of

a Quality Assurance Trending and Tracking system (QATTS) as

discussed in the previous assessment period. QATTS findings

have been effectively presented to licensee senior management

who are aware of and have proposed measures to correct and

reduce observed trends. These include training initiatives,

procedural changes, and proposed design fixes. The QATTS is

being developed by the licensee into a useful management tool.

The licensee's Nuclear Review Board (NRB) was convened during

routine sessions and on a number of special occasions during the

assessment period to review the more significant and unantici-

pated safety problems. These included confirmation of expected

reactor protection system response during the APRM noise event,

and the review of significant nonconformance findings of quality

audits such as from vendor screening, chemistry control pro-

grams, and others. NRB recommendations have been undertaken by

Engineering and Production organizations. The NRB was restruc-

tured under a new chairman at the end of the assessment period.

,

In summary, the quality programs in effect at Limerick have

included QA/QC, the Nuclear Review Board and PORC committees,

the ISEG, and effective front-line supervision of all

disciplines. The quality programs have instituted a set of

checks and balances to prevent undetected errors, and their

overall result has been good personnel attitudes, few alle-

gations, evidence of quality workmanship and a substantially

problem-free period of reactor operation.

2. Conclusion

Category 1

3. Board Recommendations

None

8

- _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

. 44

V. SUPPORTING DATA AND SUMMARIES

A. Investigations and Allegation Review

No NRC Office of Investigations reviews were conducted during the

assessment period.

There were five allegations concerning Unit 1 during this assessment

period, which included three in the area of security. Of the three

security issues, one is a carryover from last assessment period based

on additional concerns of the alleger; the other two were found to

be unsubstantiated and a drug-related concern which is still open.

Another allegation concerned demineralizer resin transfers which

involved an unsubstantiated ALARA concern. The last allegation dealt

with internal piping contamination between Unit I and Unit 2, and was

rsolved.

B. Escalated Enforcement Actions

1. Civil Penalties

None.

2. Actions Pending/ Resolved

r

None.

f 3. Orders

l

None.

4. Confirmatory Action Letters

None.

C. Management Conferences

On July 11, 1986, the licensee met with NRC management in King of

Prussia, Pennsylvania to discuss the previous SALP report findings.

l

l

l

i

i -

_ _ __ _ ___ __.___.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _________ __ ________________ ______ __-_ _____ - ______

.

.

45

D. Licensee Event Reports (LER)

1. Tabular Listing

Type of Events

A. Personnel Error 21

B. Design /Manuf./Constr./ Install. 15

C. External Cause 2

, D. Defective Procedure 8

E. Component Failure 7

X. Other 2

Total 55

A tabulation of LERs by functional area, and an LER synopsis

is attached as Table 1.

LER Nos.86-002 to 86-056 were received and reviewed by the

NRC during the assessment period.

2. Causal Analysis

The 55 LERs which were reported during the assessment period

were also subject to an ongoing review as part of NRC inspec-

tions for trends and root cause identification. The following

sets of common mode events were identified:

a. Twenty-one LERs concern events caused by personnel error,

which is a reduction both in the total number and frequency

of these occurances from last assessment period. Licensee

management is continuing its effort to better understand

and reduce personnel errors by increased training and

personnel awareness, and Independent Safety Evaluation

Group (ISEG) involvement in the Human Performance

Evaluation System (HPES).

While the number of personnel error-related events account

for approximately 40% of all reports during the assessment

period, the principal con'tributors were associated with

fire doors and barriers and inadequate communications dur-

ing surveillance testing. The licensee has recognized

>

these trends and has taken steps to reduce related causal

factors. Further, although 12 of the 21 events were in the

area of surveillance testing, a number were deficiencies

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ ___

l

+

i

!

. 46  !

.

t

!

, found by the licensee (e.g., 4 overdue or missed surveil-

lance tests) because of effective supervisory overview I

and control of testing, and do not therefore represent a

!

' significant trend because of the extensive scope and

otherwise excellent test program record.

b. Fifteen LERs were attributed to design, manufacturing,

construction or installation problems. The total number ,

,

of events appear to be high, but eleven of the LERs were -

attributed to toxic gas detection systems. Unanticipated

sensitivity to moisture and external environmental con-

,

'

ditions was the principal cause of the events. The systems

were modified during this assessment period and are in the *

process of further refinement.

i

c. LERs86-037, and 86-046 were events attributed to external

causes. Both involved misoperation of the chlorine detec- ,

i tion probes during rain storms and high winds. The

i licensee is planning to relocate and protect the probes i

from moisture intrusion.

,

d. LERs86-011, 86-014,86-035, 86-040,86-041, 86-042,  !

'86-044, and 86-056 were events attributed to procedural l

deficiencies. The total number of LERs caused by proce- i

j dure deficiencies dropped 25% from the last assessment

,

period which reflects improvement based on the experiences ,

l gained throughout the current assessment period. Further "

1 human factors improvements incorporated in procedures at  !

j. the end of the assessment period should further reduce F

l events attributable to procedural deficiencies, icluding ,

a communications breakdowns (LER Nos.86-016, 025, 032, '

3 and 047).  !

l i

, e. LERs86-013, 86-022,86-026, 86-031,86-045, 86-050,  !

l and 86-054 were events attributed to random component  ;

failure. This is a significant reduction from the 22 <

4

reportable events from the previous assessment period. '

<

'

f. Nine LERs (Nos.86-006, 009, 017 thru 19, 027, 034,

and 036) were associated with fire protection activities. '

i Seven of these involved inadequately controlled fire doors  !

and barriers which warrant further management attention

i and increased emphasis in training. The frequency of i

these events increased concurrent with outage activities  !

.

in May-June 1986, and therefore warrants particular atten-

l tion during the May 1987 refueling outage.

. i

4

!  :

'

,

[

- - - - _ _ - -

- __

.

. 47

E. Licensing Activities

1. NRR/ Licensee Meetings

October 1,1986, SchedLling of Licensing Activities

2. Schedular Extensions Granted (Full Power License Conditions)

Amendment No. I to the full power licensee granted a one-time

, extension of 14 weeks in the 18-month surveillance interval

for leak rate testing of instrumentation line excess flow

check valves.

Amendment No. 2 to the full power license granted a one-time

extension of twelve weeks in the surveillance interval for

leak rate testing of 27. containment isolation valves.

3. Exemptions Granted (Full Power License)

In conjunction with the issuance of Amendment No. 2 to the

license, a one-time exemption from the scheduler requirements

of 10 CFR Part 50 Appendix J for the leak rate testing of 27

containment isolation valves was granted.

4. License Amendments Issued

License Amendment Nos. I and 2, which extended the leak rate

test surveillance intervals on containment isolation valves,

were issued on February 6,1986 and March 3,1986,

respectively.

5. Emergency Technical Specification Changes _ Granted

License Amendment No. 3, which approved operation with a

reduction of feedwater temperature of up to 60 Farenheit

degrees and an increase of up to 105*.' in rated core flow was

issued on February 17, 1987.

There were six outstanding requests for amendments to the Unit

1 full power license at the end of the assessment period.

.

. 48

TABLE 1

TABULAR LISTING OF LERS BY FUNCTIONAL AREA

LIMERICK GENERATING STATION, UNIT NO. 1

I. LER by Functional Area

Number by Cause Code

Area A B C D E X Total

A. Plant Operations 9 11 2 2 3 2 29

B. Radiological Controls

C. Maintenance 1 1

D. Surveillance 12 3 6 4 25

E. Engineering Support

F. Emergency Preparedness

G. Security and Safeguards

I H. Training and Qualification

i Effectiveness

1

1. Licensing Activities

J. Assurance of Quality

K. Other

Totals 2 T TS~ -~ 2 ~~8 ~T 2 T5

Cause Codes: A. Personnel Error

8. Design. Manufacturing, Construction, or Installation

Error

C. External Cause

D. Defective Procedure

E. Component Failure

X. Other

.

  • 49

TABLE 1 (Continued)

II. LER Synopsis

LER Number Cause Summary

86-002 A Unplanned Isolation of the Reactor Enclosure and

Actuation of SGTS and RERS during testing due to

Personnel Error

86-003 A Unplanned Closure of Shutdown Cooling Isolation

Valve

86-004 8 Unplanned Isolation of the Reactor Enclosure and

SGTS/RERS Initiation Due to Exhaust Fan Blade Pitch

Instrumentation Imbalance

86-005 8 Main Control Room Chlorine Isolation and Emergency

Fresh Air System Actuation due to Analyzer Tape

Break

86-006 A Late Performance of Fire Hose and Cart Visual

Surveillance Tests86-007 8 Actuation of Control Room Emergency Fresh Air

System due to Analyzer Tape Break

86-008 8 Main Control Room Chlorine Isolation and Emergency

Fresh Air System Actuation due to Analyzer Tape

Discoloration

86-009 A Overdue Calibration of Remote Shutdown Panel

Instruments86-010 A Feedwater Flow Transmitter Miscalibration -

Operation in Excess of Licensed Maximum Power Level

86-011 0 Reactor Scram on High Neutron Flu < due to Ground in

EHC Circuit

86-012 B RHR Service Water Radiation Monitor loss of

Isolation Capability on Downscale Failure

86-013 E Reactor Water Cleanup Isolations during Surveil-

lance Testing

86-014 0 Reactor Enclosure Isolation due to Breach in

Equipment Access Airlock

86-015 B Chlorine Analyzer Tape Break and CREFAS Actuation

.

. 50 ,

TABLE 1 Continued)

LER Number Cause Summary

86-016 A HVAC Isolation Trip Channel Inoperable for Greater

than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> during Surveillance Testing

86-017 B Internal Fire Protection Seals Missing in

Electrical Gutters86-018 X Firewatch Violation due to Missing Penetration

Plugs86-019 A Failure to perform Hourly Fire Watch due to

Personnel Error

86-020 B Low Reactor Water Level Scram Due to Personnel

Error and Unavailability of Automatic Feedwater

Level Control Valve

86-021 A Actuation of SGTS due to Improper Use of Jumpers

During Testing

86-022 E Manual Isolation of Main Control Room Ventilation

and Emergency Fresh Air System Actuation due to

High Toxic Chemical Concentration Alarm Caused by

Detector Malfunction

86-023 A Division II ESF Actuation During Surveillance Test

due to Personnel Error caused by Procedural

Inaccuracy

86-024 A Unplanned Isolation of Reactor Enclosure HVAC and

SGTS/RERS Initiation due to Personnel Error in

Opening of Both Airlock Doors Simultaneously

86-025 A Isolation of Shutdown Cooling Caused by Communi-

cation Error during Testing

86-026 E Unplanned Isolation of the Reactor Enclosure HVAC

and SGTS/RERS Initation Due to a Blown Fuse from

Unknown Cause in High Radiation Circuitry

86-027 A Fire Watch Violation Due to Personnel Error in

Propping Open Fire Door

86-028 B Control Room Emergency Fresh Air System Actuation

due to False Toxic Gas Concentration Alarm Caused

by Drywell Chiller Freon Venting

  • !

. 51

<

TABLE 1 Continued)

LER Number Cause Summary

86-029 8 RPS/UPS Static Inverter De-Energized and Isolation

of Instrument Gas Caused by an Incomplete Connec-

tion on a Logic Card Connector during Transfer of

Power Supplies86-030 A Personnel Error Caused Unplanned Group I MSIV

Isolation Signal During Troubleshooting / Stroking

Turbine Stop Valve

66-031 E Special Report - Combined Appendix J Type B and C

Leakage Exceed Allowable Limits86-032 A Daily Surveillance Test Overlooked for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> Due

to Personnel Error / Insufficient Communication at

Shift Turnover

86-033 B Reactor Water Cleanup System Isolation on High

Differential Flow Caused by Collapse of Steam Voids

due to Piping Deficiency in Blowdown Configuration

86-034 A Open Fire Door for 5-1/2 hours Without a Posted

Firewatch Due to Personnel Error While Performing

HP Surveys86-035 D Failure to Comply with Technical Specification

Action Due to Procedural Deficiency - Overdue

Weekly IRM Channel Functional Surveillance Tests

During Shutdown

86-036 A Delay of 20 Minutes in Performing Hourly Fire Watch

for Five Barriers Due to Unscheduled Security

Computer Outage and Inadequate Communications86-037 C Control Room Ventilation Isolation and Emergency

Fresh Air System Actuation Due to Chlorine Analyzer

Malfunction

86-038 A Primary Containment Isolation Valves Inoperable

with Penetration Open

86-039 B Main Control Room Chlorine Isolations and Emergency

Fresh Air System Actuations Due to Electroylte

Probe

86-040 0 Reactor Water Cleanup System Isolations Due to High

Regenerative Heat Exchanger Room Temperature Caused

by Inadequate Ventilation and Opening of a Pressure

Relief Valve

$ 4-

n ,

.- -

!

. 52

.

TABLE 1 Continued)

LER Number Cause Summary

,~.86-041 0 Deficient Surveillance Test Procedure in Verifying

Energized 480 VAC Safeguards MCC

86-041 D Incomplete Performance of Weekly Surveillance Test

'

for Division IV DC Power Alignment Due to Personnel

and Clerical / Duplication Errors and Procedural

Deficiency

'

ll 86-043 B ,m Toxic Gas Detection System Vinyl Chloride Channel

' Operating in Nonconservative Condition Due to

Calibration Design Deficiency Caused by High

Humidity Effects86-044 0 Vinyl Chloride and AmmoniaToxic Gas Alarm Setpoints

Reversed Due to Calibration Error

86-045 E Division II Isolations Due to Blown Fuse Caused by

Improperly Fitted Test Leads and Personnel Errors86-046 C Main Control Room Chlorine Isolations & Emergency

Fresh Air System Actuations Caused by High Winds /

Moisture Effects on Probes86-047 A RCIC Steam Supply Isolation during Testing Caused

by Personnel Error and Inad2quate Communications

'86-048 A RWCU Isolation During Return t6 Service of

s

Demineralizer Caused by Improper Valving Sequence

and Personnel Error

86-049 B RWCU Isolation During Testing Due to Inaccessible

Test Connections

r

-86-050 E Removal of HPCI from Service to Repair Steam Supply

2'

Isolation Valve

86-051 X Fire Watch Not Established for Missing Spare

'l

Electrical Conduit seal

86-052 A HPCI Steam Supply Isolation During Testing Caused

,

by Personnel Error in Use of Ca11brator Unit

86-053 A Group VI C Isolation Caused by Improper Instrument

Root Valve Manipulation by Non-Licensed Plant

Operator

_ _ _ _ _ _ _ _

.

. 53

TABLE 1 Continued)

LER Number Cause Summary

86-054 E Reactor Enclosure Isolation Caused by Improperly-

Sized-Blown Fuse During SGTS Controller Replacement

86-055 B RCIC/ERFDS Temporary Cables Improperly Isolated and

Protected in Raceway from Fire Damage, Affecting

Safe Shutdown Capability

86-056 D Inconsistency Between Control Rod Block and SDV

Level Instruments Caused by Inadequate Surveillance

Test Procedures

,

_ _ _ _ . _ . _ _ _ _ _ . _

1

.

-

.

54

TABLE 2

INSPECTION HOURS SUMMARY (2/1/86 - 1/31/87)

LIMERICK GENERATING STATION, UNIT N0. I

Hours % of Time

A. Plant Operations. . . . ...... 974 35.0

8. Radiological Controls . . . . .... 301 10.8

C. Maintenance . .. ......... 362 13.0

D. Surveillance. . ........... 429 15.4

E. Engineering Support . ........ 61 2.2

F. Emergency Preparedness. ....... 326 11.7

G. Security and Safeguards . . . . . . . 328 11.8

H. Training and Qualification

Effectiveness . . . . . . . . . . . . **

I. Licensing Activities. . . . . . . . . *

J. Assurance of Quality. .... ...

  • --

Total 2781 100.0

Hours expended in facility licensing activities and operator

ifcensing activities not included with direct inspection effort

statistics.

Hours expended in the areas of training and assurance of quality

are included in other functional areas, therefore, no direct

inspection hours are given for these areas.

.

.

. 55

TABLE 3

ENFORCEMENT SUMMARY (2/1/86 - 1/31/87)

LIMERICK GENERATING STATION, UNIT NO. 1

A. Number and Severity Level of Violations

Severity Level No.

Severity Level 3 0

Severity Level 4 3

Severity Level 5 1

Deviation __1

Total 5

B. Violations vs. Functional Areas

Severity Level

FUNCTIONAL AREAS III IV V DEV TOTAL

A. Plant Operations 1 1 1 3

B. Radiological Controls O

C. Maintenance 0

D. Surveillance 0

E. Engineering Support 0

F. Emergency Preparedness 0

G. Security and Safeguards 2 2

Violation and Deviation Totals: 0 3 1 1 5

C. Summary - Enforcement Data

Inspection Inspection Severity Functional

Report No. Date Level Area Violation

86-17 7/21-31/86 4 Operations Failure to maintain

chilled water

containment isolation

valve operability

.

. 56

TABLE 3 Continued)

.

Inspection Inspection Severity Functional

Report No. Date Level Area Violation

86-17 7/21-31/86 DEV Operations Inability to remotely

close the outboard

isolation valves on

chilled water systems

86-19 9/16-19/86 4 Security Closed circuit camera

deficiency

86-25 10/9 - 25/86 4 Security Failure to maintain

safeguards information

as prescribed in

10 CFR 73.21

87-02 1/5-9/87 5 Operations Failure to post a

firewatch during

grinding operations

- - ._ -- ,. . - -_. - . -.

- _______ _ ___-___-___________ _ ___________ _

.

o 57

TABLE 4

INSPECTION REPORT ACTIVITIES (2/1/86 - 1/31/87)

LIMERICK GENERATING STATION, UNIT NO. 1

Report / Dates Inspector Hours Areas Inspected

86-04 Resident 142 Routine

3/1/86 - 4/13/86

86-05 Specialist 39 Startup test program closeout

2/24/86 - 2/28/86

86-06 Specialist 82 Follow-up on security program

3/3/86 - 3/10/86

86-07 Specialist 127 Emergency preparedness exercise

4/2/86 - 4/4/86 Team

86-08 Specialist 18 Radiological environmental

3/10/86 - 3/14/86 monitoring program

86-09 Resident 328 Routine

4/14/86 - 5/31/86

86-10 Specialist 26 Nonradiological chemistry

5/19/86 - 5/21/86 program

86-11 Resident 314 Routine

6/1/86 - 7/31/86

86-12 Specialist 38 Leak Rate Testing

5/27/86 - 5/30/86

86-13 Specialist 43 Radiation protection program

5/22/86 - 5/30/86

86-14 Specialist 40 Effectiveness of QA and QC

5/30/86 - 6/5/86 activities

86-15 Specialist 68 Routine followup on security

7/1/86 - 7/11/86 items

86-16 Specialist 33 Technical Specification

7/7/86 - 7/11/86 surveillance testing and

calibration program

- _ _ _ - _ _ - - _ _ _ _

.

. 58

TABLE 4 Continued)

Report / Dates Inspector Hours Areas Inspected

86-17 Special 30 Assess cause and evaluate inoper-

7/21/86 - 7/31/86 Resident ability of drywell chilled water

containment isolation valves

86-18 Resident 211 Routine

8/1/86 - 9/15/86

86-19 Specialist 26 Safeguards including

9/16/86 - 9/19/86 psychological testing program

86-20 Specialist 43 Maintenance programs

9/8/86 - 9/12/86

86-21 Specialist 64 Radwaste management

9/16/86 - 9/19/86

86-22 Specialist 51 Non-licensed staff training

9/22/86 - 9/26/86

86-23 Resident 285 Routine Inspection

9/16/86 - 11/26/86

86-24 Specialist 0 Licensed operator examinations

10/24/86 - 12/1/86

86-25 Special 53 Security issues

10/9/86 - 1/25/87 Resident

86-26 Specialist 39 Inspection of radiological water

11/3/86 - 11/7/86 chemistry control program

86-27 Resident 353 Routine

11/27/86 - 1/27/87

87-01 Specialist 175 Emergency preparedness exercise

1/14/87 - 1/16/87 Team

87-02 Specialist 40 Fire protection program

1/5/87 - 1/9/87

87-03 Specialist 31 Security program

1/6/87 - 1/9/87

87-04 Specialist 82 Radiological controls including

1/12/87 - 1/16/87 ALARA programs

-

- - - -

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Figure 1

Number of Days Shutdown

Limerick Generating Station, Unit No.1

Feb. 86 --l 1 DAY SHUTDOWN

--l

Mar. 86

Apr. 86

May 86 29 DAYS SHUTDOWN l

l

June 86 16 DAYS SHUTDOWN l

l

July 86 9 DAYS SHUTDOWN l

l

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Sep. 86

Oct. 86

Nov. 86

Dec. 86

Jan. 87 l 5 DAY SHUTDOWN

l