LER 93-007-00:on 930326,determined That ECCS Pump Compartment Cooler Power Supply Design Defect Could Have Prevented Adequate Containment Heat Removal.Caused by Design Errors.Mods Planned to Provide Convection CoolingML20056C208 |
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Site: |
Cooper |
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Issue date: |
04/22/1993 |
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From: |
Myers J NEBRASKA PUBLIC POWER DISTRICT |
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To: |
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Shared Package |
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ML20056C207 |
List: |
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References |
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LER-93-007, LER-93-7, NUDOCS 9305110005 |
Download: ML20056C208 (4) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3271994-10-0303 October 1994 LER 94-020-00:on 940901,discovered That Elapsed Time Meters Installed in Essential CR HVAC & SGTS Due to Defective Procedures at Time of Installation.Crefs & SGTS Declared inoperable.W/941003 Ltr ML20029E5871994-05-13013 May 1994 LER 94-007-00:on 940413,HPCI Sys Declared Inoperable.Caused by Lack of Sufficient Restraint on Tubing.Corrective Action: Tubing Placed Back on Fitting & Clamp Was Retensioned.W/ 940513 Ltr ML20029C7211994-04-22022 April 1994 LER 92-020-00:on 920130,containment Level Instruments Were Removed & re-installed Without Being Declared Inoperable. Caused by Personnel Failure to Follow Procedures.Operators retrained.W/940422 Ltr ML20046B4881993-07-30030 July 1993 LER 93-028-00:on 930630,two Potentially Valves Were Inoperable Due to Inadequate Design of Valve Operators by Manufacturer.Modified Valve operators.W/930730 Ltr ML20046A3001993-07-21021 July 1993 LER 93-010-01:on 930331 & 0621,RPS Bus B Deenergized Due to Defective Under Frequency (Uf) Trip Unit Resulting in Unplanned Actuations of Several Esfs.Action Initiated to Permanently Remove Uf feature.W/930721 Ltr ML20045H6011993-07-13013 July 1993 LER 93-025-00:on 930618,determined That Hydrogen/Oxygen Monitoring Sys May Not Effectively Perform post-accident Monitoring Functions.Caused by Insufficient Slope in Lines.Filters Removed & Pump Internals Upgraded ML20045H6051993-07-13013 July 1993 LER 93-026-00:on 930618,discovered That Hydrostatic Tests of Essential Portions of Svc Water & Reactor Equipment Cooling Sys Not Performed Once Per 10 Year ISI Interval. Inclusion of Essential Sys Portion Being Reevaluated ML20045H6071993-07-13013 July 1993 LER 93-027-00:on 930308,standby Gas Treatment Sys Unable to Establish & Maintain Reactor Bldg Pressure + or - 0.25 Inches Water Gauge Under Calm Wind Conditions.Evaluation of Secondary Containment Operability in Progress ML20045E9861993-06-28028 June 1993 LER 93-023-00:on 930528,fuel Assemblies Loaded Into Reactor Core Without Control Rods Fully Inserted,In Violation of TS 3.10.A.2.Caused by Need to Reposition Fuel Support Piece. Training Will Be revised.W/930628 Ltr ML20045E6561993-06-28028 June 1993 LER 93-024-00:on 930527,discovered That Testing of Four Reactor Vessel Low Water Level RPS Sensors Not Completed as Scheduled.Caused by Personnel Error.Stroke Testing Suspended & Surveillance Testing completed.W/930628 Ltr ML20045B4701993-06-11011 June 1993 LER 93-021-00:on 930611,determined That RB Ventilation Exhaust Inboard Isolation Valve HV-AOV-261AV Inoperable & Open Due to Personnel Error.Subj Valve Manually Closed. Proposed Change to TS Will Be submitted.W/930611 Ltr ML20045A5431993-06-0505 June 1993 LER 93-020-00:on 930507,determined That H2/O2 Sys Not Leak Tested to Verify Primary Containment Integrity During Testing of Sys.Caused by Failure to Have Administrative Controls in Place.Pressure Testing conducted.W/930605 Ltr ML20045A4331993-06-0101 June 1993 LER 93-SO1-00:on 930429,discoverd That Individual Had Tested Positive for Drugs at Another Facility on 930226.Employer Had Not Previously Been Notified.Approved Contractor Access Authorization Program suspended.W/930601 Ltr ML20045A4611993-06-0101 June 1993 LER 93-019-00:on 930501,nonconservative Testing Methodology Discovered During LLRT Due to Nonconservative Interpretation of Info Supplied by Valve Mfg.Testing Conducted for Valves Not Previously tested.W/930601 Ltr ML20044G8011993-05-28028 May 1993 LER 93-017-00:on 930428,discovered That Hourly Fire Watch Patrol for RB Per TS Had Not Been Performed.Caused by Personnel Error.Review of Fire Watch Patrol Implementation Process Will Be conducted.W/930528 Ltr ML20044E6301993-05-20020 May 1993 LER 93-015-00:on 930420,design Discrepancy in HPCI Sys Identified.Caused by Design Deficiency in Original Design. Mods Will Be Made to Startup from Current Refueling Outage to Correct Design discrepancy.W/930520 Ltr ML20044D8211993-05-17017 May 1993 LER 93-014-00:on 930316,small through-wall Leak Developed on High Pressure Side of SW Throttle Valve.Caused by Inadequate Valve Design.Frequency of Visual Insp of Valve Internals Will Be Increased to Once Per cycle.W/930517 Ltr ML20044D6511993-05-15015 May 1993 LER 93-013-00:on 930415,determined That as-found Setpoint for Seven SRVs Not within TS Limit.Caused by Lift Setpoint Discrepancies of Srvs.Review of Setpoint Data Will Be performed.W/930515 Ltr ML20044D5341993-05-14014 May 1993 LER 93-012-00:on 930414,violation of Primary Containment Integrity Occurred.Caused by Personnel Error.Procedure Change Being Made to Eliminate Test Return Line Venting When Primary Containment Integrity required.W/930514 Ltr ML20044D2041993-05-12012 May 1993 LER 93-011-00:on 930308,max Differential Pressure Between Reactor Bldg & External Environ of -0.22-inches Water Gauge Exceeded TS Required Min.Caused by Lack of Loop Seal on Rupture Seal Drain Line.Seals replaced.W/930512 Ltr ML20024G7421991-04-23023 April 1991 LER 91-002-00:on 910324,RWCU Occurred Due to High Sys Temp During Plant Cooldown.Caused by Failed Temp Indication & Potential Equipment Failure.Failed Thermocouple & Temp Switch Replaced & calibr.W/910423 Ltr ML20043D2311990-05-30030 May 1990 LER 90-005-00:on 900430,reactor Protection Sys B Motor Generator Set Output Breaker Tripped.Caused by Equipment Malfunction & Preventive Maint Program Deficiency.Sys Restored to Pretrip Operational state.W/900530 Ltr ML20042G9411990-05-10010 May 1990 LER 90-004-00:on 900413,ESF Group Isolations & Diesel Generator Starts Occurred Due to Equipment Malfunction & Personnel Error.Equipment Repaired,Manual Disconnect Operating Location Labeled & Personnel trained.W/900510 Ltr ML20011F1321990-02-23023 February 1990 LER 90-001-00:on 900124,outboard Steam Supply Line Isolation Valve Unexpectedly Closed During Surveillance Testing,Causing Isolation of HPCI Sys.Caused by Procedural Inadequacy.Test Procedure Will Be upgraded.W/900223 Ltr ML20005E3331989-12-26026 December 1989 LER 89-026-00:on 891125,reactor Scram Occurred Due to Closure of Outboard Msivs.Caused by post-filter Media Ignition by Hot Air or Particles from Dryer.Air Dryer B Disassembled & inspected.W/891226 Ltr ML19332F1191989-12-0707 December 1989 LER 88-016-02:on 880517,pipe Stress Analyses Revealed That Resultant Stresses for Five Piping Segments/Components Exceed Plant Design Basis.Caused by Support Design Problems. Long-term Corrective Program implemented.W/891207 Ltr ML19325E2201989-10-27027 October 1989 LER 89-025-00:on 890928,main Turbine Trip Occurred,Followed Immediately by Reactor Scram.Caused by Spurious Actuation of Level Switch Due to Equipment Vibration.Plant Stabilized & Temporary Instruction Re Pump Shifting issued.W/891027 Ltr ML20024C3571983-06-28028 June 1983 LER 83-008/03L-0:on 830530,HFA Relay 9-17-16A K6B Contacts Failed to Open.Cause Not Determined.Relay Coil Replaced. Systematic Replacement of All Relays within 4-yr Period planned.w/830628 Ltr ML20028F0921983-01-20020 January 1983 LER 82-025/03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified ML20028F0781983-01-20020 January 1983 LER 82-024/03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced ML20028B4671982-11-22022 November 1982 LER 82-022/03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified ML20028B4661982-11-19019 November 1982 LER 82-021/03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement ML20052G5321982-05-0606 May 1982 LER 82-008/03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair ML20052B4041982-04-22022 April 1982 LER 82-007/03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modified ML20052A3561982-04-21021 April 1982 LER 82-006/03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established ML20050B2101982-03-19019 March 1982 LER 82-005/03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position ML20041F8271982-03-0505 March 1982 LER 82-004/03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised ML20041C4151982-02-18018 February 1982 LER 81-003/03L-1:on 810223,valve RHR-MO-26B Motor Current Increased & Remained High When Valve Reached Closed Position.Valve Motor Breaker Manually Tripped & Valve Declared Inoperable.Caused by Failure of Brake Coil ML20041C3881982-02-17017 February 1982 LER 82-003/03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily ML20041C3741982-02-17017 February 1982 LER 82-002/03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced ML20041C3871982-02-17017 February 1982 LER 82-001/03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed ML20040D3491982-01-20020 January 1982 LER 81-026/03L-0:on 811223,switches NBI-LIS-01A & NBI-LIS- 101B Found Set at Level Lower That Tech Spec Limits.Caused by Setpoint Drift.Switches Returned to Correct Setpoints. Instrument Drift to Be Closely Monitored ML20040D9261982-01-0505 January 1982 LER 81-025/04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded ML20038C5321981-12-0303 December 1981 LER 81-024/03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced ML20010G0961981-08-25025 August 1981 LER 81-020/03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule ML20010F9881981-08-25025 August 1981 LER 81-019/03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced ML20010G2661981-08-25025 August 1981 LER 81-021/03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced ML20010A1391981-07-22022 July 1981 LER 81-018/03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset ML20010A1671981-07-13013 July 1981 LER 81-017/03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed ML20010A5391981-07-0909 July 1981 LER 81-016/03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient 1994-05-13
[Table view] Category:RO)
MONTHYEARML20024J3271994-10-0303 October 1994 LER 94-020-00:on 940901,discovered That Elapsed Time Meters Installed in Essential CR HVAC & SGTS Due to Defective Procedures at Time of Installation.Crefs & SGTS Declared inoperable.W/941003 Ltr ML20029E5871994-05-13013 May 1994 LER 94-007-00:on 940413,HPCI Sys Declared Inoperable.Caused by Lack of Sufficient Restraint on Tubing.Corrective Action: Tubing Placed Back on Fitting & Clamp Was Retensioned.W/ 940513 Ltr ML20029C7211994-04-22022 April 1994 LER 92-020-00:on 920130,containment Level Instruments Were Removed & re-installed Without Being Declared Inoperable. Caused by Personnel Failure to Follow Procedures.Operators retrained.W/940422 Ltr ML20046B4881993-07-30030 July 1993 LER 93-028-00:on 930630,two Potentially Valves Were Inoperable Due to Inadequate Design of Valve Operators by Manufacturer.Modified Valve operators.W/930730 Ltr ML20046A3001993-07-21021 July 1993 LER 93-010-01:on 930331 & 0621,RPS Bus B Deenergized Due to Defective Under Frequency (Uf) Trip Unit Resulting in Unplanned Actuations of Several Esfs.Action Initiated to Permanently Remove Uf feature.W/930721 Ltr ML20045H6011993-07-13013 July 1993 LER 93-025-00:on 930618,determined That Hydrogen/Oxygen Monitoring Sys May Not Effectively Perform post-accident Monitoring Functions.Caused by Insufficient Slope in Lines.Filters Removed & Pump Internals Upgraded ML20045H6051993-07-13013 July 1993 LER 93-026-00:on 930618,discovered That Hydrostatic Tests of Essential Portions of Svc Water & Reactor Equipment Cooling Sys Not Performed Once Per 10 Year ISI Interval. Inclusion of Essential Sys Portion Being Reevaluated ML20045H6071993-07-13013 July 1993 LER 93-027-00:on 930308,standby Gas Treatment Sys Unable to Establish & Maintain Reactor Bldg Pressure + or - 0.25 Inches Water Gauge Under Calm Wind Conditions.Evaluation of Secondary Containment Operability in Progress ML20045E9861993-06-28028 June 1993 LER 93-023-00:on 930528,fuel Assemblies Loaded Into Reactor Core Without Control Rods Fully Inserted,In Violation of TS 3.10.A.2.Caused by Need to Reposition Fuel Support Piece. Training Will Be revised.W/930628 Ltr ML20045E6561993-06-28028 June 1993 LER 93-024-00:on 930527,discovered That Testing of Four Reactor Vessel Low Water Level RPS Sensors Not Completed as Scheduled.Caused by Personnel Error.Stroke Testing Suspended & Surveillance Testing completed.W/930628 Ltr ML20045B4701993-06-11011 June 1993 LER 93-021-00:on 930611,determined That RB Ventilation Exhaust Inboard Isolation Valve HV-AOV-261AV Inoperable & Open Due to Personnel Error.Subj Valve Manually Closed. Proposed Change to TS Will Be submitted.W/930611 Ltr ML20045A5431993-06-0505 June 1993 LER 93-020-00:on 930507,determined That H2/O2 Sys Not Leak Tested to Verify Primary Containment Integrity During Testing of Sys.Caused by Failure to Have Administrative Controls in Place.Pressure Testing conducted.W/930605 Ltr ML20045A4331993-06-0101 June 1993 LER 93-SO1-00:on 930429,discoverd That Individual Had Tested Positive for Drugs at Another Facility on 930226.Employer Had Not Previously Been Notified.Approved Contractor Access Authorization Program suspended.W/930601 Ltr ML20045A4611993-06-0101 June 1993 LER 93-019-00:on 930501,nonconservative Testing Methodology Discovered During LLRT Due to Nonconservative Interpretation of Info Supplied by Valve Mfg.Testing Conducted for Valves Not Previously tested.W/930601 Ltr ML20044G8011993-05-28028 May 1993 LER 93-017-00:on 930428,discovered That Hourly Fire Watch Patrol for RB Per TS Had Not Been Performed.Caused by Personnel Error.Review of Fire Watch Patrol Implementation Process Will Be conducted.W/930528 Ltr ML20044E6301993-05-20020 May 1993 LER 93-015-00:on 930420,design Discrepancy in HPCI Sys Identified.Caused by Design Deficiency in Original Design. Mods Will Be Made to Startup from Current Refueling Outage to Correct Design discrepancy.W/930520 Ltr ML20044D8211993-05-17017 May 1993 LER 93-014-00:on 930316,small through-wall Leak Developed on High Pressure Side of SW Throttle Valve.Caused by Inadequate Valve Design.Frequency of Visual Insp of Valve Internals Will Be Increased to Once Per cycle.W/930517 Ltr ML20044D6511993-05-15015 May 1993 LER 93-013-00:on 930415,determined That as-found Setpoint for Seven SRVs Not within TS Limit.Caused by Lift Setpoint Discrepancies of Srvs.Review of Setpoint Data Will Be performed.W/930515 Ltr ML20044D5341993-05-14014 May 1993 LER 93-012-00:on 930414,violation of Primary Containment Integrity Occurred.Caused by Personnel Error.Procedure Change Being Made to Eliminate Test Return Line Venting When Primary Containment Integrity required.W/930514 Ltr ML20044D2041993-05-12012 May 1993 LER 93-011-00:on 930308,max Differential Pressure Between Reactor Bldg & External Environ of -0.22-inches Water Gauge Exceeded TS Required Min.Caused by Lack of Loop Seal on Rupture Seal Drain Line.Seals replaced.W/930512 Ltr ML20024G7421991-04-23023 April 1991 LER 91-002-00:on 910324,RWCU Occurred Due to High Sys Temp During Plant Cooldown.Caused by Failed Temp Indication & Potential Equipment Failure.Failed Thermocouple & Temp Switch Replaced & calibr.W/910423 Ltr ML20043D2311990-05-30030 May 1990 LER 90-005-00:on 900430,reactor Protection Sys B Motor Generator Set Output Breaker Tripped.Caused by Equipment Malfunction & Preventive Maint Program Deficiency.Sys Restored to Pretrip Operational state.W/900530 Ltr ML20042G9411990-05-10010 May 1990 LER 90-004-00:on 900413,ESF Group Isolations & Diesel Generator Starts Occurred Due to Equipment Malfunction & Personnel Error.Equipment Repaired,Manual Disconnect Operating Location Labeled & Personnel trained.W/900510 Ltr ML20011F1321990-02-23023 February 1990 LER 90-001-00:on 900124,outboard Steam Supply Line Isolation Valve Unexpectedly Closed During Surveillance Testing,Causing Isolation of HPCI Sys.Caused by Procedural Inadequacy.Test Procedure Will Be upgraded.W/900223 Ltr ML20005E3331989-12-26026 December 1989 LER 89-026-00:on 891125,reactor Scram Occurred Due to Closure of Outboard Msivs.Caused by post-filter Media Ignition by Hot Air or Particles from Dryer.Air Dryer B Disassembled & inspected.W/891226 Ltr ML19332F1191989-12-0707 December 1989 LER 88-016-02:on 880517,pipe Stress Analyses Revealed That Resultant Stresses for Five Piping Segments/Components Exceed Plant Design Basis.Caused by Support Design Problems. Long-term Corrective Program implemented.W/891207 Ltr ML19325E2201989-10-27027 October 1989 LER 89-025-00:on 890928,main Turbine Trip Occurred,Followed Immediately by Reactor Scram.Caused by Spurious Actuation of Level Switch Due to Equipment Vibration.Plant Stabilized & Temporary Instruction Re Pump Shifting issued.W/891027 Ltr ML20024C3571983-06-28028 June 1983 LER 83-008/03L-0:on 830530,HFA Relay 9-17-16A K6B Contacts Failed to Open.Cause Not Determined.Relay Coil Replaced. Systematic Replacement of All Relays within 4-yr Period planned.w/830628 Ltr ML20028F0921983-01-20020 January 1983 LER 82-025/03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified ML20028F0781983-01-20020 January 1983 LER 82-024/03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced ML20028B4671982-11-22022 November 1982 LER 82-022/03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified ML20028B4661982-11-19019 November 1982 LER 82-021/03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement ML20052G5321982-05-0606 May 1982 LER 82-008/03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair ML20052B4041982-04-22022 April 1982 LER 82-007/03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modified ML20052A3561982-04-21021 April 1982 LER 82-006/03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established ML20050B2101982-03-19019 March 1982 LER 82-005/03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position ML20041F8271982-03-0505 March 1982 LER 82-004/03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised ML20041C4151982-02-18018 February 1982 LER 81-003/03L-1:on 810223,valve RHR-MO-26B Motor Current Increased & Remained High When Valve Reached Closed Position.Valve Motor Breaker Manually Tripped & Valve Declared Inoperable.Caused by Failure of Brake Coil ML20041C3881982-02-17017 February 1982 LER 82-003/03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily ML20041C3741982-02-17017 February 1982 LER 82-002/03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced ML20041C3871982-02-17017 February 1982 LER 82-001/03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed ML20040D3491982-01-20020 January 1982 LER 81-026/03L-0:on 811223,switches NBI-LIS-01A & NBI-LIS- 101B Found Set at Level Lower That Tech Spec Limits.Caused by Setpoint Drift.Switches Returned to Correct Setpoints. Instrument Drift to Be Closely Monitored ML20040D9261982-01-0505 January 1982 LER 81-025/04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded ML20038C5321981-12-0303 December 1981 LER 81-024/03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced ML20010G0961981-08-25025 August 1981 LER 81-020/03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule ML20010F9881981-08-25025 August 1981 LER 81-019/03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced ML20010G2661981-08-25025 August 1981 LER 81-021/03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced ML20010A1391981-07-22022 July 1981 LER 81-018/03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset ML20010A1671981-07-13013 July 1981 LER 81-017/03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed ML20010A5391981-07-0909 July 1981 LER 81-016/03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient 1994-05-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212K9781999-09-30030 September 1999 Safety Evaluation Accepting USI A-46 Implementation Program ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217G7461999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Cooper Nuclear Station ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C5001999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cooper Nuclear Station ML20211D6491999-08-25025 August 1999 Part 21 Rept Re Nonconformance within LCR-25 safety-related Lead Acid Battery Cells Manufactured by C&D.Analysis of Cells Completed.Analysis of Positive Grid Matl Shows Nonconforming Levels of Calcium within Positive Grid Alloy ML20210R0381999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Cooper Nuclear Station ML20210J2921999-07-29029 July 1999 Special Rept:On 990406,OG TS & Associated Charcoal Absorbers Were Removed from Svc.Caused by Scheduled Maint on Hpci. Evaluation of Offsite Effluent Release Dose Effects Was Performed to Ensure Plant Remained in Compliance ML20209H8281999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Cooper Nuclear Station ML20211A9981999-07-12012 July 1999 Draft,Probabilistic Safety Assessment, Risk Info Matrix, Risk Ranking of Systems by Importance Measure ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209E1061999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Cns.With ML20196B3851999-06-17017 June 1999 Summary Rept of Facility Changes,Test & Experiments,Per 10CFR50.59 for Period 970901-990331.Summary of Commitment Changes Made During Same Time Period Also Encl ML20195K2851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Cooper Nuclear Station.With ML20206P0481999-05-12012 May 1999 Safety Evaluation Concluding That NPP Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at CNS & Adequately Addressed Actions Requested in GL 96-05 ML20206J0811999-05-0404 May 1999 Rev 14 to CNS QA Program for Operation ML20206P9751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cooper Nuclear Station ML20205Q0891999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Cooper Nuclear Station.With ML20204G8951999-03-15015 March 1999 CNS Inservice Insp Summary Rept Fall 1998 Refueling Outage (RFO-18) ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20204B3701999-03-11011 March 1999 SER Accepting Third 10-year Interval Inservice Insp Plan Requests for Relief for RI-17,Rev 1 and RI-25,Rev 0.Request for Relief RI-13,Rev 2 Involving Snubber Testing & Is Being Evaluated in Separate Report ML20204C9751999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Cooper Nuclear Station ML20199E6751999-01-14014 January 1999 Monthly Operating Rept for Dec 1998 for Cooper Nuclear Station ML20195B9191998-12-31031 December 1998 1998 NPPD Annual Rept. with ML20196J9641998-12-0707 December 1998 Safety Evaluation Accepting Licensee Third 10-yr Interval Inservice Insp Plan Request for Relief RI-27,rev 1 ML20198D2471998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Cooper Nuclear Station.With ML20196A2861998-11-23023 November 1998 SER Re Core Spray Piping Weld for Cooper Nuclear Station. Staff Concluded That Operation During Cycle 19 Acceptable with Indication re-examined During RFO 18 ML20196A5241998-11-23023 November 1998 Safety Evaluation Accepting Proposed Alternative to Use UT Techniques Qualified to Objectives of App Viil as Implemented by PDI Program in Performing RPV Shell Weld & Shell to Flange Weld Examinations ML20196A5061998-11-23023 November 1998 Safety Evaluation Re Flaw Indication Found in Main Steam Nozzle to Shell Weld NVE-BD-N3A at Cns.Plant Can Be Safely Operated for at Least One Fuel Cycle with Indication in as-is Condition ML20196C4241998-11-20020 November 1998 Rev 1 to Cooper Nuclear Station COLR Cycle 19 ML20195H1761998-11-17017 November 1998 SER Authorizing Proposed Alternative in Relief Requests RV-06,RV-07,RV-09,RV-11,RV-12 & RV-15 Pursuant to 10CFR50.55a(a)(3)(ii).RV-08 Granted Pursuant to 10CFR50.55a(f)(6)(i) & RV-13 Acceptable Under OM-10 ML20195F8601998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Cooper Nuclear Station.With ML20155D9961998-10-31031 October 1998 Rev 0 to GE-NE-B13-01980-24, Fracture Mechanics Evaluation on Observed Indication at N3A Steam Outlet Nozzle to Shell Weld at Cooper Nuclear Station ML20154Q5661998-10-0505 October 1998 Rev 0 to CNS COLR Cycle 19 ML20154L5381998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Cooper Nuclear Station.With ML20151Z6141998-09-16016 September 1998 SER Accepting Util Responses to NRC Bulletin 95-002 for Cooper Nuclear Station ML20154F7931998-08-31031 August 1998 Rev 0 to J11-03354-10, Supplemental Reload Licensing Rept for CNS Reload 18,Cycle 19 ML20153B1101998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Cooper Nuclear Station ML20237E7771998-08-20020 August 1998 Revised COLR Cycle 18 for Cooper Nuclear Station ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C0591998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Cooper Nuclear Station ML20236R9131998-07-20020 July 1998 SER Accepting Rev 13 to Quality Assurance Program for Operation Policy Document for Plant ML20236P2971998-07-0707 July 1998 Rev 2 to NPPD CNS Strategy for Achieving Engineering Excellence ML20236R0931998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Cooper Nuclear Station ML20249A7701998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Cooper Nuclear Station ML20247G6131998-05-13013 May 1998 Part 21 Rept Re Defect Contained in Automatic Switch Co, Solenoid Valves,Purchased Under Purchase Order (Po) 970161. Caused by Presence of Brass Strands.Replaced Defective Valves ML20247G0951998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Cooper Nuclear Station ML20237B6861998-04-24024 April 1998 Vols I & II to CNS 1998 Biennial Emergency Exercise Scenario, Scheduled for 980609 ML20217A1531998-04-16016 April 1998 Closure to Interim Part 21 Rept Submitted to NRC on 970929. New Date Established for Completion of Level I & 2 Setpoint Project Committed to in .Final Approval of Setpoint Calculations Will Be Completed by 980531 ML20216G5331998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Cooper Nuclear Station 1999-09-30
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form 3se U E. WuCLEAa REGULATO3Y COMMssteDN
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. LICENSEE EVENT REPORT (LER) ExPmis v2vas i
FACIL8TY NAME 11) DOCKE T NUMSE R (2) PAGE434 f Cooper Nuclear Station o l5 l o } o l o l 219 !8 1 lOFl 0 I 6 TITLE set l ECCS Pump Compartment Cooler Power Supply Design Deficiency Could Have Prevented .
adequate Conteinment Heat Removal !
EVENT DATE ($1 LER WUMe&R166 REPORT DATE (7p OTHER f ActLITIE5 INVOLVED (B) ,
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NAME TELEPHONE NgMgER ARE A CODE ,
John R. Myers 410l2 81215l - l 3181111 i COMPLETE ONE LINE f OR E ACH COMPONENT FAILURE DESCRISED IN THf$ REPORT (13)
CAUSE SYST6M COMPONE NT T
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Efforts associated with the Design Basis Reconstitution Program for Cooper Nuclear i Station (CNS) have identified a design discrepancy in the compartment cooling for the Residual Heat Removal (RHR) pumps. This discrepancy could potentially affect 7 the ability to maintain sufficient Low Pressure Coolant Injection flow in the event of a LOCA in the Core Spray (CS) System. In the event of a CS line break and a loss .
of offsite power concurrent with the failure of one division of 4160 VAC emergency power, two RHR pumps would be available to mitigate the consequences of the LOCA. l The loss of 4160 VAC emergency power would result in the loss of compartment cooling for one of the RHR pumps, potentially resulting in premature failure. Thus, only l one RHR pump would remain operable to mitigate the consequences of the CS line c break, a condition which is not within the current licensing basis. On March 26, at ;
12:10 pm, this condition was determined to be reportable. With the plant in cold shutdown, a CS line break is not a credible accident and, therefore, Technical Specification Limiting Conditions for Operation were not applicable.
This condition is the result of design errors which occurred during the implementation of the Low Pressure Coolant Injection loop select modification in :
1976. Prior to startup from the refueling outage, modifications will be made to resolve the identified concerns i
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A. Event Descrintion l l
During ongoing efforts associated with the Nebraska Public Power _
District's Design Basis Reconstitution Program for Cooper Nuclear .[
Station (CNS), a design discrepancy in the compartment cooling for the Residual Heat Removal (RHR) pumps was identified. This discrepancy l involved the ability of the RHR pumps to continue to operate if l compartment cooling is lost due to the failure of one division of- '
1 4160 VAC emergency power upon a design basis accident (DBA) involving !
the Core Spray (CS) system. On March 26, at 12:10 pm, an evaluation of f the discrepancy was conducted by the Station Operations Review Committee j (SORC), which determined that this condition was reportable. At_the time, the plant was in a refueling outage with the Reactor defueled. In this condition, neither RHR nor CS were required to be operable, and, (
since a CS line break is not postulated with the Reactor depressurized, j there were no immediate compensatory measures required. i DBA conditions include a loss-of-coolant accident (LOCA) with a concurrent loss-of-offsite power (LOOP) and a worst case single failure. :
The postulated worst case single failure is a loss of one division of l 4160 VAC emergency power, since this causes the failure of two of the j four RHR pumps, one of the two CS pumps, and loss of the compartment cooler in one of the RHR pump compartments. Two RHR pumps are located
- in each compartment. Power to one RHR pump in each compartment is from the Division 1 emergency power source, and power to the other if from-Division 2. One compartment cooler is also supplied from the Division 1 ,
emergency power source, and the other from Division 2. The loss of the _
compartment cooler has been postulated to result in high temperature in ;
the compartment leading to the failure of an operating RHR pump after j approximately ten minutes. A CS system IDCA initially results in the j two RHR pumps injecting to the Reactor vessel without any core spray, j Upon failure of one of the operating RHR pumps due to the high _
temperature in the compartment, only one RHR pump would be. available tio - I mitigate the consequences of the DBA. The single RHR pump is. adequate to provide core cooling, but may not be sufficient to provide both core and containment cooling. The General Electric ECCS Performance /LOCA i Analysis previously assumed and analyzed configuration was one Core ,
spray pump and one RHR pump, or two RHR pumps. Thus,-this condition is- ;
outside the licensing basis of CNS. ~j B. Plant Status 5 Shutdown for the 1993 Refueling Outage, with the Reactor defueled.
C. Basis for Report j i
A condition alone that could have prevented the fulfillment of.the safety function of systems needed to mitigate the consequences of an- ;
accident, reportable in accordance with 10CFR50.73(a)(2)(v). )
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i D. Cause This condition is the result of design errors which occurred during the implementation of the Low Pressure Coolant Injection (LPCl) loop select
- modification in 1976. In response to changes in the ECCS rule, 10CFR50.46, in the early 1970s, Cooper Nuclear Station was required to perform a plant modification,' commonly called the LPCI loop select ,
modification, to satisfy the peak clad temperature requirements under ;
, DBA conditions. Prior to the modification, the two RHR pumps in each i Reactor Building compartment were powered from one division of emergency power, which also powered the compartment cooler. The major changes of the LPCl loop select nodification included cross-powering two of the RHR pumps and converting the LPCI injection valves and the Reactor Recirculation System discharge valves to 250 VDC power. The dependence on AC power of the compartment coolers and the effect of a loss of cooling on the ability of the pumps to continue operating was apparently not recognized by the Architect / Engineer nor Nebraska Public Power District personnel responsible for the design change.
- As a part of the modification and in response to the new ECCS l performance rules, a Single Failure Analysis was also conducted to identify the limiting component failures for both the Reactor l Recirculation System suction and discharge line breaks. The Single !
Failure Analysis was performed by the Architect / Engineer for Cooper Nuclear Station in 1976. This analysis also did not consider the potential consequences of the loss of AC power on the compartment coolers and the resultant effect on the pumps, i E. Safety Sirnificance r The safety objective of the CS and RHR Systems is to provide a source of water to provide core and containment cooling in the event of a LOCA. !
These systems were intended to perform this task with a LOOP and worst i possible single failure. For a CS system LOCA under these conditions, the loss of compartment cooling could potentially result in the subsequent failure of one of the two operational RHR pumps. Operating !
procedures direct that the RHR system be aligne.d to use the RHR Heat ,
Exchanger to provide cooling for the water being injected into the i Reactor vessel. Review of this condition by General Electric indicates the single RHR pump would be adequate to maintain the peak clad i temperature within the requirements of 10CFR50.46. Both RHR pumps would operate for the initial 10 minutes of the transient, when peak clad ,
temperature concerns are greatest. Additionally, the calculations for +
compartment heatup were conservative, not accounting for structural heat i capacity and ventilation available due to piping penetrations allowing I airflow to other areas within the Re-actor Building, thus the 10. minute i time limit is very conservative. .
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E. Safety Sinnificance (Continued)
The analysis for Primary Containment is based on maintaining the flow from one RHR pump in Torus Cooling to maintain containment temperature below 200 degrees Fahrenheit. As part of the response'to a DBA, the Emergency Operating Procedures require that operators maintain cognizance of Primary Containment temperature. LPCI flow is diverted to Torus cooling or spray as required to maintain containment temperature
. and pressure within an appropriate range. If containment integrity were !
threatened by high temperature or pressure, LPCl flow would be diverted to ensure containment integrity was maintained. A backup water source to supply the Reactor vessel with cold water is available from the .
Control Rod Drive and Service Water systems. Together with the RHR pump in Torus Cooling, this may have provided sufficient cooling to mitigate the consequences of the CS line break, although the condition is not within the licensing basis of the plant.
F. Safety Implications The event which must occur in order for the compartment cooling to be of concern is a CS IDCA with a concurrent LOOP and a simultaneous failure of one 4160 VAC emergency power source. The probability of these three !
unrelated events occurring simultaneously is extremely remote (less than 'j 10-8 per year of reactor operation). :
G. Corrective Action {
E At the time this condition was identified, the plant was in a refueling.
outage with the Reactor defueled. In this condition, neither RHR nor CS -j were required to be operable, and, since_ a CS line break is not {
postulated with the Reactor depressurized, there were no immediate j
- compensatory measures required. . Prior to startup from the refueling i outage, modifications are planned to provide natural convection cooling for the equipment in these compartments by replacing the solid equipment- ~
hatches with grating. Analyses are being performed to ensure that fire -
protection, environmental qualification, radiological, and flooding issues are addressed. :
i H. Similar Events 1 LER 92-013. Error.in Limiting Single Failure Assumptions'for the ECCS Performance Analysis, discusses another condition related to insufficient design review for the LPCI loop selection modification.
i 26A - *V,5. CPOs 19F B-520- 590P0070 -
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05000298/LER-1993-001 | LER 93-001-00:on 930225,several Design Discrepancies in SW & Reactor Equipment Cooling Sys Identified.Caused by Piping Configuration Error During Plant Const.Mechanical & Electrical Mods Will Be made.W/930318 Ltr | | 05000298/LER-1993-007 | LER 93-007-00:on 930326,determined That ECCS Pump Compartment Cooler Power Supply Design Defect Could Have Prevented Adequate Containment Heat Removal.Caused by Design Errors.Mods Planned to Provide Convection Cooling | | 05000298/LER-1993-008 | LER 93-008-00:on 930328,4,160-volt Breakers 1BG,1GB & 1GE Tripped Due to Actuation of 1GS Breaker Lockout Relay.Caused by Oversight in Design Change Installation Instructions. Work Stopped & Design Change Implemented | | 05000298/LER-1993-029 | LER 93-029-00:on 930708,partially Withdrawn Control Rod 26-31 Scrammed.Caused by RPS Scram Signal from Two of Four Reactor Pressure Scram Switches.Scram Reset & Pressure Testing completed.W/930806 Ltr | | 05000298/LER-1993-030 | LER 93-030-00:on 930708,discovered Inadequate Inservice Testing of Svc Water Sys Check Valves Due to Flow Instrument Calibr Error & Personnel Error in Specifying Sys Flow Requirement.Revised Calibr Factor developed.W/930809 Ltr | |
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