ML20195E650

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Comment Supporting Petition for Rulemaking PRM 50-52 Re NRC Reinstatement of Financial Qualifications of Util as Consideration in Operating Licensing Hearings for Electric Utils
ML20195E650
Person / Time
Site: Peach Bottom, Limerick, 05000000
Issue date: 10/24/1988
From: Birnie P
MARYLAND NUCLEAR SAFETY COALITION
To:
NRC OFFICE OF THE SECRETARY (SECY)
References
FRN-53FR32913, RULE-PRM-50-52 53FR32913-00005, 53FR32913-5, NUDOCS 8811100038
Download: ML20195E650 (1)


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i l' S' c ear Regulatory Commission COCKET MR.iEIR Washington, D.C. 20555 PETIT;0t! RULE PRM SD w Attention: Docketing & Service Branch gg y w 7 Er: Docket No.PRM-50-62 of 10 CFR Part 50

Dear Sir:

i

! We support the request that the NRC reinstate financial qualifications [

of utilities as a consideration in the operating licensing hearings for electric utilities.

4- .

This issue has direct and indirect bearing on public henith and safety.

A utility that is under financial duress, often a result of ineffective '

management, may take short cuts in operation and procedures which result i in accidental releases of radiation that endanger the public.  ;

Our experience in researching the Philadelphia Electric Company (PEco),

givec us reason to believe that large, unplanned expenser have greatly '

wea!.ened the utility, with no relief in sight. This weakened fiscal ,

condition can translate into substandard operation.  !

We were told that PECo has poured over 5350 million into refurbishing

, Peach Bottom, plus has the continuing monthly cost of 35 million each 5 i month (now 19 months, with no restart in sight) for replacement power -

while Peach Bottom is out of service. Another 59 million a month cost is split among the three other partner utilities. These three utilities -

have sued PECo $250 million to recover these costs. Early this year some PECo stockholders announced a lawsuit against management for its {

t gross mismanagement of Peach Bottom.

l PEco estimates it will cost $80 million to repair a rndioactive fuel  !

leak at Limerick I that was detected this pas.t August .

PEco's long history of incompetence and irresponsibility should have [

been a factor in considering the licensing of Limerick I and II. It is  ;

]' irresponsible nf tha VRC to rescind the rule which elimir.ates finanelal  !

- qu n ', i f i c a t i on s f rom ec>nwidn at ion, in linnaing. -'-

j P!ce-e r r. i n s t e L c t tri s Tu1W l 8813100038 801024 Si"C'PC'"' *

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EQBOX902/COLUhBA,MD/210M i GOD 381-2714/433-4674  !

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