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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20211G6101997-09-29029 September 1997 LER 97-S01-00:on 970829,discovered That Shotgun Shell Was Missing from Ammunition Carrier.Caused by Improper Issuance & Control of Weapons & Ammunition.Missing Shell Immediately Replaced 05000298/LER-1993-0301993-08-0909 August 1993 LER 93-030-00:on 930708,discovered Inadequate Inservice Testing of Svc Water Sys Check Valves Due to Flow Instrument Calibr Error & Personnel Error in Specifying Sys Flow Requirement.Revised Calibr Factor developed.W/930809 Ltr 05000298/LER-1993-0291993-08-0606 August 1993 LER 93-029-00:on 930708,partially Withdrawn Control Rod 26-31 Scrammed.Caused by RPS Scram Signal from Two of Four Reactor Pressure Scram Switches.Scram Reset & Pressure Testing completed.W/930806 Ltr 05000298/LER-1993-0081993-04-22022 April 1993 LER 93-008-00:on 930328,4,160-volt Breakers 1BG,1GB & 1GE Tripped Due to Actuation of 1GS Breaker Lockout Relay.Caused by Oversight in Design Change Installation Instructions. Work Stopped & Design Change Implemented 05000298/LER-1993-0071993-04-22022 April 1993 LER 93-007-00:on 930326,determined That ECCS Pump Compartment Cooler Power Supply Design Defect Could Have Prevented Adequate Containment Heat Removal.Caused by Design Errors.Mods Planned to Provide Convection Cooling 05000298/LER-1993-0011993-03-18018 March 1993 LER 93-001-00:on 930225,several Design Discrepancies in SW & Reactor Equipment Cooling Sys Identified.Caused by Piping Configuration Error During Plant Const.Mechanical & Electrical Mods Will Be made.W/930318 Ltr 05000298/LER-1982-014, Amended LER 82-014/03X-1:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-13,BJ-15,BJ-20 & BJ-23.Caused by Improper Fabrication Techniques.Affected Piping & Fittings Replaced1983-02-0303 February 1983 Amended LER 82-014/03X-1:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-13,BJ-15,BJ-20 & BJ-23.Caused by Improper Fabrication Techniques.Affected Piping & Fittings Replaced 05000298/LER-1982-005, Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested1982-10-20020 October 1982 Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested ML20204D4181978-12-0808 December 1978 /01T-0 on 781124:while Checking RR MG Set 1B Speed control,1 Amp fuse(F2) in Drive Amplifier Circuit Was Pulled Out & Checked.Caused Rapid Increase in Pwr Level,Tripping RR MG Set 1B ML20148A7231978-12-0707 December 1978 /03L-0 on 781111:during S.P.6.4.1.2. (Withdrawn Control Rod Operability), Control Rod 30-31 Was Found Uncoupled from Its Control Rod Drive. Cause Cannot Be Determined Until Control Rod Drive Is Removed & Examined ML20150D3371978-11-13013 November 1978 /03L-0 on 781016:cable HP58,Div 1,was Found Routed Thru Div 11 Riser Under Panel 9-3.Caused by Personnel Error During Constr.Redundant Sys Were Operable ML20150D3191978-10-13013 October 1978 /03L-0 on 780918:during Normal Oper,After Cooling Down the Torus,Rhr Heat Exchanger 1B Bypass RHR-MO-66B Failed to Oper,Due to Loose Set Screw on Yoke of Limiterque SMB-3 Operator ML20150D3561978-09-28028 September 1978 /03L-0 on 780912:Cooper-Bessemer Diesel Engine Type KSV-16-T Main Bearing Overheated.Main Bearing 10 Was Damaged Due to Minimal Oil Flow During Engine Coastdown. Caused by Foreign Particles in Oil 1997-09-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212K9781999-09-30030 September 1999 Safety Evaluation Accepting USI A-46 Implementation Program ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217G7461999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Cooper Nuclear Station ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C5001999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cooper Nuclear Station ML20211D6491999-08-25025 August 1999 Part 21 Rept Re Nonconformance within LCR-25 safety-related Lead Acid Battery Cells Manufactured by C&D.Analysis of Cells Completed.Analysis of Positive Grid Matl Shows Nonconforming Levels of Calcium within Positive Grid Alloy ML20210R0381999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Cooper Nuclear Station ML20210J2921999-07-29029 July 1999 Special Rept:On 990406,OG TS & Associated Charcoal Absorbers Were Removed from Svc.Caused by Scheduled Maint on Hpci. Evaluation of Offsite Effluent Release Dose Effects Was Performed to Ensure Plant Remained in Compliance ML20209H8281999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Cooper Nuclear Station ML20211A9981999-07-12012 July 1999 Draft,Probabilistic Safety Assessment, Risk Info Matrix, Risk Ranking of Systems by Importance Measure ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209E1061999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Cns.With ML20196B3851999-06-17017 June 1999 Summary Rept of Facility Changes,Test & Experiments,Per 10CFR50.59 for Period 970901-990331.Summary of Commitment Changes Made During Same Time Period Also Encl ML20195K2851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Cooper Nuclear Station.With ML20206P0481999-05-12012 May 1999 Safety Evaluation Concluding That NPP Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at CNS & Adequately Addressed Actions Requested in GL 96-05 ML20206J0811999-05-0404 May 1999 Rev 14 to CNS QA Program for Operation ML20206P9751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cooper Nuclear Station ML20205Q0891999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Cooper Nuclear Station.With ML20204G8951999-03-15015 March 1999 CNS Inservice Insp Summary Rept Fall 1998 Refueling Outage (RFO-18) ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20204B3701999-03-11011 March 1999 SER Accepting Third 10-year Interval Inservice Insp Plan Requests for Relief for RI-17,Rev 1 and RI-25,Rev 0.Request for Relief RI-13,Rev 2 Involving Snubber Testing & Is Being Evaluated in Separate Report ML20204C9751999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Cooper Nuclear Station ML20199E6751999-01-14014 January 1999 Monthly Operating Rept for Dec 1998 for Cooper Nuclear Station ML20195B9191998-12-31031 December 1998 1998 NPPD Annual Rept. with ML20196J9641998-12-0707 December 1998 Safety Evaluation Accepting Licensee Third 10-yr Interval Inservice Insp Plan Request for Relief RI-27,rev 1 ML20198D2471998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Cooper Nuclear Station.With ML20196A2861998-11-23023 November 1998 SER Re Core Spray Piping Weld for Cooper Nuclear Station. Staff Concluded That Operation During Cycle 19 Acceptable with Indication re-examined During RFO 18 ML20196A5241998-11-23023 November 1998 Safety Evaluation Accepting Proposed Alternative to Use UT Techniques Qualified to Objectives of App Viil as Implemented by PDI Program in Performing RPV Shell Weld & Shell to Flange Weld Examinations ML20196A5061998-11-23023 November 1998 Safety Evaluation Re Flaw Indication Found in Main Steam Nozzle to Shell Weld NVE-BD-N3A at Cns.Plant Can Be Safely Operated for at Least One Fuel Cycle with Indication in as-is Condition ML20196C4241998-11-20020 November 1998 Rev 1 to Cooper Nuclear Station COLR Cycle 19 ML20195H1761998-11-17017 November 1998 SER Authorizing Proposed Alternative in Relief Requests RV-06,RV-07,RV-09,RV-11,RV-12 & RV-15 Pursuant to 10CFR50.55a(a)(3)(ii).RV-08 Granted Pursuant to 10CFR50.55a(f)(6)(i) & RV-13 Acceptable Under OM-10 ML20195F8601998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Cooper Nuclear Station.With ML20155D9961998-10-31031 October 1998 Rev 0 to GE-NE-B13-01980-24, Fracture Mechanics Evaluation on Observed Indication at N3A Steam Outlet Nozzle to Shell Weld at Cooper Nuclear Station ML20154Q5661998-10-0505 October 1998 Rev 0 to CNS COLR Cycle 19 ML20154L5381998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Cooper Nuclear Station.With ML20151Z6141998-09-16016 September 1998 SER Accepting Util Responses to NRC Bulletin 95-002 for Cooper Nuclear Station ML20154F7931998-08-31031 August 1998 Rev 0 to J11-03354-10, Supplemental Reload Licensing Rept for CNS Reload 18,Cycle 19 ML20153B1101998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Cooper Nuclear Station ML20237E7771998-08-20020 August 1998 Revised COLR Cycle 18 for Cooper Nuclear Station ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C0591998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Cooper Nuclear Station ML20236R9131998-07-20020 July 1998 SER Accepting Rev 13 to Quality Assurance Program for Operation Policy Document for Plant ML20236P2971998-07-0707 July 1998 Rev 2 to NPPD CNS Strategy for Achieving Engineering Excellence ML20236R0931998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Cooper Nuclear Station ML20249A7701998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Cooper Nuclear Station ML20247G6131998-05-13013 May 1998 Part 21 Rept Re Defect Contained in Automatic Switch Co, Solenoid Valves,Purchased Under Purchase Order (Po) 970161. Caused by Presence of Brass Strands.Replaced Defective Valves ML20247G0951998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Cooper Nuclear Station ML20237B6861998-04-24024 April 1998 Vols I & II to CNS 1998 Biennial Emergency Exercise Scenario, Scheduled for 980609 ML20217A1531998-04-16016 April 1998 Closure to Interim Part 21 Rept Submitted to NRC on 970929. New Date Established for Completion of Level I & 2 Setpoint Project Committed to in .Final Approval of Setpoint Calculations Will Be Completed by 980531 ML20216G5331998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Cooper Nuclear Station 1999-09-30
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COOPER NUCLEAR ST ATioN m.
Nebraska Public Power District "" "" "d" *o"MMis"i"T" "'"
i CNSS933204 ,
August 9, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
Dear Sir:
Cooper Nuclear Station Licensee Event Report 93-030, Revision 0, is forwarded as :
I an attachment to this letter.
Sincerely, R. L. Gardner Plant Manager r
RLG/j u !
Attachment !
cc: J. L. Milhoan ;
G. R. Horn ;
J. M. Meacham R. E. Wilbur V. L. Wolstenholm !
D. A.' Whitman INPO Records Center NRC Resident Inspector R. J. Singer CNS Training CNS Quality Assurance 130044 !
r I f 9308160098 930909 'N PDR ADOCK 05000299 r3 .
S PDR j t-
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NRC Form 386 - U.$, NUCLEAR StEEULATOAV COMMISEfDN 7
APPROVED OMS NO. MeiOO104 I LICENSEE EVENT REPORT (LER) N'at *: "'" lt f
FACILITY fuAME (1) DOCE E T NUMBE R (2) 8' AGE (Ji ,
Cooper Nuclear Station o 151010 l o l 2l 9 l8 1 lOFl 0 l3 ;
TITLE (de .
Inadeauate In-Service Testing Of Service Water System Check Valves Due To Flow Instrument Calibration Error And Personnel Error In Specifying. System Flow Requirement EVENT DATE (El LER NUMBER EG) REPORT DATE (73 OTHf R f AC8UTIES INVOLVED (8)
' ' AClLIT Y h AMES f
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MONTH DAY YEAR DOC 8LET NUMBE.Rt5) ol5l0l0lo; ; l- ;
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NAME TELEPHONE NUM6ER AHE A CODE I Donald L. Reeves, Jr. 4l 012 812 151- 131811 l 1 ,
COMPLETE ONE LtNE FOR E ACH COMPONENT F ALLURE DESCRIBED IN THis REPORT (131 ,
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On July 8,1993, as a result of determining that the conversion of Service Water .
(SW) Flow Rate measured by an annubar flow monitoring device was incorrect, it was (
discovered that In-Service Testing (IST) of the SW Pump discharge check valves had not been performed in accordance with the requirements of Generic Letter (GL) 89-04.
In accordance with the GL requirement, verification that a check valve has stroked >
to its full open position requires the maximum accident condition flow rate be -
established through the valve. However, due to the flow instrument calibration ,
error, actual SW System flow was less than indicated by approximately eight and one- ;
half percent. Additionally, the surveillance procedure used to verify SW Pump :
discharge check valve operability on a quarterly basis did not require that the ,
maximum accident condition flow rate be established. At the time this condition was !
discovered, required surveillance testing in preparation for startup from the 1993 Refueling Outage was being performed.
'i The cause of the IST test deficiency was due to the flow instrument calibration-error, an original design deficiency, and failure to recognize that the flow rate specified in the surveillance procedure for verifying operability of.the check ,
valves was not the maximum accident condition flow rate required by GL 89-04. !
A revised calibration factor was developed and incorporated in the surveillance test !
procedure, Additionally, the procedure was revised to establish the correct SW I System flow for the test and to correctly state the test acceptance criteria. l Assurance of SW System check valve operability was verified prior to startup from '
the 1993 Refueling Outage. ,i t
neQterm See .
4 Nec foem as4A U.S. NUCLE AR Rf GULATO;tY COMMIS$10N LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AerRovro oMn No 3 _o,o.
EXPIRE S. 8/31/88 8 ACIL8TV ev&ME 0 6 DOCKET NUMBE R Qt LE R NUMBER ($l PAGE(31
"^a " M.W.'.' '100 Cooper Nuclear Station itKT IN omus wece in % :- . une eedste ael NRC Mm XLWul1176 ol5l0l0l0l2l9l8 9l 3 -
0l3l0 -
0 l0 0l2 or 0l3 A. Event Description On July 1,1993, it was determined that the conversion of Service Water (SW) Flow Rate measured by an annubar flow monitoring device was incorrect. This discrepancy was evaluated for its impact on SW System operability. A calculation based upon the results of the A SW Subsystem surveillance test conducted on June 23, concluded that both Subsystems remained operable. A subsequent evaluation on July 8 determined that previous In-Service Testing (IST) of the SW Pump discharge check valves had not been performed in accordance with the requirements of Generic Letter (GL) 89-04, Guidance on Developing Acceptable Inservice Testing Programs. As specified in the GL, verification that a check valve has stroked to its full open position requires the flow rate through the valve to be the maximum required accident condition flow rate. However, due to the flow instrument calibration error, actual SW flow was less than indicated by nearly eight and one-half percent. Additionally, the surveillance procedure used to verify SW Pump discharge check valve operability on a quarterly basic required that a SW System flow rate of 6000 gpm be established, as opposed to the required maximum required accident condition flow rate of 6243 gpm, a difference of approximately four percent.
B. Plant Status Performing required surveillance testing in preparation for startup from the 1993 Refueling Outage.
C. Basis for Report Failure to perform quarterly SW check valve IST in accordance with ASME requirements, reportable in accordance with 10CFR50.73(a)(2)(1)(B) as a condition prohibited by Technical Specifications.
D. Cause Design and Personnel. The K factor associated with the conversion of annubar d/p to gpm was not correctly specified by the manufacturer when procured for installation in the system during original construction.
Additionally, Engineering personnel responsible for the IST Program did not recognize that the flow rate specified in the surveillance procedure for verifying operability of the check valves was not the maximum required accident condition flow rate required by Generic Letter 89-04.
E. Safety Sinnificance once per refueling cycle, the SW System is tested at a flow rate in excess of 6250 gpm during the post LOCA flow test, with the secondary result of assuring operability of the check valves. While the actual flow rate was less than indicated by approximately ten percent during tests conducted prior to this refueling outage, the flow rate obtained during past post-LOCA flow tests has been adequate to assure check valve NRC FO8EM 366A *U.S. LPOs 1996 520-589 00010
($43)
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION _ _ aerneveo oue woimo-oio.
EXP!RES: 8/31/88 i FACitfTY NAME (O DOCacET NUMBf R Cl - tg R wuMBER (H pagg g3)
" ^a -"EMIk^' 4'17.%?% i:
Cooper Nuclear Station ol5lo[ojol2l9l8 9l 3 0F '
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G. Safety Sinnificance (continued) t operability in accordance with the GL requirement. Further, since' 't publication of Generic Letter 89-04, each check valve has been disassembled and inspected or replaced at an approximate 24 month -
interval. The combination of surveillance testing and periodic ,
inspections have assured operability of the valves.
F. Safety Implications i
To verify satisfactory operation of safety-related equipment, assurance of check valve operability such that SW flow is not restricted is most critical with the plant at rated power. ,
G. Corrective Action A revised calibration factor was developed and incorporated in the ,
surveillance test procedure. Additionally, the procedure was revised to establish the correct SW System flow for the test and to correctly l state the test acceptance criteria. Assurance of check valve- .
operability was obtained during testing of the B SW Subsystem with the revised procedure on July 8, 1993. Operability of the A SW Subsystem ,
check valves was verified based on performance of the A SW Subsystem ,
post LOCA flow test on June 23, 1993. '
The SW System is unique in that the specification of flow requirements l in the USAR includes an adjustment to ensure required- flow will be 'i obtained at low river levels. This condition is unique for' systems !
contained in the IST Program. For this reason, this is considered.to be .!
an isolated occurrence. 1; t
Correction of the SW System annubar flow monitor K factor completed action taken in response to LEPs93-015 associated with_a similar flow. 4 instrument deficiency in the High Pressure Coolant Injection System, All safety-related flow instruments are considered to be fully operable.
H ., Similar Events l
93-015 High Pressure Coolant Injection System Design Discrepancy _ l Resulting In A Nonconservative Difference Between Actual And j Indicated Flow ;
t l
- wat potu assa eu,s, cen, 39ts+520 569,00070 '
_ $43)
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05000298/LER-1993-001 | LER 93-001-00:on 930225,several Design Discrepancies in SW & Reactor Equipment Cooling Sys Identified.Caused by Piping Configuration Error During Plant Const.Mechanical & Electrical Mods Will Be made.W/930318 Ltr | | 05000298/LER-1993-007 | LER 93-007-00:on 930326,determined That ECCS Pump Compartment Cooler Power Supply Design Defect Could Have Prevented Adequate Containment Heat Removal.Caused by Design Errors.Mods Planned to Provide Convection Cooling | | 05000298/LER-1993-008 | LER 93-008-00:on 930328,4,160-volt Breakers 1BG,1GB & 1GE Tripped Due to Actuation of 1GS Breaker Lockout Relay.Caused by Oversight in Design Change Installation Instructions. Work Stopped & Design Change Implemented | | 05000298/LER-1993-029 | LER 93-029-00:on 930708,partially Withdrawn Control Rod 26-31 Scrammed.Caused by RPS Scram Signal from Two of Four Reactor Pressure Scram Switches.Scram Reset & Pressure Testing completed.W/930806 Ltr | | 05000298/LER-1993-030 | LER 93-030-00:on 930708,discovered Inadequate Inservice Testing of Svc Water Sys Check Valves Due to Flow Instrument Calibr Error & Personnel Error in Specifying Sys Flow Requirement.Revised Calibr Factor developed.W/930809 Ltr | |
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