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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARNG-99-1415, Monthly Operating Rept for Sept 1999 for Daec.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Daec.With NG-99-1226, Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With NG-99-1115, Monthly Operating Rept for July 1999 for Daec.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Daec.With NG-99-0963, Monthly Operating Rept for June 1999 for Daec.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Daec.With NG-99-0835, Monthly Operating Rept for May 1999 for Daec.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Daec.With NG-99-0682, Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With NG-99-0530, Monthly Operating Rept for Mar 1999 for Daec.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Daec.With NG-99-0330, Monthly Operating Rept for Feb 1999 for Daec.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Daec.With NG-99-0020, Monthly Operating Rept for Dec 1998 for Daec.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Daec.With NG-98-2010, Monthly Operating Rept for Nov 1998 for Daec.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Daec.With NG-98-1875, Monthly Operating Rept for Oct 1998 for Daec.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Daec.With NG-98-1717, Monthly Operating Rept for Sept 1998 for Daec.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Daec.With ML20153B4141998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DAEC NG-98-1389, Monthly Operating Rept for July 1998 for DAEC1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DAEC ML20236R3251998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DAEC ML20249B5171998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DAEC ML20247H9381998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DAEC ML20216F6791998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for DAEC NG-98-0650, Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center NG-98-0398, Monthly Operating Rept for Feb 1998 for DAEC1998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for DAEC NG-98-0252, Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center NG-98-0017, Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center1997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center NG-97-2118, Monthly Operating Rept for Nov 1997 for DAEC1997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DAEC NG-97-1959, Monthly Operating Rept for Oct 1997 for DAEC1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for DAEC NG-97-1781, Monthly Operating Rept for Sept 1997 for Duane Arnold Energy Center1997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Duane Arnold Energy Center ML20217C3491997-08-31031 August 1997 Revised MOR for Aug 1997 for DAEC ML20210V1851997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for DAEC NG-97-1452, Monthly Operating Rept for July 1997 for DAEC1997-07-31031 July 1997 Monthly Operating Rept for July 1997 for DAEC NG-97-1258, Monthly Operating Rept for June 1997 for DAEC Per GL 97-021997-06-30030 June 1997 Monthly Operating Rept for June 1997 for DAEC Per GL 97-02 NG-97-1033, Monthly Operating Rept for May 1997 for Duane Arnold Energy Center1997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Duane Arnold Energy Center NG-97-0894, Monthly Operating Rept for Apr 1997 for Duane Arnold Energy Ctr1997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Duane Arnold Energy Ctr NG-97-0674, Monthly Operating Rept for Mar 1997 for Duane Arnold Energy Ctr1997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Duane Arnold Energy Ctr NG-97-0453, Monthly Operating Rept for Feb 1997 for Duane Arnold Energy Center1997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Duane Arnold Energy Center NG-97-0308, Monthly Operating Rept for Jan 1997 for Duane Arnold Energy Center1997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Duane Arnold Energy Center NG-97-0059, Monthly Operating Rept for Dec 1996 for Duane Arnold Energy Center1996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Duane Arnold Energy Center NG-96-2647, Monthly Operating Rept for Nov 1996 for Duane Arnold Energy Center1996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Duane Arnold Energy Center NG-96-2447, Monthly Operating Rept for Oct 1996 for Duane Arnold Energy Center1996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Duane Arnold Energy Center NG-96-2166, Monthly Operating Rept for Sept 1996 for DAEC1996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for DAEC NG-96-1913, Monthly Operating Rept for Aug 1996 for DAEC1996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for DAEC NG-96-1713, Monthly Operating Rept for Jul 1996 for DAEC1996-07-31031 July 1996 Monthly Operating Rept for Jul 1996 for DAEC NG-96-1481, Monthly Operating Rept for June 1996 for Duane Arnold Energy Ctr1996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Duane Arnold Energy Ctr NG-96-1298, Monthly Operating Rept for May 1996 for Duane Arnold Energy Center1996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Duane Arnold Energy Center NG-96-1055, Monthly Operating Rept for Apr 1996 for Duane Arnold Energy Center1996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Duane Arnold Energy Center NG-96-0825, Monthly Operating Rept for Mar 1996 for DAEC1996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for DAEC NG-96-0624, Monthly Operating Rept for Feb 1996 for DAEC1996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DAEC NG-96-0320, Monthly Operating Rept for Jan 1996 for DAEC1996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for DAEC ML20096C3101995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Duane Arnold Energy Ctr NG-95-3516, Monthly Operating Rept for Nov 1995 for Duane Arnold Energy Ctr1995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Duane Arnold Energy Ctr NG-95-3235, Monthly Operating Rept for Oct 1995 for Duane Arnold Energy Ctr1995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Duane Arnold Energy Ctr NG-95-3057, Monthly Operating Rept for Sept 1995 for Duane Arnold Energy Ctr1995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Duane Arnold Energy Ctr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H8991999-10-18018 October 1999 SER Approving Licensee Requests for Relief NDE-R001 (Part a & B),NDE-R027,NDE-028,NDE-R029,NDE-R030,NDE-R032 & NDE-R035. Relief Request NDE-036,denied & Relief Request NDE-R-034, Deemed Unnecessary NG-99-1415, Monthly Operating Rept for Sept 1999 for Daec.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Daec.With ML20212H2381999-09-22022 September 1999 Safety Evaluation Supporting Amend 228 to License DPR-49 NG-99-1226, Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With NG-99-1115, Monthly Operating Rept for July 1999 for Daec.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Daec.With NG-99-0963, Monthly Operating Rept for June 1999 for Daec.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Daec.With ML20195G9901999-06-0909 June 1999 Safety Evaluation Supporting Amend 227 to License DPR-49 NG-99-0835, Monthly Operating Rept for May 1999 for Daec.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Daec.With ML20206N7551999-05-13013 May 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safey-Related Power-Operated Gate Valves NG-99-0682, Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With NG-99-0530, Monthly Operating Rept for Mar 1999 for Daec.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Daec.With ML20207G0251999-03-0303 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety- Related MOVs at Duane Arnold & That Licensee Adequately Addressed Actions Requested in GL 96-05 NG-99-0330, Monthly Operating Rept for Feb 1999 for Daec.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Daec.With ML20202B4311999-01-26026 January 1999 Safety Evaluation Accepting Request for Approval to Use ASME Code Case N-508-1 in ISI Program for Duane Arnold Energy Ctr ML20202B3851999-01-26026 January 1999 Safety Evaluation Addressing Thermo-Lag Related Ampacity Derating Issues.Ampacity Derating Analysis Results Acceptable NG-99-0020, Monthly Operating Rept for Dec 1998 for Daec.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Daec.With ML20206N3211998-12-0707 December 1998 Final Part 21 Rept Re Piston Failure of MSIV Actuator at Daec.Rept Indicates That No Reportable Defect Exists,Per 10CFR21 NG-98-2010, Monthly Operating Rept for Nov 1998 for Daec.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Daec.With ML20196F9571998-11-24024 November 1998 Rev 20 to QA Program Description,Ufsar 17.2 for Daec NG-98-1875, Monthly Operating Rept for Oct 1998 for Daec.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Daec.With NG-98-1767, Cyclic Rept of Facility Changes,Tests & Experiments,Fire Plan & Commitment Changes,For Period from 970301-980930. with1998-09-30030 September 1998 Cyclic Rept of Facility Changes,Tests & Experiments,Fire Plan & Commitment Changes,For Period from 970301-980930. with NG-98-1717, Monthly Operating Rept for Sept 1998 for Daec.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Daec.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML20153B4141998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DAEC NG-98-1389, Monthly Operating Rept for July 1998 for DAEC1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DAEC ML20236X5321998-07-29029 July 1998 Safety Evaluation Re USI A-46 Program Implementation for Plant ML20236W0021998-07-29029 July 1998 Safety Evaluation Accepting Request for Relief NDE-R020 Re Third 10-yr ISI Interval of Plant,Per 10CFR50.55a(a)(3(i) ML20236S2541998-07-14014 July 1998 Special Rept 98-01:on 980629,diesel-driven Fire Pump Was Inoperable for Greater than Seven Days.Caused by Sheared Off Tie Rods on Accessory Drive End of Engine.Evaluated Condition,Procured Parts & Replaced Tie Rods ML20236R3251998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DAEC ML20249B5171998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DAEC ML20247P5651998-05-18018 May 1998 Part 21 Rept Re Model SA-A101 MSIV A' Actuator Showing Evidence of Internal Leakage,In Both Directions Past Pneumatic Piston.Situation Being Reviewed to Determine If Failure Could Pose Substantial Safety Hazard ML20247K1881998-05-0808 May 1998 Rev 0 to Cycle 16 COLR, for May 1998 ML20247H9381998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DAEC ML20217K7251998-04-16016 April 1998 Correction to SE of Relief Request MC-R001 Re Qualification Requirements for non-destructive Exam Personnel Performing Containment Insp ML20216J9171998-04-16016 April 1998 Safety Evaluation Accepting Relief Request MC-R001 for First 10-yr Interval of Containment Insp Program Per 10CFR50.55a (a)(3)(ii),per 971219 Request ML20217K0471998-04-0101 April 1998 Safety Evaluation Authorizing Proposed Alternative in Relief Request NDE-R004 for Plant Third 10-yr ISI Interval,Based on Finding That Compliance W/Code Would Result in Hardship W/O Compensating Increase in Level of Quality & Safety ML20217H8831998-04-0101 April 1998 Safety Evaluation Supporting Request for Relief for Third ISI Program NG-98-0650, Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center ML20216F6791998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for DAEC ML20217F8841998-03-23023 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Program Plan Requests for Relief for Plant NG-98-0398, Monthly Operating Rept for Feb 1998 for DAEC1998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for DAEC NG-98-0252, Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center ML20199L3481998-01-31031 January 1998 Rev 0 to Duane Arnold Energy Ctr Emergency Action Level (EAL) Technical Basis Document ML20249B3331997-12-31031 December 1997 1997 Annual Rept for Alliant Corporation ML20249B3351997-12-31031 December 1997 1997 Annual Rept for Corn Belt Power Cooperative ML20249B3391997-12-31031 December 1997 Central Iowa Power Coopertive 1997 Annual Rept NG-98-0017, Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center1997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center NG-97-2118, Monthly Operating Rept for Nov 1997 for DAEC1997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DAEC ML20199J6841997-11-21021 November 1997 SER Approving Relief Requests to Second 10-year Inservice Inspection Interval for Duane Arnold Energy Center NG-97-1959, Monthly Operating Rept for Oct 1997 for DAEC1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for DAEC 1999-09-30
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lowa Electric Light and Power Company ;
7 July 15,1993 ~
NG-93-2855 Mr. John B. Martin '
Regional Administrator Region 111 U.S. Nucicar Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 !
Subject:
Duane Arnold Energy Center ,
Docket No: 50-331 Operating License DPR-49 June 1993 Monthly Operating Report
Dear Mr. Martin:
i Please find enclosed the Duane Arnold Energy Center Monthly Operating Report for June 1993. The report has
, been prepared in accordance with the guidelines of NUREG-0020 and distribution has been made in accordance with DAEC Technical Specifications, Section 6.11.1.c.
Very truly yours,
[. I David Wilson Plant Superintendent, Nuclear DLW/RBW/cc Enclosures File A-ll8d :
cc !
Dir. of Nuclear Reactor Regulation Mr. Dennis Murdock U.S. Nuclear Regulatory Commission Central lowa Power Cooperative Mail Station PI-137 Box 2517 Washington, D.C. 20555 (Orig.) Cedar Rapids, IA 52406 Mr. Robert Pulsifer Mr. William Loveless Project Manager U.S. NRC 1 Whitenint North I Whiteflint North
- Mail Stop 13E21 Mail Stop 11C14 11555 Rockville Pike 11555 Rockville Pike ,
Rockville, MD 20852 Rockville, MD 20852 (2)
Document Control Desk Dr. William A. Jacobs, Jr.
INPO Records Center GDS Associates,Inc.
- 1100 Circle 75 Parkway Suite 720 ME Suite 1500 1850 Parkway Place
'*$', Atlanta, GA 30339-3064 Marietta, GA 30068-8237 O
t o Mr. Steve Brown ' Mr. Dale Arends 8' lowa State Utilities Board
- O 1,ucas State Office Building Corn 130013th Belt Power Street Nort Coohcrative St Des Moines,IA 50319 . Humboldt, IA 50548 to
.N rd :
Director. Research Services Utility Data Institute NRC Resident Inspector gg 1700'K St. NW Suite 400
.I no Washington, DC 20006 Duane Arnold Energy Center
200006
4 e
OPERATING DATA REPORT DOCKET NO: 50-011 DATE: (i7 71 9.
Unit: loane Arnold Enerav Cente.t COMPLETED BY: lichard Woodward TELEPHONE: (319) 851-7318 OPERATING STATUS
- 1. Unit Name: Quane Arnold Encray Center
- 2. Reporting Period: June 1993 ,
- 3. Licensed Thermal Power (MWt): 1658 - Notes
- 4. Nameplate Rating (Gross MWe): 565 frurbin_ej
- 5. Design Electrical Rating (Net MWe): 13 8
- 6. Maximum Dependable Capacity (Gross MWe): 145_
- 7. Maximum Qcpendable Capacity (Net MWe): 515
-8. If Changes Occur in Capacity Ratings (1tems Number 3 through 7) since the last report, Give Reasons: 14/A
- 9. Power Level to Which Restricted, If Any (Net MWo): 82% (averate for month of Jun_q)
- 10. Reasons for Restrictions, if Any: Thermal power c.spability has decreased slinhtly more than 0.2% 0.gr day singg_the onset of coast-down April 5.1993.
This Month Year-to-Date Cumulative
- 11. Hours in Reporting Period 720.0 4,343.0 161,399.0
- 12. Number of Hours Reactor Was Critical 720.0 4,218.1 120,199.3
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 192.8
- 14. Hours Generator On-Line 720.0 4,203.1 117,225.6
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 992,049.2 6.541,987.0 160,625,280.7
- 17. Gross Electrical Energy Generated (MWH) 324,746.0 2,176,189.0 53,801,098.5
- 18. Net Electrical Energy Generated (MWH) 302,610.0 2,045,379.5 50,442,033.3
- 19. Unit Service Factor 100.0 % 96.8% 72.6 %
- 20. Unit Availability Factor 100.0 % 96.8 % 72.6 %
- 21. Unit Capacity Factor (Using MDC Net) 81.6 % 91.4 % 62.1 %
- 22. Unit Capacity Factor (Using DER Net) 78.1 % 87.5 % 59.4%
- 23. Unit Forced Outage Rate 0.0% 0.0% 12.1 %
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of each): Refueling, July 29,1993, 59 days.
- 25. If Shutdown at End of Report Period, Est. Date of Startup: N/A t
.. .a
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. AVERAGE DAILY UNIT POWER LEVEL DOCKET NO: 50-0331 DATE: 07/15/93 Unit: Duane Arnold Enercy Center -
COMPLETED BY: Richard Woodward TELEPlIONE: (319) 851-7318 MONTil June 1993 Average Daily Average Daily Power Level Power Level Day (MWe-Net) Day (MWe-Net) 1 448 3 16 421.7 2- 446.1 17 412.2 3- 440.5 18 413.6 4 444.2 19 410.9 ,
5 445.0 20 413.2 6 437.2 21 411.1 7 112f(t 22 408.3 8 428.6 23 403.9 9 ilf1(t ' 24 403.4 ,
t 10 132_0 25 407.0 I
11 121 2 26 403 7 12 4131
. 27 iQL3.
13 420 9 28 400.9 14 4216 29 3986 15 425.3 30 398.4 6
I i
1
s REFUELING INFORMATION DOCKET NO: 50-0331 DATE: 07/15/93 Unit: Duane Amold Enemy' Center
- COMPLETED BY: Richard Woodward TELEPHONE: (319) 851-7318
- 1. Name of facility.
Duane Arnold Energy Center
- 2. Scheduled date for next refueling shutdown.
July 29,1993
- 3. Scheduled date for restart following refueling.
September 26,1993
- 4. Will refueling or resumption of operation thereafter :equire a technical specification change or other license amendment?
Received Amendment #192, no further change needed
- 5. Scheduled date(s) for submitting proposed licensing action and supporting information.
Not applicable
- 6. Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new opeinting pmcedures.
No
- 7. The number of fuel assemblies (a) in the core,(b) in the spent fuel stoinge pool , (c) new fuel on the re-fuel floor,
- a. 368
- b. 1152
- c. 128
- 8. The present licensed spent fuel pool stoinge capacity and the size of any increase in licensed storage capacity that has been requested or is planned,in number of fuel assemblics.
- a. 2050 - Licensed Capacity or
- b. 1898 under the presently installed storage rack capacity.
- c. 3152 requested by RTS#252, submitted March 26,1993 i i
- 9. The projected date of the last refueling that can be discharged to the spent fuel pool assuming ,
the present licensed capacity. -
- a. 2000 - Licensed Capacity or
- b. 1998 under the presently installed storage rack capacity.
i
DOCKET NO: 50-0331 .,
DATE: 07/15/93 Unit: Duane Amold Enercy Center COMPLETED BY: Richard Woodward TELEPIIONE: (319) 851-7318 n
UNIT SliUTDOWNS AND POWER REDUCTIONS
. REPORT MONTH: June 1993 There were no shutdowns or power reductions in excess of 20% during the month.
No. Date type Duration Reason Method of Licensee Event System . Comp. Cause (1) (Hours) (2) Shutting Report # Code Code i Down (4) (5)
Reactor (3)
N/A 1 - F: Forced 2 - Reason: 3 - Method: 4 - Exhibit G-S: Scheduled A-Equipment Failure (Explain) 1-Manual Instructions for Preparation of Data Entry B-Maintenance or Test 2-Manual Scram Sheets for Licensee Event Report (LER) File -
C-Refueling 3-Automatic Scram (NUREG-0161)
D-Regulatory Restriction 4-Continued ,
E-Operator Training & License 5-Reduced Load 5 - Exhibit 1 Examination 9-Other (Explain) (Same Source)
F-Administrative G-Operational Error (Explain)
Il-Other (Explain
_. . . . . s _ _ . - . , _ . -
. . .- - . ~ , . _ . . . . .- . -
- 4. ,-
o 6 4 -3, .
"(i DOCKET NO.: 50-033)
. DATE: 07/15/93-Unit: Duane Arnold Enerav Center l COMPLETED BY: Richat _d woodward TELEPIIONE: (319) 851-7318 Monthly Operational Overview for June 1993:
At the beginning of June the DAEC had coasted down to 87% of licensed thermal power.
The core has been in "all-rods-out" configuration since April 5. The plant operated at - 1 uniformly decreasing power capability throughout the month, briefly reducing electric output by 5? MWHe on June 27 to perform Turbine Valve Surveillances. By the end of June, power level had coasted-down to 79%. The coast-down will continue until the refueling outage, now scheduled to commence July 29. l The following table summarizes June plant operation and categorizes production losses in terms of average MWe, capacity factor, and full power equivalent hours. -i Average Capacity Equivalent Full-MWe Factor Power Hours Surveillance losses, control rod movements, etc. 0.1 0.0% 0.1 Seasonal Losses 5.4 1.0% 6.9 ;
Losses due to degraded heat rate 4.9 0.9% 6.2 ;
Other Losses 3.9 0.7% 5.0 Coast-down 100.4 17.7 % 127.8 Actual Gross Electric output 45_LO . 79.7% ' iLLQ Design Gross Electric Output 565.7 100.0 % 720.0 On June 11,1993, with the plant operating at 85% power, while performing the Emergency Diesel Generator (EDG) operability surveillance, the 'A' EDG tripped approximately three seconds after the initial start signal. The most probable cause was determined to be a partially latched mechanical trip mechanism, although this condition was not able to be recreated during troubleshooting efforts. Corrective actions for this event include procedural enhancements, redundant reset operations, and engine stand improvements to facilitate ,
efficient operation of the reset lever. (LER 93-04)
Licensinn Action Summary:
Plant Availability; 100.0 % Unplanned Auto Scrams (w/ Critical) this month: 0 ,
Number of reportable esents: 1 Unplanned Auto Scrams (w/ Critical)last 12 months:2 i
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