ML20135F987
ML20135F987 | |
Person / Time | |
---|---|
Site: | Cooper |
Issue date: | 03/31/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20135F984 | List: |
References | |
50-298-97-02, 50-298-97-2, NUDOCS 9704040067 | |
Download: ML20135F987 (19) | |
See also: IR 05000298/1997002
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ENCLOSURE 2
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket No.: 50-298
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License No.: DPR-46
Report No.: 50-298/97-02
Licensee: Nebraska Public Power District
Facility: Cooper Nuclear Station
Location: P.O. Box 98
Brownville, Nebraska
Dates: January 12 through February 22,1997
Inspectors: Mary Miller, Senior Resident inspector
Chris Skinner, Resident inspector
Approved By: Larry Yandell, Acting Chief, Project Branch C
Division of Reactor Projects
Attachments: Supplemental Information
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9704040067 970331
i PDR ADOCK 05000298
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EXECUTIVE SUMMARY
Cooper Nuclear Station
NRC inspection Report 50-298/97-02
Operations
- Control room crews evidenced comprehensive turnovers and strong ownership of
plant safety.
- Inspectors identified that the licensee had failed to enter the action statement for
the inoperable limit switch for residual heat removal train crosstie Valve RHR-MO-
20, for over a year. Inspectors also identified that the licensee had failed to
document the basis for tagging Valve RHR-MO-20 in the closed position, had f ailed
to declare the limit switch inoperable, and did not perform Technical Specification
monthly surveillance tests for the valve or the associated limit switch for the entire I
cycle. The inspectors determined that the licensee staff held a consistent rationale
for not performing the monthly surveillance tests, which considered cycling the
valve undesirable because it cross-tied both residual heat removal trains.
- A weakness was identified in that the licensee's interim corrective actions I
associated with a f ailure to implement Technical Specification requirements were
not clearly understood. A second failure, one month later, almost occurred.
- Inspectors and a licensee supervisor concurrently identified a weakness in that the
licensee did not convene the Safety Operations Review Committee to review the
safety impact of resetting alllow power range monitors prior to the work being
performed under an emergency work order.
Maintenance
- Inspectors identified a violation that included three examples of a failure to properly
implement a calibration procedure. The examples included: (1) the f ailure to
provide appropriate instructions to determine the as-found condition of a relay,
which caused technicians to perform actions outside the proceduro, (2) the f ailure
to perform an action step included in a note until prompted by the inspectors, and
(3) the f ailure to provide correct information regarding the test status of a relay.
The inspectors noted that the procedure had been performed at least three times
and technicians had failed to recognize that the procedure was inadequate.
- Inspectors identified a violation in that licensee personnel did not initiate a PIR to
address three examples of a failure to properly implement a calibration procedure.
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- Inspectors identified that the maintenance program did not provide clear guidance
on the use of the PIR process to document discrepancies.
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Ennineerina
- Engineers were proactive in identifying a potential issue with taper pins on the
diesel generators.
- In a reevaluation of the standby gas treatment system, and the associated
evaluation of the stack effect discussed in Information Notice 88-76, the licensee I
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identified that the reverse of the stack effect was applicable at Cooper Nuclear
Station and evaluated this condition. Inspectors noted that the information notice
did not address this reverse of the stack affect.
- Inspectors identified that, in an operability evaluation and PIR associated with
moisture accumulation in an outocor tank communicating with secondary
containment atmosphere, the licensee did not address the generic applicability of
the f ailure mechanism. In particular, the licensee did not address the effects of
warm, moist air, by contact with cold piping, resulting in an unexpected
accumulation of moisture in vital equipment.
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Report Details
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Summary of Plant Status
The plant was maintained at 100 percent power for the reporting period, except for routine ;
main turbine governor valve testing, when power was reduced to approximately j
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70 percent. l
l. Operations
01 Conduct of Operations
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01.1 General Comments
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a. Insoection Scope (71707)
j Inspectors observed routine control room turnovers and crew activities during the
l inspection 96ricd.
b. Observations and Findinas
- inspectors' observations of more than 30 control room crew turnovers found that
j the turnovers provided information to oncoming crew members which addressed all !
j relevant concerns noted by the prior shift. Shift crew briefings clearly )
i communicated expectations for operations ownership of day-to-day plant safety and )
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demonstrated thorough familiarity with plant conditions and operational evolutions l
< and testing.
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inspectors noted that operators requested resolution from engineering concerning
repeated failures of a secondary containment ventilation valve solenoid. Previous
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failures had been noted on problem identification reports (PIRs), but engineering's
resolution consisted only of solenoid replacement. Operations refused to accept
further replacements of the solenoid without additional engineering evaluation to
correct the problem. Subsequently, the licensee promptly evaluated the issue and
i initiated discussions with the vendor. The licensee has not yet identified the root
l cause for this problem, but is frequently (e.g., monthly) replacing this solenoid to
' assure operability of the valve.
, c. Conclusions
Operations turnovers, familiarity with plant conditions, and ownership of plant ,
safety was strong. Operations evidenced strong ownership of the plant by requiring I
appropriate resolution of a repeated equipment failure.
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O2 Operational Status of Facilities and Equipment
O 2.1 Diesel Generator iniector Pumo Leak
a. Inspection Scope (71707)
The inspector reviewed the licensee's actions to addre:s a leak on Fuel injector 4L
on Diesel Generator 2.
b. Observations and Findinqs
On February 10,1997, during a routine monthly surveillance test on Diesel
Generator 2, the licensee identified a fuel leak on Cylinder 4L. A similar railure was
noted on Cylinder 7R approximately 6 months earlier. Both times, the licensee
attributed the problem to cracks in the fuel lines which were replaced.
Subsequently, the licensee determined the root cause of the leak to be a crack in
the injector pump. Injector pump cracks on this diesel generator design have
occurred previously and were described in vendor information letters. The licensee
replaced the pump ar'd tested the diesel generator satisfactorily. The licensee also
ran Diesel Generator 1 to verify its operability, because they were unable to
determine if a common mode f ailure existed.
Because of this f ailure and a similar prior failure during the cycle, the inspectors
questioned if assumptions regarding probability of diesel generator failure were
nonconservative. The licensee concluded that the current probabilistic risk of diesel
generator failure assumptions bounded the frequency of observed failures. The
inspectors agreed with that conclusion.
c. Conclusions
The inspectors concluded the diesel generator was run an additional two times due
to an incorrect determination of the root cause of the fuel leak. Inspectors noted
that the licensee had not addressed whether increased failures were still bounded
by probabilistic risk assumptions, until questioned by the inspector.
07 Quality Assurance in Operations
07.1 Inadeauate Interim Corrective Actions
a. Insoection Scope (717071
The inspectors reviewed actions by the licensee to correct an earlier problem
associated with entry into a Technica! Specification (TS) action statement.
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i b. Observations and Findinas
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i On January 28,1997, an oncoming licensee shift supervisor identified that a TS
] action statement had not been implemented in that an inoperable secondary
I containment ventilation valve was open when TS 1.0.v.3 required that the valve be
l closed within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of being declared inoperable. The shift supervisor directed
i that the valve be closed and noted that the action was completed within the 4-hour i
j action statement.
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Although the direct safety significance of this occurrence was minimal, the f act that
- this was a fortuitous catch by the oncoming shift supervisor caused the NRC to
- question whether the interim corrective actions from a similar event on
December 24,1996, were effective. The licensee had identified this problem and
documented it in PIR 96-1119. The permanent corrective action proposed for this
PIR was a change to procedures, but the change had not _been implemented by
January 28,1997, when the second instance occurred.
In a separate PIR, the licensee's Quality Assurance (QA) organization identified
several inste. ces where the licensee had failed to implement a required TS action
statement. This QA-identified weakness indicated a broader concern regarding
operating crews' implementation of TS requirements, and implied that past efforts
to correct this concern were not successful,
c. Conclusions
The inspectors identified that the licensee's interim corrective actions for a
December 1996 failure to follow TS requirements were weak and almost resulted in
a recurrence of the same violation of TS. Additionally, a QA audit had indicated an
increasing trend in the failure of the licensee to enter TS action statements.
Although the immediate safety significance of the event was minor, this was an
example of weak corrective actions by the operations staff,
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08 Miscellaneous Operations issues
G 08.1 (Closed) URI 298/96009 01: Adequacy of administrative control of disabled
annuncetors. Although guidelines were provided for disabling annunciators, the
inspectors identified that the licensee did not specify requirements to determine if
an evaluation in accordance with 10 CFR 50,59 was necessary, nor were operators
required to determine if the disabled annunciator was required by abnormal
procedures or_ described in the Updated Safety Analysis Report (USAR). These
evaluations were necessary in order to determine the consequences of and proper
compensatory action for a disabled annunciator.
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The licensee stated that a Station Operations Review Committee (SORC)-approved
procedure would be initiated to address the process for disabling annunciators and
would include appropriate requirements for review of applicable procedures, license
commitments, and design requirements.
Based on the inspectors' review of disabled annunciators and their compensatory ,
actions to date, no violations were identified. The licensee's plans to provide more !
comprehensive controls for disabling annunciators appeared appropriate. However, !
due to the slow implementation of a controlled procedure and the lack of sensitivity i
to address the annunciation function of the sump fill rate timer by engineering (see l
NRC Inspection Report 50-298/96-31), this issue will be tracked as an inspection !
followup item (298/97002-01).
II. Maintenance
M1 Conduct of Maintenance
M 1.1 General Comments .
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i a. Inspection Scope (62707 and 61726)
The inspectors observed all or portions of the following work activities:
Procedure Title
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SP 96-1002 Relay PC-REL-RMAX Contact 2 and
Relay PC-REL-RMBX Contact 5 Replacement
6.LPRM.302 LPRM Calibration and Setpoint Adjustments
MWR 97-0168 250v Battery Charger C Rela */ K5 Replacement
7.3.1.6 125/250vdc Station Battery Charger Protective Relays
Testing and Calibration l
7.3.28.1 Lead Removal and Installation
b. Conclusions
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Maintenance observed by the inspectors appeared appropriate, with exceptions
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M2 Maintenance and Material Condition of Facilities and Equipment
M 2.1 Absence of Taoer Pins Render Diesel Generators inoperable
a. Inspection Scone (62707)
Inspectors followed an engineering issue regarding the absence of taper pins on the
diesel generator fuel rack housings.
b. Observations and Findinas
On January 22,1997, licensee engineering identified an absence of several taper
pins used to help secure the fuel rack housing system (located between each diesel
generator cylinder), which could cause the fuel rack supports to have inadequate
seismic support capability. The vendor stated that, without taper pins, the bolts
securing the fuel rack bearing housing required at least 30 thousand pounds per
square inch (ksi) preload. No preload had been recorded for these bolts on diesel
generator work orders. The licensee's walkdown found that for Diesel Generator 1,
one housing did not include all required taper ains. For Diesel Generator 2, four
housings did not have the required taper pins. The licensee was unable to
determine if greater than 30 ksi preload had been applied to the associated bolts.
At 12:05 p.m. the licensee declared both diesel generators inoperable, entered the
appropriate TS action statement, and planned the required plant shutdown. An
emergency work order was written to implement appropriate preload on the affected
fuel rack bearing housings and determine as-found conditions with match-marks. ;
The bolts were then tightened to 30 ksi. The licensee concluded that, based on the
location of final match-marks, greater than 30 ksi preload had been applied to the
bolts.
Inspector followup concerning how these diesel generators could be restored from
thei; previous overhaul with the missing taper pins will be tracked as an inspection
followup item (298/97002-02).
The engineering performance related to this problem is discussed in Section E2.1.
c. Conclusions
Resolution of two inoperable diesel generators due to lack of taper pins in same fuel
rack housings appeared appropriate. !
M2.2 Recovery From Failed Surveillance of Core Power Distribution
a. Insoection Scope (61726)
The inspector reviewed the licensee's recovery from a failure of a traversing incore
probe (TIP) surveillance test of core power distribution and subsequent resetting of
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local power range monitors (LPRMs) to return the plant to the as-found i
configuration. This surveillance allows for resetting the gains of the LPRMs to l
properly reflect core power distribution.
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b. Observations and Findinas ]
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At 9:10 p.m. on January 23,1997, the licensee identified that a TIP detector f ailed !
during performance of an LPRM calibration. The licensee had completed the first ,
half of the surveillance which involved evaluating and adjusting gains on LPRMs to ]
reflect power distribution during that T!P assessment. During the second half of the
surveillance, which provides dMa to the core thermal limit computer, the TIP failure
occurred. As a result, the licensee did not have a baseline for the core power
calculation with the LPRMs at their newly adjusted setting. The licensee then
determined that the LPRMs should be returned to the presurveillance LPRM gain
settings.
Since the surveillance could not be completed, an emergency maintenance work -
request (MWR), which provided instructions to operators to reset LPRMs to prior
LPRM gain settings, was initiated. Technicians started returning LPRMs to the as-
found condition at 3:48 a.rn. on January 24. The inspectors noted that the control
room had declared the appropriate average power range monitor inoperable, while
the associated LPRMs were being reset, and had entered and exited appropriate TS
action statements. During the recovery from the failed surveillance, the
instrumentation and control supervisor questioned the lack of SORC review of this
process. A short time later, the inspectors independently questioned the lack of
SORC review of the evolution.
Based upon the concerns identified by the supervisor and the inspectors, the
licensee convened a SORC meeting, evaluated the recovery from the failed
surveillance, and determined that the in-progress activity was being performed
appropriately and the instructions appeared to return the LPRMs to the as-found
status.
The inspectors also noted that no interim guidance had been provided to the control
room during this evolution which would have provided operators with instructions
during this anomalous condition. For example, inspectors questioned what
operators would be expected to do if a power transient were to occur during this
evolution, since all LPRM settings were in transition from an as-left to as-found
condition and information provided to calculate thermal limits may not have been in
an analyzed state. Licensee interviews with control room supervision indicated that
control room supervisors would consider tripping the unit if a power transient
condition occurred during this time frame. inspectors noted a need for
unambiguous guidance prior to the evolution so that operators would know what
actions were expected of them if challenges to plant operation occurred.
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c. Conclusiom
The inspectors found that operators initiated an emergency maintenance work
i request (MWR), which required resetting all LPRMs to the as found condition, to
- recover from a TIP failure during the core power calculation surveillance. The
j inspectors noted that the lack of a SORC review of the evolution prior to or
concurrent with the evolution indicated a weakness in the proactive review of plant
! operations. This issue was raised independently by a licensee supervisor. No
i specific guidance was provided to operators on how to respond to abnormal
} conditions which could have occurred during this evolution.
! M2.3 Licens' ee Evaluation of Secondarv Containment Testina Reaardina Stack Effect
l .(!nformation Notice (IN)88-761
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a. Insoection Scoce (62726)
- The inspector reviewed the licensee's evaluation of the containment differential
pressure testing described by IN 88-76,' which concerned stack effects of
temperature differential between the inside and outside of a containment building.
These effects could cause a nonconservative pressure differential between inside
and outside secondary containment.
b. Observations and Findinas
During routine inspector review of containment differential pressure testing,
inspectors noted that the licensee had reviewed and evaluated IN 88-76. The
licensee concluded that, because the pressure sensor for secondary containment
was located high in the reactor building, the stack effect described by IN 88-76 did
not result in a secondary containment differential pressure concern.
The inspector inquired if a reverse of that effect, caused by low temperatures inside
the reactor building and high temperatures outside the reactor building, would cause
a nonconservative pressure differential at the base of the reactor building due to the
different densities of air and the location of the detector high in the plant. The I
licensee acknowledged that the reverse of the stack effect discussed by IN 88-76 l
was possible and could affect the plant in a nonconservative manner and that this
phenomenon had been evaluated. However, the effect was very small since river
water provided cooling to the reactor building. The licensee had concluded that
river water temperatures and available heat exchanger capacity in the reactor ,
building did not significantly lower reactor building temperature with respect to l
outdoor ambient temperature. The reverse of the stack effect at the base of the
reactor building would, therefore, result in an insignificant differential pressure ;
change of approximately 0.01 inch water gauge. I
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c. Conclusions
The licensee's evaluation of the stack effect on containment testing appeared
appropriate and thorough and included vulnerabilities beyond that described by
M3 Maintenance Procedures and Documentation
M 3.1 Maintenance on 250v Batterv Charaer C
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a. Inspection Scone (62707)
The inspector observed the testing and replacement of an alarm relay for 250v
Battery Charger C.
b. Observajions and Findinas
On February 4,1997, the inspectors observed replacement of a battery charger
relay which provided an alarm signal to the control room on battery charger high '
output voltage. MWR 97-0168 instructions required that the as-found values for
the old relay be determined using Procedure 7.3.1.6, "125/250v Station Battery
Charger Protective Relays Testing and Calibration," Revision 7.
The inspector identified three issues concerning the implementation of ,
Procedure 7.3.1.6. To obtain the as-found data, Step 4.6 required that the '
minimum range for the relay be selected for the initial test voltage input. The
electrician used the minimum tolerance value as the minimum range value. The
next step (Step 4.7) required that the voltage be increased until the relay closed.
When the electrician applied the test voltage, the relay closed. In response,
therefore, the electrician decreased the voltage until the relay opened then increased
the voltage until the relay closed. While the actions did determine the as-found
condition, Procedure 7.3.1.6 did not contain any steps specifying the actions that
the electrician performed.
The second problem was that a note preceded by a place-keeping check-off box,
just before Step 4.1, required an action to be performed. The inspectors identified
that the electrician performed Steps 4.1 and 4.2 prior to performing the action
stated in the note.
The licensee responded that the note should have been a step and that the wording
of Step 4.7 would be changed to allow the electrician to vary the voltage. The
licensee stated they would correct the procedure and a PIR was written.
The electrician identified a third problem in that Step 4.15 incorrectly required
decreasing voltage "until the relay closes," instead of "until the relay opens." When
this problem was identified, the job was stopped and the battery charger restored to
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its normal configuration. The procedure was corrected and then the electricians
completed the procedure. The inspectors identified that the procedure had been
performed three times in the past few weeks without identification of this concern.
Procedure 7.3.1.6 was not appropriate to the circumstances in that actions had to
be performed which were not listed in the crocedure, a note in the procedure
required an action to be performed whic. < ". missed, and a step listed the
incorrect test position of the relay. This is ? violation of 10 CFR Part 50,
Appendix B, Criterion V, which requires procedures appropriate to the
circumstances (298/97002-03).
After the job was completed, the inspectors discussed these findings with the
electricians. During the discussion, the electricians stated that the actions to vary
the voltage were beyond the procedure steps, but necessary in order to obtain the
required as-found data, inspectors agreed that as-found data could not be obtained
without varying the voltage.
On February 6,1997, the inspectors determined that no PIR was initiated until the
inspectors questioned why a PIR had not been written to document the identified
problems with Procedure 7.3.1.6.
The failure to initiate a PlR to document three procedural deficiencies in the
l ficensee's corrective action program is an example of a violation of 10 CFR Part 50,
- Appendix B, Criterion XVI, which requires conditions adverse to quality to be
promptly identified (298/97002-04).
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c. Summarv
The inspectors identified two violations in that maintenance personnel failed to
properly implement a calibration procedure and failed to document the identified
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problems in the problem identificatinr1 system.
M4 Maintenance Staff Knowledge and Performance
M4.1 Failure to Resolve TS Discrepancy
a. Insoection Scope (71707)
Inspectors reviewed actions and documentation associated with the lack of
surveillance on Limit Switch RHR-MLS-16, for RHR Crosstie Valve RHR-MO-20.
This valve separates the two redundant residual heat removal (RHR) trains.
b. Observations and Findinas
Crosstie Valve RHR MO-20 was declared inoperable and tagged shut on
January 23,1995, when the licensee recognized that required monthly surveillance
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tests would crosstie both trains of RHR. Since this valve is not required, except in
J certain beyond-design-basis events, this appeared to be a valid concern. The
- licensee identified that the associated limit switch, RHR-MLS-16, was incorrectly
j listed in TS Table 4.2.814 as RHR-MLS-8. Additionally, the TS required a
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functional test once per month, and this involved cycling RHR-MO-20. Inspectors
also noted that the action required when the component operability is not assured
! for that limit switch was stated in Note 1.e as " repair as soon as possible. It does
not directly affect systems operations."
i The limit switch provided indication that the valve was closed, thereby confirming
- that the RHR trains were not crosstied, inspectors noted that, although the
j surveillance test had not been performed since January 1996, the TS action
- statement for the limit switch had not been entered, no evaluation had been
performed concerning its safety function, and no action was pending,. except
j' resolution in the upcoming improved TS implementation. I
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3 Inspectors also noted that no documentation was available to address the licensee's
] lack of entry into the TS action statement or the lack of testing of the limit switch.
l The licensee stated that, because the action statement described in TS 3.5.f.1 for
I Valve RHR-MO-20 was entered and tracked, it was understood that the limit switch '
would not be tested. The inspector noted that this rationale did not address the
i reason for not entering the action statement for the limit switch or for not
3 documenting an evaluation for the failure to return the switch to an operable status
i as soon as possible as required by TS.
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j A discussion of surveillance testing issues, as noted in NRC Inspection Report 50-
j- 298/95-001, documented that this issue need not be resolved before plant restart.
} The inspection report noted that RHR Crosstie Valve RHR-20 had been tested on a
} monthly basis; however, the licensee determined the test was not desirable since it
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temporarily tied the two divisions of RHR together and made them vulnerable to a I
single failure. The limit switch could not be tested independently of valve ,
i operation. The inspection team informed the licensee that the proposed procedure
! change to test only from the nearest relay downstream of a limit switch rather ,
i cycling the valve, did not actually test the limit switch and, consequently, would ;
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not have satisfied the TS requirement. As stated in NRC Inspection Report 50
] 298/95-01, the licensee subsequently decided that the proper course of action was
- to declare the limit switch inoperable and enter and follow the TS action statement,
! which was to repair the instrument as soon as possible.
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j The inspectors noted that as of January 31,1997, the licensee had neither entered
j the action statement to declare the limit switch inoperable, nor implemented actions'
! to address this apparent contradiction in the administrative control of the limit
switch. This oversight illustrates a lack of rigorous attention to TS tracking.
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c. Conclusions
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For a period of over 2 years,Jhe licensee did not address a discrepancy in the TS I
and did not enter an action statement
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for a limit switch for which required TS i
surveillance was not performed.\ For this issue and a related valve testing concern, I
no safety evaluations were documt.qted, although the licensee staff could verbally
articulate an evaluation for these con. erns. A preliminary NRC review concluded i
that the verbally stated evaluation to amid an RHR train crosstie was appropriate. I
M8 Miscellaneous Maintenance issues (92902)
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M8.1 LOcen) Violation 298/94016-02: 480v breaker s.vstem surveillance testing l
inadequate. .-The corrective actions implemented ter this specific event were
documented in NRC Inspection Report 50-298/94-31.
As part of the corrective actions for this issue, the licenst.9 initiated a surveillance i
testing validation program (STVP) to verify that all surveillarne requirements l
contained in the TS, USAR, and design criteria have been adequately translated into l
surveillance test requirements. In October 1996, during the insp9ctors' review of i
the corrective action for the violation, a number of USAR deficienc:9s were noted as l
3r lentified by the licensee in 1995, but were not corrected. Additionk1y, a j
significant number of corrective actions were not documented as closed Based on I
the inspectors' findings, the licensee performed a review of the STVP iteres to l
determine if any other items were still open.
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On January 20,1997, a PlR was written which described the inability to verify
closure of 95 open items documented in the STVP. On January 29,1997, aprojeta
team was forrned to determine the status and close or resolve those items that still
remained open. On February 13,1997, the project team completed their review N
-~and determined that 66 of the 95 items had not been implemented, and that all of N
the 95 STVP items were of minor safety significance. All 95 items were N"
subsequently completed.
This violation remains open pending evaluation by the inspectors of the adequacy of
licensee corrective actions.
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Ill. Enaineerina
E2 Engineering Support of Facilities and Equipment
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E2.1 Enaineerina identification and Resolution of Potentially inoperable Diesel Generators l
Due to Lack of Fuel Rack Housina Taper Pins I
Inspection Scope (37551) !
a.
The inspector observed engineering's contribution to the identification and ;
resolution of a potential diesel generator inoperability. l
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b. Observations and Findinas l
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As discussed in Section M2.1, the diesel system engineer identified that taper pins l
! were not installed on all diesel fuel rack bearing housings located between each l
l cylinder. The lack of taper pins brought into question the seismic qualification of ,
t these housings. ,
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The diesel vendor determined that, in the absence of taper pins, the fasteners on .
each housing would maintain the housings in place if 30 ksi preload was applied. i
The diesel generator system engineer identified that, for some housings on each l
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diesel generator, taper pins were not installed, and identified that 30 ksi preload on !'
each bolt could not be verified using maintenance records.
! Engineering promptly communicated this concern to coerations and maintenance i
and, with bolt match-marks, determined that the as-found" condition of the bolting i
indicated that adequate preload had been applied, i
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c. Conclusions {
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The. diesel system engineer evidenced strong problem identification and resolution '
capabilities regarding the potential inoperability of both diesel generators due to lack !
of taper pins on some fuel rack bearing housings. The root cause of this issue will l
be tracked as an inspection followup item (298/97002-02). ;
E2.2 Operability Evaluation of Containment Penetrations Affected by an Unevaluated
l
N Failure Mechanism
's a. inspection Scoce (37551)
The inspectors evaluated the licensee's resolution of unexpected ice in a tank,
N which was not previously considered a failure mechanism in the design of the tank.
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b. Observations and Findinas
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On January 28,1997, the licensee initiated a PIR which described an unexpected
ice blockage in the drain valve of a tank. The tank, located just outside secondary
containment, communicated with the interior of secondary containment via a 3-inch
drain line and a 2-inch vent line. The tank's purpose was to provide a drain path,
accessible from outside containment, for changing motor generator set oil during
outages. This finding by the licensee indicated that humidity from the reactor
building atmosphere had been drawn into the tank as a result of daily temperature
cycling, had condensed in the tank, and had later frozen. The inspector recognized .
that the accumulation of water and/or ice in this tank was a vulnerability which
apparently had not been considered in the design and control of this tank's
configuration.
The licensee stated that the tank was for maintenance convenience only. The l
associated safety analysis required that the tank not adversely interact with the
Class I seismic secondary containment structure and that the secondary
containment penetrations not fail.
l
On January 30, the inspector requested a licensee engineering manager to tour the
outside of the secondary containment and turbine building structures to address
potential vulnerability brought to light by the liquid condensation mechanism. The
inspector noted that, to date, the broader scope of building penetration vulnerability ,
to condensation and subsequent fleeze/ thaw effects had not been addressed by the
l licensee's response to the problem. The inspector noted that two TS systems had
been affected by similar moisture buildup over the past 5 years and identified the
need fcr appropriate sensitivity to this type of mechanism. During the tour, the
inspector noted several containment and turbine building penetrations which
appeared to be vulnerable to similar condensation and freeze / thaw effects, although
no imminent failures were noted. The engineering manager agreed that these
- questions should be evaluated.
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c. Conclusions !
The inspectors concluded that the licensee prablem identification and operability l
evaluation was timely and showed improved rigor and safety focus. However, !
further inspector involvement was required for the licensee to evaluate the broader
implications of a potential failure mechanism caused by condensation.
E4 Engineering Staff Knowledge and Performance
,
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E4.1 (Ocen) IFl 298/96026-07: Potential nonconservative failure of average power range
monitor (APRM) flow bias circuit. On November 22,1996, during a surveillance
} test of APRM E, alarms indicated an unexpected condition in the Division I reactor
- protection system. Instrument and control technicians correctly diagnosed that the ,
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negative voltage to the flow bias unit power supply failed. The flow bias unit
provided scram signal input for all three APRMs in Division 1.
Inspector followup on February 4,1997, identified that, although similar
vulnerability of other power supplies in the reactor protection system (RPS) was
noted in the services information letter, no detailed licensee evaluation had been
documented which addressed operability of the RPS with respect to the failure of
those other power supplies. On February 12, the licensee completed a detailed
evaluation of RPS power supplies and concluded that no significant vulnerability
existed. The inspector review of this evaluation is continuing.
The inspector identified that the licensee had not yet performed a detailed
evaluation to determine the cause and extent of the problem concerning reset of the
flow bias scram, although the licensee had provided interim compensatory action for
the individual failure which occurred in November. Followup will evaluate a
potentially nonconservative reactor protection system failure mode, timeliness of
evaluation and corrective action, and failure to incorporate industry experience.
E8 Miscellaneous Engineering issues
E8.1 (Closed) URI 50-298/95018-05: Automatic depressurization system accumulator
test. This item addressed the change of automatic depressurization system valve
accumulator pressure to a higher pressure to address the need to overcome
accident pressure during a design basis event. The accumulators provide motive
force to operate the automatic depressurization system relief valves. The inspectors
questioned past operability of the valves before the pressure was raised. The
licensee was unable to address the question at that time.
A recent licensee investigation into past operability concluded that the automatic
depressurization system would have been operable under design basis events. The
licensee investigated accumulator pressure design basis requirements and found
that, for a valve to be operable, a minimum of 68 psi was required for five
actuations at atmosphere pressure, subsequent to one actuation at design pressure
or two actuations at 70 percent design pressure. The inspectors had questioned if
this finding was reportable in accordance with 10 CFR 50.73. Based on the
licensee finding that past equipment configuration indicated operable valves, they
determined the requirements of 10 CFR 50.73 did not apply. These actions
appeared appropriate to the inspectors.
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IV. Plant Support
S2 Status of Security Facilities and Equipment
S 2.1 Control of Security Plan in Control Room
a. Inspection Scope
inspectors reviewed control of personnel access to the security plan,
b. Observations and Findinas
inspectors noted that a security plan located in the shift supervisor's desk in the
control room did not appear to have any restricted access control other than the
access restriction required for entry into the control room. The shift supervisor's
desk is located in an open cubicle in the control room. The licensee believes that
the security plan was not read by unauthorized personnel since the shift supervisor
has observation of his desk area and because of the questioning attitude of other
operators who may observe individuals at the shift supervisor's desk during his
absence. The security manager relocated the plan to a controlled security area near
the control room immediately. '
The licensee stated that this issue was minor since operators would have identified
and questioned individuals reviewing documents in the shift supervisor's cubicle
without a need to know. 10 CFR 73.21(d) requires that security documents be I
locked while not attended, but the licensee's procedures allowed the security plan l
to be in the shift supervisor's desk. This issue will be followed up by inspectors l
from the regional office (298/97002-05).
c. Conclusions
A minor security issue identified by the inspectors will be followed up by inspectors
from the regional office.
VI. Manaoement Meetinas
X1 Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management at the
exit meeting on February 25,1997. The licensee acknowledged the findings presented.
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
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SUPPLEMENTAL INFORMATION
PARTIAL LIST OF PERSONS CONTACTED
Licensee
Mike Bennett, Licensing Supervisor
Dan Buman, Engineering Support Manager
Jack Dillich, Maintenance Manager
Fadi Diya, Design Engineering Manager
Rick Gardner, Operations Manager
Philip Graham, Vice President-Nuclear Energy
David S. Kimball, Radiation Operations Supervisor
Ole Olson, Plant Engineering Manager
Mike Peckham, Plant Manager
Jim Pelletier, Senior Manager of Engineering
INSPECTION PROCEDURES USED
IP 37751: Onsite Engineering
IP 61726: Surveillance Observation
IP 62707: Maintenance Observation
IP 71707: Plant Operations
IP 71750: Plant Support Activities
IP 92901: Followup - Plant Operations
IP 92902: Followup - Maintenance
IP 92903: Followup - Engineering
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened.
298/97002-01 IFl Review of administrative controls of disabled annunciators
(08.1)
298/97002-02 IFl Diesel generator taper pins not installed (M2.1 and E2.1)
298/97002-03 VIO Failure to properly implement a procedure (M3.1)
298/97002-04 VIO Failure to document problems in the problem identification
system (M3.1)
298/97002-05 IFl Evaluation of storage of security plan in the control room
(S2.1)
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Closed
298/96009-0~l URI Control of disabled annunciators (08.1)
298/95018-05 URI Automatic depressurization system accumulator test (E8.1)
Discussed
298/94016-02 VIO 480v breaker system inadequate (M8.1)
298/96026-07 IFl Potential nonconservative failure of APRM flow basis circuit
(E4.1)
LIST OF ACRONYMS USED
APRM average power range monitor
IFl inspector followup item
IN information notice
ksi thousand pounds per square inch
LPRM local power range monitors
PIR problem identification report I
OA quality assurance
SORC Station Operations Review Committee
TIP traversing incore probe
TS Technical Specification
URI unresolved item
USAR Updated Safety Analysis Report
!