Similar Documents at Byron |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20080G4721995-01-18018 January 1995 Ro:On 941223,invalid Failure Experienced on 2A DG During Normal Start of Engine to Support Transformer Maint Activities.Speed Module Which Initiates Various Control & Support Features as Function of Engine Speed Replaced ML20078L8961994-11-21021 November 1994 Ro:On 941101,DG 2A Invalid Failure Occurred.Problem Isolated to Failed 125 Volt Dc Relay on Instantaneous pre-position Circuit Board.Subj Circuit Board Will Be Replaced W/New Design During Next Unit 2 Refueling Outage ML20114C1141992-08-19019 August 1992 Special Rept:On 920407,fuel Injection Pump in Right Cylinder 7 Seized,Preventing Injection of Fuel Into Associated Cylinder.Caused by Particulate Contamination.On 920320,noise Emanated from Right Cylinder 4 ML20086F9791991-11-22022 November 1991 Special Rept:On 910920,22,27,1001 & 02,invalid Failures of Diesel Generators 1A & 1B Occurred.Redundant Diesel Generator Operable During Each Event.Diesel Generator 1B Placed on Weekly Testing Frequency ML20079P5851991-10-0909 October 1991 Ro:On 910904,09 & 16,seismic Monitoring Instrumentation (Tape Decks 1 & 2 & Sensor 5) Inoperable for More than 30 Days.Playback Tape Deck & Sensor Repaired & Restored to Operable Status ML20058A3681990-10-0101 October 1990 Deviation Investigation Rept 90-026-00:on 900815,EDG 2A Cylinder 10L Dislocated Pushrod Due to Collapsed Hydraulic Lifter ML20055G3461990-06-27027 June 1990 Ro:On 900412,engine Tripped Due to Spurious High Jacket Water Temp Trip Valve Actuation During Partial Surviellance to Verify Operability of Diesel Generator 2A.Nuclear Work Request Initiated to Repair or Replace Trip Valve ML20247C5601989-05-18018 May 1989 Special Rept:On 890224,during Local Leak Rate Surveillance Test,Overall Max Pathway Containment Leakage Failed to Meet Acceptance Criteria & Containment Isolation Valves Exhibited Excessive Leakage.Caused by Improper Valve Stroking ML20246P9061989-03-20020 March 1989 Ro:On 890214,nonvalid Test & Failure Experienced on 2B Diesel Generator.Caused by Nuclear Station Operator Inexperience & Procedural Discrepancy.Nuclear Station Operator Counseled & Procedure Change Initiated ML20236E1821989-03-10010 March 1989 Ro:On 890305,moderator Temp Coefficient Determined to Be More Positive than Allowed by Tech Spec 3.1.1.3.a & Limiting Condition for Operation Entered.Control Rods Maintained within New Withdrawal Limits Until Core Burnup Reached ML20195G5811988-06-13013 June 1988 Deviation Investigation Rept 88-076-00:on 880516,diesel Genrator 1B Uncontrollably Loaded During Monthly Operability Surveillance.Caused by 3IMX Relay Failure.Load Reduced W/ Governor Control Switch & Subj Relay Replaced ML20238D9711987-12-21021 December 1987 Ro:On 870925,during Monthly Operability Surveillance of Diesel Generator 1A,fuel Oil Leak Occurred at Connection of Fuel Pump W/Fuel Pump Discharge Line.Caused by Cracked Fitting at Cylinder Pump Discharge.Pump & Line Replaced ML20237C9051987-12-0303 December 1987 Ro:On 871105,diesel Generator 2A Inoperable for 22 H.Caused by Dirty Voltage Range & Adjustment Potentiometer (Pot) in Voltage Regulator.Pot Cleaned & Exercised Through Full Range ML20236F8351987-10-27027 October 1987 Ro:On 870814,governor Hunting Observed Following Diesel Generator Startup.Caused by Intermittent Operation of 4EX3 Relay.Diesel Generator 1B Will Remain on Monthly Testing Schedule Per Tech Spec 4.8.1.1.2 ML20236T9321987-10-27027 October 1987 Special Rept:On 870831,Train a Safety Injection Occurred During Performance of Bimonthly Surveillance of solid-state Protection Sys.Caused by Cognitive Personnel Error.Emergency Procedure 2BEP-0 Entered & Exited When Plant Stabilized ML20236Q1301987-10-19019 October 1987 Ro:On 870812,reactor Tripped Following Safety Injection & Main Steam Line Isolation During Power Ascension.Caused by Fully Open Governor Valve.Necessary Equipment auto-started/ Actuated Per Design ML20236E5011987-06-25025 June 1987 Ro:On 870318 & 0417,diesel Generator 1A Failed to Reach Rated Speed,Voltage & Frequency within Required Time Set by Tech Specs.Caused by Inadequate Prime in Fuel Oil Supply Line & Ruptured Diaphragm,Respectively ML20236B8871987-06-18018 June 1987 Ro:On 870428,valid Test & Failure on Diesel Generator 2B Occurred.Caused by Method Used for Determining Start Time. Diesel Generator Monthly Operability Surveillance Procedures Revised ML20207T2771987-03-0606 March 1987 Ro:On 870210,diesel Generator 1A Experienced Valid Test Failure.Caused by Failure of Check Valve to Supply Day Tank in Event That Check Valve Fails to Seat.Addl Soft Seat Check Valve Installed Between Engine & Supply Day Tank ML20212K9321987-02-27027 February 1987 Special Rept;On 870215,wide-range Noble Gas Monitor Taken Out of Svc for Mod to Demonstrate Capability to Test for Radioiodine,Per TMI Action Plan Item II.F.1.Mod Scheduled for Completion by mid-Mar 1987 ML20198S1011986-05-29029 May 1986 Special Rept:On 860505,diesel Generator 2A Declared Incapable Due to Contaminated Fuel & Broken Rocker Arms on Seven Left Cylinder.Caused by Bent Retaining Rings & Insufficient Generator Crosshead Procedure.Parts Replaced ML20195D1001986-05-19019 May 1986 Ro:On 860430,Unit 2 Diesel Generator 1B Required 12.5 to Reach Rated Conditions.Caused by Inadequate Prime in Fuel Oil Supply Line.Union Lightened ML20203F6021986-03-20020 March 1986 Special Rept:On 860223 & 0313,diesel Generator 1B Experienced Two Nonvalid Tests & Failures Due to Isochronous Relay Failure.Caused by Intermittent Continuity Between Contacts in Isochronous Relay While in Test Mode ML20203K9371986-03-11011 March 1986 Special Rept:On 860212 & 17,Cooper Bessemer Diesel Generator 2A Failures Occurred Due to Rocker Arm Failure.Caused by Liner Misalignment W/Subsequent Head Alignment.Heads Realigned or Replaced ML20135F8431985-09-0303 September 1985 Ro:On 850813,30- & 250-ft Wind Direction Recorders & 30-ft Air Temp Recorder in Main Control Room Reported Inoperable. Caused by Damaged Fuses in Communication Line Between Meteorological Tower & Control Room.Fuses Replaced ML20127J2541985-06-13013 June 1985 Ro:On 850527,control Room Indication of 30-ft Wind Speed Lost.Caused by Problems W/Communication Links Between Tower Instrumentation & Control Room Readouts.Work in Progress to Restore Operability ML20126M8411985-06-0303 June 1985 Correction to 850523 Special Rept:Second & Third Sentences of Second Paragraph Should Read ...On One of Sys Five Sensor Signal Cables.This Signal Cable Is for Free Field Sensor ML20127E1111985-05-23023 May 1985 Special Rept:On 850419,seismic Instrumentation Sys Began Alarming Continuously.Troubleshooting Indicated 120 Mv Peak to Peak 60 Cycle Signal on Sys Fire Sensor Signal Cables. Problem Under Investigation ML20107D5151985-02-0808 February 1985 Updated Special Rept Re Diesel Generator Failures. Reevaluation Reduced Failures of Diesel Generator 1A to One Common Failure,Decreasing Total to Two Failures Out of 58 Valid Tests ML20106A1761985-01-12012 January 1985 Special Rept:On 841228,suction Relief Valve 1RH8708A & on 841230,RHR Sys Lifted on High Pressure Transient During Restoration of Loop Following Performance of Surveillance Procedure Bvs 0.5-2.SI.3 ML20076K7771983-07-0808 July 1983 Ro:On 830630,during Insp of Spent Fuel Rack,Five Propane Gas Cylinders Found in Spent Fuel Pool Area.Caused by Personnel Error.Cylinders Will Be Stored Outside Fuel Handling Bldg.Signs Re Combustible Matl Will Be Posted 1995-01-18
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H5221999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Byron Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212B9261999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Byron Station,Units 1 & 2.With ML20210R3431999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Byron Station, Units 1 & 2.With ML20210E2251999-07-21021 July 1999 B1R09 ISI Summary Rept Spring 1999 Outage, 980309-990424 ML20209G1751999-07-0808 July 1999 SG Eddy Current Insp Rept,Cycle 9 Refueling Outage (B1R09) ML20207H7941999-06-30030 June 1999 Rev 0 to WCAP-15180, Commonwealth Edison Co Byron,Unit 2 Surveillance Program Credibility Evaluation ML20207H8071999-06-30030 June 1999 Rev 0 to WCAP-15178, Byron Unit 2 Heatup & Cooldowm Limit Curves for Normal Operations ML20207H7851999-06-30030 June 1999 Rev 0 to WCAP-15183, Commonwealth Edison Co Byron,Unit 1 Surveillance Program Credibility Evaluation ML20207H7771999-06-30030 June 1999 Rev 0 to WCAP-15177, Evaluation of Pressurized Thermal Shock for Byron,Unit 2 ML20209H3711999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Byron Station, Units 1 & 2.With ML20207H7561999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20207H7621999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20195J8001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Byron Station,Units 1 & 2.With ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206R6991999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Byron Station Units 1 & 2.With ML20195C7961999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) M980023, Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A)1999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) ML20205P7001999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Byron Station,Units 1 & 2.With ML20205B5091999-03-26026 March 1999 SER Accepting Relief Requests 12R-24,Rev 0 & 12R-34,Rev 0, Related to Second 10-year Interval Inservice Insp for Byron Station,Units 1 & 2 ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20204G3831999-03-19019 March 1999 Safety Evaluation Accepting Second 10-yr Interval ISI Request for Relief 12R-11 M990004, Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function1999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20206A8831999-03-17017 March 1999 Rev 0 to NFM9900043, Byron Unit 1,Cycle 10 COLR in ITS Format W(Z) Function ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20204C7671999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Byron Station,Units 1 & 2.With ML20199G8271998-12-31031 December 1998 Rev 1 Comm Ed Byron Nuclear Power Station,Unit 1 Cycle 9 Startup Rept ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20202F6181998-12-31031 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20199E6371998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Byron Station,Units 1 & 2.With ML20202F6021998-12-31031 December 1998 Cycle 9 COLR in ITS Format & W(Z) Function ML20196K6731998-12-31031 December 1998 10CFR50.59 Summary Rept for 1998 ML20207H7731998-11-30030 November 1998 Rev 0 to WCAP-15125, Evaluation of Pressurized Thermal Shock for Byron,Unit 1 ML20207H8011998-11-30030 November 1998 Rev 0 to WCAP-15124, Byron Unit 1 Heatup & Cooldown Limit Curves for Normal Operation ML20198D1501998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195F8321998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Byron Nuclear Power Station,Units 1 & 2.With 05000454/LER-1998-018, Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a1998-10-0909 October 1998 Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154L5501998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20197C9051998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20151Z9651998-08-31031 August 1998 Revised MOR for Aug 1998 for Byron Nuclear Power Station. Rept Now Includes Page 9 Which Was Omitted from Previously Issued Rept ML20238F6551998-08-28028 August 1998 SE Authorizing Licensee Request for Relief NR-20,Rev 1 & NR-25,Rev 0 Re Relief from Examination Requirement of Applicable ASME BPV Code,Section XI for First ISI Interval Exams ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B3361998-08-14014 August 1998 B2R07 ISI Summary Rept,Spring 1998 Outage, 961005-980518 ML20237B4841998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Byron Nuclear Power Station Units 1 & 2 1999-09-30
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a4
- a. j 7" Commonwealth Edison -
- i j , / 72 West Adams Street, Chicago, Illinois _-
' ' ' ' ~
.i Address RIply to: Post Office Box 767
\v ' Chicago, Ilknois 60690 - 0767 May 18, 1989 Dr. Thomas E..Murley, Director
' Office of Nuclear Reactor _ Regulation
' U.. S. Nuclear Regulatory Commission Washington, DC. 20555'
Subject:
Byron Station Unit 2 ~
Failed Local Leak Rate Test Report NRC Docket No. 50-45ji Reference (a):- May 3, 1989, letter'from D. R. Muller to T. - J. Korach
'(b): Jahuary:18,.1989, letter from J. A. Silady to T. E. Murley
Dear Dr. Murley:
This letter provides the. report for the Byron Unit 2 local leak rate test .
l (LLRT). 'The specific LLRT failure involved three valves in separate lines that contributed tu exceeding the. acceptance criteria of 0.60 La. Upon' reviewing
, reference (a), since this failure did not consist of'two containment isolation valves ~1n series that were found to leak and exceed the Technical Specification allowable limits, and this failure did not identify a single cause that resulted in a group of components becoming inoperable, an LER was not required.
Commonwealth Edison is submitting the attached special report as documented in reference (b), to ensure that the staff is notified of the LLRT failure, even though an ILRT was not performed.
Please contact this office should any additional information be required.
l Very truly yours, l' ,
R. A. Chrzanowski Nuclear Licensing Administrator
'8905240500 890518 1, PDR ADOCK 05000455 S PDC 0147T 1 cc: Regional Administrator - RIII psg,Z L. N. Olshan - NRR F. A. Maura - RIII [
Byron Resident Inspector (
M..C. Parker - IDNS
,, DEVIATION REPORT DVR NO.
06 - 02 - 89 - 029 STA UNIT YEAR NO. Form Rev 2.0
_ FART 1 l TITLE OF DEVIATION OCCURRED 02/24/89 1400 FAILED LOCAL LEAK RATE TESTS DATE TIME SYSTEM AFFECTED PLANT STATUS AT TIME OF EVENT TESTING MODE 5 POWER (%) 0% WORK REQUES NO. l X l l l PC DESCRIPTION OF EVENT During the execution of Local Leak Rate Tests, the following valves had excessive leakage:
2RY8026, 2 SIB 968, 2500020. All were repaired and retested.
POTENTIALLY SIGNIFICANT EVENT PER NSD DIRECTIVE A-07 YES g g lX l .NO 10CTR50.72 NRC RED PH0HE l l NOTIFICATION MADE l l l X l TIME RESPONSIBLE SUPERVISOR DATE PART2l OPERATING ENGINEER'S C0tttENTS None.
N')N REPORTABLE EVENT l X l NOTIFICATION g g 30 DAY REPORTABLE /10CFR REGION III DATE TIME 5 DAY REPORT PER 10CFR21 l l NSD DATE TIME g ANNUAL /SPECIAL REPORT REQUIRED CECO CORPORATE NOTIFICATION MADE IF AB9VE NOTIFICATION IS PER 10CFR21 R. # ,
,, , TELECOPY CECO CORPORATE OFFICER DATE TIME PRELIMINARY REPORT COMPLETED AND REVIEWED J. W. Schrock 02/27/89 OPERATINL ENGINEER DATE /
INVESTIGATION REPORT 3. RESOLUTION g ,
/ j ACCEPTED BY STATION REVIEW N yUA W v. 4 -4' ~I[ y
/ oM+ t/, leS, -
RESOLUTION APPROVED AND AUTHORIZED FOR DISTRIBUTION ~s _4A N ./ / J STATIONMANMi(T DdTE/
86-5176 (Form 15-52-1) 11-20-85 DOCUMENT ID (0278R/0034R)
- o. _ _ _ .
. OEVIATION INVESTIGATION REPORT (DIR)
Facility Name PAGE
_Syron Nuclear Power Station 1 10 0 4 Title F6ILED LOCAL LEAK RATE TESTS EVENT DATE DIR NUPEER REPORT DATE p
/ SEQUENTIAL // REVISION
//j/
f
/j/j MODE MONTH DAY YEAR STA UNIT YEAR NUteER NU M MONTH DAY YEAR 5 POWER
_Al 2 21 4 81 9 1 01.6 01 2 81 9 -
0 l 21 9 --
010 l l l l l0 CONTACT FOR THIS DIR NAE TELEPHONE NUPEER AREA CODE A. Javorik. Assistant Tech Staf f Supervisor Ext. 2206 8l115 2l314l-l5l414l1 COMPLETE ONE LINE FOR EACH COMPONEN A LURE DESCRIBED IN THIS REPORT CAUSE l SYSTEM COMPONENT MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE 6 TURER TO NPRDS TURER TO NPRDS X WlI l Il Sl V El 31 51 0 Y X Al B l Il St V Cl61315 Y X Bl0 l Il Sl V KlOl815 Y l l l l l SUPPLEMENTAL REPORT EXPECTED MONTH DAY YEAR p
SUBMISSION l YES (if ves. complete EXPECTED SUBMISSION DATE) Xl NO TEXT Energy Industry Identification System (E!IS) codes are identified in the text as (XX)
A. PLANT CONDITIONS PRIOR TO EVENT:
, Event Date/ Time 02/24/89 / 1400 Unit 1 MODE 1 - Power Operation Rx Power 99% RCS (AB) Temperature / Pressure Normal Operatino Unit 2 MODE 5 - Cold Shutdown Rx Power 0% RCS (AB) Temperature / Pressure 100'F / 0 PSIG B. DESCRIPTION OF EVENT:
During the Unit 2 first Refueling Outage (B2R01) excution of the Primary Containment (PC) (BD) local Leak Rate Test Surveillance, it was determined that the overall maximum pathway containment leakage failed to meet the acceptance criteria of 0.60 La (277.76 SCFH). The surveillance was started on 01/09/89 and ended on 02/24/89, Three containment isolation valves exhibited excessive leakage that contributed to the overall failure. The valves involved and the dates of failure discovery are: Steam Generator Blowdown Isolation Valve 2SD002D (1/28/89), Pressurizer Relief Tank (PRT) to the Auto Gas Analyzer Isolation Valve 2RY8026 (2/4/89), and Safety Injection Accumulator Nitrogen Supply Check Valve 25I8968 (2/16/B9). Nuclear Work Requests were ger.erated and corrective maintenance was nerfonned to reduce leakage rates. Because the Unit was in Modes 5 and 6, the Limiting Condition for Opera on Action Requirement was not applicable. All components were repaired and retested prior to the unit entering Mode 4, when containment integrity is required.
(0278R/0034R)
______ _____ - ___ _ ___ - a
. DEVIATION INVESTIGATION REPORT TEXT CONTINUATION
___ Form Rev 2.0 FACILITY HAHE DIR NUMBER PAGE SEQUENTIAL REVISION STA UNIT YEAR NUMBER NUPEER Byron Nuclear Power Station 01 6 01 2 81 9 -
0l2l9 0 10 2 0F 014 TEXT Energy Industry Identification System (E!IS) codes are identified in the text as (XX)
C. CAUSE OF EVENT:
The Steam Generator Biowdown Isolation Valve failed due to improper valve stroke. The root cause of the improper stroke is indeterminate.
The PRT to the Auto Gas Analyzer Isolation Valve had a diaphragm which had degraded through normal usage.
The Nitr. gen Supply Check Valve failed due to rubber debris lodged in the valve internals. The source of the debris could not be determined.
D. SAFETY ANALYSIS:
The safety consequences of the Steam Generator Blowdown Isolation Valve leakage is minimized by the IB classification (seismic and safety related) design of the steam generators and associated piping inside containment. In a design basis Loss of Coolant Accident, the steam generators and associated piping provide the containment isolation function. The isolation valve is not challenged by post accident containment pressure. The isolation valves receive an auto closure signal during a Phase A containment isolation in order to maintain Steam Generator inventory, and thus do not perfonn a containment isolation function.
The other failed isolation valves (2RY8026, 2SI80968) have redundant automatic containment isolation valves in series with them. These redundant valves passed the Local Leak Rate Testing and provided acceptable containment isolation.
E. CORRECTIVE ACTIONS:
Valve 2SD002D had its valve stroke adjusted to ensure proper seating. The diaphragm and 0-ring for 2RY8026 were replaced. The valve internals for check valve 2S18968 were cleaned and the seating surfaces were lapped. All components were retested with acceptable results. The valves will continue to be tested at j the frequency specified by 10CFR50 Appendix J and the Technical Specifications.
A Technical Specification change request is being submitted to exempt the Steam Generator Blowdown Containment Isolation valves, 2SD002A-H and 2SD005A-D, from Type C Testing. This exemption is based on the evaluation given in the first paragraph of the safety analysis above. The same evaluation is already j applied to the feedwater and Main Steam Isolation Valves. Action Item Record 88-0267 tracks this corrective action.
i (0278R/0034R) m - - - - - - - - --- _ - -
h
. . DEVIATION INVESTIGATION REPORT TEXT CONTINUATION Form Rev'2.0
-FACILITY NANE. DIR NUMBER PAGE SEQUENTIAL REVISION STA UNIT YEAR NUMBER ' NUMBER 8vron Nuclear Power Station 01 6 01 2 81 9 --
012l9 -
0 10 3 0F 0l4
. TEXT. . Energy Industry ! identification System (EIIS)' codes are identified in the text as [XX].
'F. BECURRING QENTS SEARCH AND ANALYSIS:
a )' '{yENT SEARCH IDIR. LER)
DIR NUMBER ~ IjJJ,g -
6-1-87-061 Local Leak Rate Test Failure.
6-2-87-085 Local Leak Rate Test failure.
6-2-87-118 Local Leak Rate Test Failure.
6-1-88-205 Local Leak Rate Test failure.
Valve 2RY8026 had previously failed Local Leak Rate Testing (DIR 6-2-87-085)..
y .. b ) INDUSTRY SEARCH (OPEX's NPRDS)
An NPRDS search was not performed due to the generic nature of the failures.
'c).. 18fR'
' All of the afinAed valves had work histories that include repacking, stroke adjustment, and operator repair. 2RY8026 had a stroke adjustment to repair the previous LLRT failure. 2518968 was repaired during pre-operational testing due to a failed LLRT. None of the maintenance history is of.
'an exceptional nature, d) ANALYSIS No additional information can be obtained from the recurring events search, j ; G. CONPONENT FAILURE DATA:
I
't%NufACTURER NDENCLATURE Borg-Warner 1500 lb, 2 inch Valve Assy 851-C-0148/072 -
. Cope-Vulcan 3/8 ASNE Valve Class 1500 3/8TA78RL Kerotest 1 Series 600# Y-Type Check Valve IC66 H. OTHER RELATED DOCUENTS:
None.
(0278R/0034R)
._:6L _ _ _ _ - - _ - _ . _ _ - _ - _ _ - - _ - _ _ _ _ - - - - _ _ - _ - _ _ _ _ _ _ _ _ _ _ - - _ - _ - _ - _ _ _ _ _ _ _ _ - _ _ _ _ _
l .' .t. ,
DEVIATION INVESTIGATION REPORT TEXT CONTINUATION-Fonn Rev 2.0 FACILITY NAME DIR NUPEER PAGE j, SEQUENTIAL REVISION l, 1 STA UNIT YEAR NUPBER NUPBER l Byron Nuclear Power Station 01 6 01 2 81 9 -
012'l9 -
0 l0 4 0F O'l 4
-TEXT- Energy Industry Identification System (EIIS) cedes are identified in the text as [XX)
- I. EFFECTIVENESS REVIEW:
. None Scheduled.
J. -ADDITIONAL DATA:
a)- Affected Technical Specification: 3.6.1.C, 4.6.1.2 b) Procedures: .BVS 6.1.2.d-1.1 through .26 c) Equipment Involved: See Component Failure Data
- d) Other
- Local Leak Rate Test Failures. Type B, Type C Failures
'(0278R/0034R)
. a. - __ _ ______________o