05000298/LER-1981-021-03, /03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced

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/03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced
ML20010G266
Person / Time
Site: Cooper 
Issue date: 08/25/1981
From: Freborg S
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20010G259 List:
References
LER-81-021-03L, LER-81-21-3L, NUDOCS 8109150504
Download: ML20010G266 (1)


LER-1981-021, /03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced
Event date:
Report date:
2981981021R03 - NRC Website

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f0 61 DOCK ET NUMBE R 68 69 EVENT DATE 74 7h REPOR T D ATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l a l 2 l l During the performance of a surveillance procedure on #2 diesel generator, an injec-I l o l d 1 tor line failed. #2 DG was shut down and declared inoperable. Redundant #1 DG was in-l 1014 I l operable at the time of this occurrence. Applicable surveillance procedures were com-l l o 151 1 menced per RTS 3.5.F.2 for both DG's being inoperable. This event is not repetitive. I 1016 I I There were no adverse ef fects on the public health and safety.

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