LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Submitted |
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h"T COOPER NUCLEAR STATION
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Nebraska Public Power District
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CNSS830193 March 17, 1983 jh;bky x
Mr. John T. Collins, Regional Administrator
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/pg2?//g U. S. Nuclear Regulatory Commission
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Office of Inspection and Enforcement Region IV 611 Ryan Plaza Drive Suite.1000 b/
Arlington, Texas 76011
Dear Sir:
This report is submitted in accordance with Section 6.7.2.B.2 of the Technical Specifications for Cooper Nuclear Station and discusses a reportable occur-rence that was discovered on February 23, 1983. A licensee event report form is also enclosed.
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Report No.:
50-298-83-01 Report Date:
March 17, 1983 7{ [i - SL((_
Occurrence Date:
February 23, 1983 Facility:
Cooper Nuclear Station Brownville, Nebraska 68321 Identification of Occurrence:
A condition which led to operation in a degraded mode permitted by a limiting condition for operation established in Paragraph 3.5.E.1 of the Technical Specifications.
Conditions Prior to Occurrence:
The reactor was operating at approxinately 100% of rated thermal power and reactor pressure was approximately 1000 psig.
Description of Occurrence:
While performing Surveillance Procedure 6.2.2.2.4 (125V DC Control Power Transfer of Automatic Depressurization System), safety relief valve (SRV) 71-C failed to transfer to its alternate power source on loss of pre-ferred power.
Designation of Apparent Cause of Occurrence:
The apparent cause of this occurrence was attributed to a normally open contact in a General Electric Type HFA relay failing to close on loss of power.
Analysis of Occurrence:
SRV 71-C is one of eight Target Rock pressure relief valves on the reactor vessel. These particular Target Rock valves are pilot operated O
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Mr. John T. Collins March 17, 1983 Page 2 valves each with an air operated solenoid valve.
SRV 71-C is one of six SRVs associated with the Automatic Depreesurization System (ADS).
While performing Surveillance Procedure 6.2.2.2.4 on the SRVs, SRV 71-C failed to transfer to its alternate source of control power on a simulated loss of primary power. Several attempts were made to initiate transfer by pulling fuse 945-2E-F3C, however, the control power would not transfer.
Investigation revealed that the malfunction was caused by a normally open contact on relay 945-2E-KllC failing to make contact on loss of power.
After the above attempt to transfer control power failed, contact wipe atM gap adjustments were performed on the relay contacts. This procedure was performed in accordance with General Electric Service Information Letter No. 44, S4, Attachment B.
Following the gap and wipe adjustments, Surveillance Procedure 6.2.2.2.4 was repeated satisfactorily, with SRV 71-C transferring to its alternate control power source when relay 945-2E-KilC was de-energized.
SRV 71-C remained operable during relay contact failure of 945-2E-K11C.
Only the transfer function on loss of preferred power was rendered inoperable. All eight SRVs would have functioned in a pressure relief mode and could have been operated manually if required. With reference to USAR, Volume II, Section VI-7-6, only five of the six SRVs cre re-quired to be operable. This occurrence presented no adverse consequences from the standpoint of public. health and safety.
Corrective Action
Relay 945-2E-KilC was adjusted per Ceneral Electric Service Information Letter No. 44, S4, Attachment B.
Surveillance Procedure 6.2.2.2.4 (Control Power Transfer of ADS System) was again performed on the subject valve with satisfactory results. No further action is required.
Sincerely, L. C. Lessor Station Superintendent Cooper Nuclear Station LCL:STS:cg Attach.
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| 05000298/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-001/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-001-03, /03L-0:on 830223,while Performing Surveillance Procedure 6.2.2.2.4,safety Relief Valve 71-C Failed to Transfer Alternate Power Source When Fuse Pulled.Caused by Bad Contact on Relay.Relay Control Wipe Adjusted | /03L-0:on 830223,while Performing Surveillance Procedure 6.2.2.2.4,safety Relief Valve 71-C Failed to Transfer Alternate Power Source When Fuse Pulled.Caused by Bad Contact on Relay.Relay Control Wipe Adjusted | | | 05000298/LER-1983-002-03, /03L-0:on 830218,source Range Monitor Rod Blocks Not Tested Prior to Hot Startup.Caused by Inadequate Procedures.Procedure 2.1.2 Revised | /03L-0:on 830218,source Range Monitor Rod Blocks Not Tested Prior to Hot Startup.Caused by Inadequate Procedures.Procedure 2.1.2 Revised | | | 05000298/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-002/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-003/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-003-03, /03L-0:on 830403,indication & Control Power for Reactor Bldg Exhaust Valve HN-260MV Failed,Resulting in Valve Not Automatically Closing on Isolation Signal.Caused by Burned Out Lamp.Lamp & Fuse Replaced | /03L-0:on 830403,indication & Control Power for Reactor Bldg Exhaust Valve HN-260MV Failed,Resulting in Valve Not Automatically Closing on Isolation Signal.Caused by Burned Out Lamp.Lamp & Fuse Replaced | | | 05000298/LER-1983-004-03, /03L-0:on 830409,during Sp 6.1.4,contacts of Relay 917-5A-K7D Failed to Open.Cause Not Determined.Relay Coil Replaced & Proper Operation Verified.All Ac Hfa Relays on Essential Sys Will Be Tested During Spring 1983 Outage | /03L-0:on 830409,during Sp 6.1.4,contacts of Relay 917-5A-K7D Failed to Open.Cause Not Determined.Relay Coil Replaced & Proper Operation Verified.All Ac Hfa Relays on Essential Sys Will Be Tested During Spring 1983 Outage | | | 05000298/LER-1983-004, Forwards LER 83-004/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-004/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-005-03, /03L-0:on 830505,scram Discharge Vol Drain Value CRD-CV-AOV33 Failed to Close Per Tech Specs.Caused by Grafoil Packing Working Between Valve Stem & Body.Valve Repacked | /03L-0:on 830505,scram Discharge Vol Drain Value CRD-CV-AOV33 Failed to Close Per Tech Specs.Caused by Grafoil Packing Working Between Valve Stem & Body.Valve Repacked | | | 05000298/LER-1983-006-03, /03L-0:on 830509,during Performance of Surveillance Procedure 6.3.10.9.1,four RHR Mechanical Snubbers Frozen.Caused by RHR Shutdown Cooling Creating Water Hammer & Overloading snubbers.w/830608 Ltr | /03L-0:on 830509,during Performance of Surveillance Procedure 6.3.10.9.1,four RHR Mechanical Snubbers Frozen.Caused by RHR Shutdown Cooling Creating Water Hammer & Overloading snubbers.w/830608 Ltr | | | 05000298/LER-1983-007-03, /03L-0:on 830518,during Refueling,Both Standby Gas Treatment Sys Diesel Generators Found Inoperable.Caused by Personnel Failure to Follow Tech Spec Requirements. Requirements Reviewed & Clarified | /03L-0:on 830518,during Refueling,Both Standby Gas Treatment Sys Diesel Generators Found Inoperable.Caused by Personnel Failure to Follow Tech Spec Requirements. Requirements Reviewed & Clarified | | | 05000298/LER-1983-008-03, /03L-0:on 830530,HFA Relay 9-17-16A K6B Contacts Failed to Open.Cause Not Determined.Relay Coil Replaced. Systematic Replacement of All Relays within 4-yr Period planned.w/830628 Ltr | /03L-0:on 830530,HFA Relay 9-17-16A K6B Contacts Failed to Open.Cause Not Determined.Relay Coil Replaced. Systematic Replacement of All Relays within 4-yr Period planned.w/830628 Ltr | | | 05000298/LER-1983-009-01, /01T-0:on 830629,pinhole Leaks Found in heat- Affected Zone of Weld CWA-BJ-2 During Insulation Removal on 6-inch Reactor Water Cleanup Suction Line.Caused by Intergranular Stress Corrosion Cracking | /01T-0:on 830629,pinhole Leaks Found in heat- Affected Zone of Weld CWA-BJ-2 During Insulation Removal on 6-inch Reactor Water Cleanup Suction Line.Caused by Intergranular Stress Corrosion Cracking | | | 05000298/LER-1983-010-03, /03L-0:on 830617,during Functional Surveillance Testing by Wyle Lab,One Main Steam Snubber Failed to Meet Bleed Rate Criteria & One Svc Water Snubber Failed to Meet Lockup Rate.Caused by Plugging by Foreign Matl | /03L-0:on 830617,during Functional Surveillance Testing by Wyle Lab,One Main Steam Snubber Failed to Meet Bleed Rate Criteria & One Svc Water Snubber Failed to Meet Lockup Rate.Caused by Plugging by Foreign Matl | | | 05000298/LER-1983-011-01, /01T-0:on 830710,welds CSA-BJ-5 & 6 Found Leaking During Grinding of Weld Crowns.Caused by Intergranular Stress Corrosion Cracking.Welds to Be Repaired by Weld Overlay Methods.Piping Will Be Replaced | /01T-0:on 830710,welds CSA-BJ-5 & 6 Found Leaking During Grinding of Weld Crowns.Caused by Intergranular Stress Corrosion Cracking.Welds to Be Repaired by Weld Overlay Methods.Piping Will Be Replaced | | | 05000298/LER-1983-012-03, /03L-0:on 830621,during Control Rod Shuffle,Fuel Bundle Removed & Reloaded Into Core in Same Position W/O All Control Rods Inserted.Caused by Personnel Error.Crews Briefed | /03L-0:on 830621,during Control Rod Shuffle,Fuel Bundle Removed & Reloaded Into Core in Same Position W/O All Control Rods Inserted.Caused by Personnel Error.Crews Briefed | | | 05000298/LER-1983-013, Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1983-013-03, /03L-0:on 830831,during Local Leak Rate Test, Procedure 6.3.1.1,20,penetrations Found Leaking Excessively. Caused by Discs & Seats Being Lapped.Valves Repaired | /03L-0:on 830831,during Local Leak Rate Test, Procedure 6.3.1.1,20,penetrations Found Leaking Excessively. Caused by Discs & Seats Being Lapped.Valves Repaired | | | 05000298/LER-1983-014-03, /03L-0:on 830915,during Surveillance Testing, Pressurization of Suppression Chamber Air Space Noted During HPCI Turbine Operation.Caused by Error in Vacuum Breaker Design/Installation.Breaker Replaced | /03L-0:on 830915,during Surveillance Testing, Pressurization of Suppression Chamber Air Space Noted During HPCI Turbine Operation.Caused by Error in Vacuum Breaker Design/Installation.Breaker Replaced | | | 05000298/LER-1983-015-03, /03L-0:on 830923,pressure Switch NBI-PS-102A Failed to Perform High Pressure Safety Trip of Reactor Recirculation Pump A.Caused by Relay Failure to Energize. Relay Replaced | /03L-0:on 830923,pressure Switch NBI-PS-102A Failed to Perform High Pressure Safety Trip of Reactor Recirculation Pump A.Caused by Relay Failure to Energize. Relay Replaced | |
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