05000298/LER-1982-021-03, /03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement

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/03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement
ML20028B466
Person / Time
Site: Cooper Entergy icon.png
Issue date: 11/19/1982
From: Bednar L
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20028B460 List:
References
LER-82-021-03L, LER-82-21-3L, NUDOCS 8211300406
Download: ML20028B466 (1)


LER-1982-021, /03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement
Event date:
Report date:
2981982021R03 - NRC Website

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