|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20012C5131990-03-16016 March 1990 LER 86-029-02:on 860718,19,21 & 870508,loss of Reactor Protection Sys Power Occurred Due to Spurious Tripping of Alternate Feed EPA Breakers.Caused by Low Output Voltage of Alternate Feed Transformer.Output adjusted.W/900316 Ltr ML20006E1571990-02-0909 February 1990 LER 90-001-00:on 900117,unplanned Actuation of ESF Reactor Bldg Standby Ventilation Sys B Occurred,Causing Interlocking Relays in Control Circuits to Deenergize.Caused by Transient Voltage Dip.Procedures Re Bus Loads modified.W/900209 Ltr ML19354D8331990-01-12012 January 1990 LER 89-011-00:on 891222,unplanned Actuation of ESF Primary Containment Isolation Sys Occurred When Performing Sys Layup Implementation Package for Hpci.Caused by Inadequate Procedure.Breaker Positions changed.W/900112 Ltr ML20005F8641990-01-11011 January 1990 LER 89-010-00:on 891212,unplanned Actuation of ESF Control Room Air Conditioning Train a Occurred.Caused by Removal of Leads from Relay During Test to Prevent ESF Sys Actuations. Electrical Relay Replaced & Wiring Mod made.W/900111 Ltr ML20011D2371989-12-15015 December 1989 LER 89-009-00:on 891115,notification Received of Potential Failure Mechanism of Four 3-way Solenoid Operated Pilot Valves.Caused by Incorrect Mounting of Valves.Valves Remounted Vertically & Field Walkdown done.W/891215 Ltr ML19332C5591989-11-15015 November 1989 LER 89-008-00:on 891016,control Room Alarms Received Indicating Fire Pump Had Started & Deluge Valve Had Opened. Caused by Actuation of Manual Pull Station.Deluge Sys Restored to Normal & Personnel interviewed.W/891115 Ltr 1993-06-11
[Table view] Category:RO)
MONTHYEARML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20012C5131990-03-16016 March 1990 LER 86-029-02:on 860718,19,21 & 870508,loss of Reactor Protection Sys Power Occurred Due to Spurious Tripping of Alternate Feed EPA Breakers.Caused by Low Output Voltage of Alternate Feed Transformer.Output adjusted.W/900316 Ltr ML20006E1571990-02-0909 February 1990 LER 90-001-00:on 900117,unplanned Actuation of ESF Reactor Bldg Standby Ventilation Sys B Occurred,Causing Interlocking Relays in Control Circuits to Deenergize.Caused by Transient Voltage Dip.Procedures Re Bus Loads modified.W/900209 Ltr ML19354D8331990-01-12012 January 1990 LER 89-011-00:on 891222,unplanned Actuation of ESF Primary Containment Isolation Sys Occurred When Performing Sys Layup Implementation Package for Hpci.Caused by Inadequate Procedure.Breaker Positions changed.W/900112 Ltr ML20005F8641990-01-11011 January 1990 LER 89-010-00:on 891212,unplanned Actuation of ESF Control Room Air Conditioning Train a Occurred.Caused by Removal of Leads from Relay During Test to Prevent ESF Sys Actuations. Electrical Relay Replaced & Wiring Mod made.W/900111 Ltr ML20011D2371989-12-15015 December 1989 LER 89-009-00:on 891115,notification Received of Potential Failure Mechanism of Four 3-way Solenoid Operated Pilot Valves.Caused by Incorrect Mounting of Valves.Valves Remounted Vertically & Field Walkdown done.W/891215 Ltr ML19332C5591989-11-15015 November 1989 LER 89-008-00:on 891016,control Room Alarms Received Indicating Fire Pump Had Started & Deluge Valve Had Opened. Caused by Actuation of Manual Pull Station.Deluge Sys Restored to Normal & Personnel interviewed.W/891115 Ltr 1993-06-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20135D8011996-11-26026 November 1996 Part 21 Rept Re Two Safety Related Valves Supplied by Velan Valve Corp Were Not in Compliance W/Originally Supplied QA Documentation.Returned Valves to Velan in May 1996 & on 961120 Velan Advised That Valves Had Been Misplaced ML20080G4691995-01-26026 January 1995 Record of Telcon W/Nrc & Licensees 950126 to Clarify Position Re Dispositioning of Exempt Sources Listed in Section 6.3.3 of Shoreham Termination Survey Final Rept Dtd Oct 1994 ML20069F0001994-01-24024 January 1994 Vols 1-4 to Shoreham Decommissioning Project Termination Survey Final Rept ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20057F2261993-09-30030 September 1993 Safety Evaluation Supporting Exemption Request from Requirements of 10CFR50.54(q) for License NPF-82 ML20056C7181993-07-14014 July 1993 SE Supporting Amend 10 to License NPF-82 ML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20045C8881993-06-0808 June 1993 Vols 1 & 2 to Refueling Jib Crane 1T31-CRN-008A Incident Root Cause Analysis. W/One Oversize Encl ML20044C1181993-02-28028 February 1993 Shoreham Nuclear Power Station Updated Decommissioning Plan. ML20128P6451993-02-28028 February 1993 Snps Decommissioning Project Termination Survey Final Rept for Steam Turbine Sys (N31) ML20128P7431993-02-19019 February 1993 Rev 3 to 93X027, Nuclear QA Surveillance Rept ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20128B9641992-10-31031 October 1992 Rev 0 to Shoreham Decommissioning Project Termination Survey Plan ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20099H5781992-07-31031 July 1992 Rev 4 to Shoreham Defueled Sar ML20114A6311992-07-28028 July 1992 Shoreham Decommissioning Plan ML20101K5791992-06-25025 June 1992 Long Island Power Authority Shoreham Decommissioning Project,Shoreham Nuclear Power Station,Technical Rept on Water Processing & Water Mgt Activities for Reactor Pressure Vessel & Wet Cutting Station ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20082M5081991-08-26026 August 1991 Rev 3 to Shoreham Defueled Sar PM-91-125, Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station1991-07-31031 July 1991 Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station PM-91-112, Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station1991-06-30030 June 1991 Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station PM-91-075, Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station1991-04-30030 April 1991 Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr SNRC-1806, Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 19901991-04-15015 April 1991 Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 1990 PM-91-058, Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station1991-03-31031 March 1991 Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station PM-91-037, Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station1991-02-28028 February 1991 Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station PM-91-016, Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station1991-01-31031 January 1991 Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station SNRC-1797, 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 19901990-12-31031 December 1990 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 1990 SNRC-1794, Shoreham Nuclear Power Station Annual Operating Rept,19901990-12-31031 December 1990 Shoreham Nuclear Power Station Annual Operating Rept,1990 SNRC-1799, Lilco 1990 Annual Rept1990-12-31031 December 1990 Lilco 1990 Annual Rept ML20069Q3901990-12-31031 December 1990 Shoreham Nuclear Power Station Decommissioning Plan. (Filed in Category P) ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20056A2001990-07-31031 July 1990 Safety Evaluation Supporting Amend 6 to License NPF-82 PM-90-097, Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station1990-06-30030 June 1990 Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station ML20055E3911990-06-25025 June 1990 Safety Evaluation Supporting Amend 5 to License NPF-82 PM-90-083, Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station1990-05-31031 May 1990 Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station 05000322/LER-1988-0151990-05-16016 May 1990 LER 88-015-02:on 880916,seismic Monitoring Instrumentation, Including Peak Acceleration Recorders,Removed from Svc for More than 30 Days Due to Corrosion on Scratch Plates.Cover Gasket Replaced & Thermal Barrier Mount to Be Installed 05000322/LER-1986-0391990-05-16016 May 1990 LER 86-039-01:on 861006,unplanned Initiation of Reactor Bldg Standby Ventilation Sys Occurred W/All Rods Inserted in Core.Caused by Faulty Design of Retaining Device.Warning Signs Attached to Valve Actuator & Valve Mod Initiated 05000322/LER-1986-0321990-05-16016 May 1990 LER 86-032-01:on 860728,RWCU Isolated on High Differential Flow Sensed by Steam Leak Detection Sys While Placing Filter Demineralizers in Operation.Cause Not Determined. Operating Procedures Revised to Monitor RWCU Sys 05000322/LER-1987-0091990-05-16016 May 1990 LER 87-009-01:on 870203,full Reactor Trip Occurred Due to Perturbation in Ref Leg.Caused by Spurious Low Level Reactor Pressure Vessel Water Level Signal.Existing Level & Pressure Transmitters Replaced W/Newer Models 05000322/LER-1987-0221990-05-16016 May 1990 LER 87-022-01:on 870604,HPCI Test Valve to Condensate Storage Tank,Globe Valve & Hpci/Rcic Test Valve to Condensate Storage Tank Failed to Close Against Sys Operating Pressure.Disc of motor-operated Valve 37 Modified 05000322/LER-1989-0051990-05-16016 May 1990 LER 89-005-01:on 890321,results of Local Leak Rate Test of Core Spray Suction Valve a Determined That Leakage,When Combined W/All Type B & C Penetration Leakages,Exceeded Tech Spec Limit.Caused by Normal Valve Degradation 05000322/LER-1989-0031990-05-16016 May 1990 LER 89-003-01:on 890310,emergency Diesel Generator (EDG) 102 Manually Shutdown During 18-month Surveillance Test Due to Failure of EDG Output Breaker.Cause Not Determined. Replacement Breaker Installed in Cubicle 102-8 05000322/LER-1985-0591990-05-16016 May 1990 LER 85-059-01:on 851219,half Reactor Trip,Full NSSS Shutoff Sys Isolation & Reactor Bldg Standby Ventilation Sys Initiation Occurred Due to Loss of Power to Reactor Protection Sys Bus B.Assembly Breaker Reset 05000322/LER-1987-0351990-05-16016 May 1990 LER 87-035-02:on 871221,880106 & 0330,high Energy Line Break Logic Isolations of RWCU & Main Steam Line Drain Valves Occurred.Caused by Problems W/Temp Monitoring Units. Grounding Scheme Changed & Transformers Rewired 05000322/LER-1988-0031990-05-16016 May 1990 LER 88-003-01:on 880322,unplanned Automatic Initiation of Reactor Bldg Standby Ventilation Sys Side a Occurred During Deenergization of Relay.Caused by Close Placement of Relay Terminals.Wiring Inside Electrical Panels Reworked 1997-05-01
[Table view] |
Text
, - - - .
4 - J x;
c-5 ' '4 :
.o .
- r; 5 . .
7 a' gg f LONG' ISLAND: LIGHTING COM PANY-
/jc L_ -
J" SHOREHAM NUCM AR POWER CT ATION
- P.O. Sf,.2 E2A WADING fHVE R, NEW YORK 11792 '
il., TEL. m m erossoo
' \l ,
PM 90-152'
' September 28,~1990 '! -
-- U di. Nuclear Regulatory Commission Document Control Desk
" Washington, D.C. 20555 f
. }l
Dear. Sir:
'.In accordance with/100FR50.73, enclosed is-Shoreham Nuclear. .
Power, Station's Licensee, Event Report, LER 90-007. -
- j
, . Sin ;: -
rely;youha,- '
A .. 1 )
%1Aww t
' Leonard:J. Cajone' .j
. Plant Manager: .l
=7- , RP/amo; L
Enclosure:
i
- . oc 11- ThomasjT. Martin, Regional Administrator _. !
Institute of Nuclear' Power Operations, Records Center j
i o American'Nuclour Insurers
~
-i SR2.A21'.0200' ]
2
'l
, 1 6)
+
t j
9010050178 900928 l PDR ADOCK 05000322 !
S' PDC-ZE 2 2-P c. . . .. . .
fg
';g C Pon s att,- . U.S.KUCLEA2 At1ULATORY COMMISSION - APPROvf D OM8 NO. 31640104 i E XPl%t3. 4/30!g}
y =,. ,
e ESTIMATED SURDEN f f R til1PONst TO COMPLY TrTM THIS
, . .. LICENSEE EVENT REPORT (LER) EO1"INY'%'O'o'jfo'fv"Ro"t8EsV,'JAYt Tent ftC%'R i
^;'!v"'A?OTV ' " '
< OA^t'"A"UM'"ii,s'J'!ifddTs?"
M'MO0ItiM A "J86o'fET.'Osso?OU'C &f!"**
'i? r eACiuTT NAast ni oOcalT NvMuh m Paar m Shoreham Nuclear Power Station Unit 1 0 15 l 0 l 0 l '013 l2l2 1jorl0l4 h " Unplanned Actuation of Engineered Safety Feature Systems
' Dorina an ~IIrc Surveillance Test tVENT D&T4 ill LIR NUM9th (61 REPORT Daf t 171 OTMtm F ACILITit$ INVOLVED les 8 AcettTv hAMit OOcatt NuustR.Si MONTH DAv f t AR vfAR 88 Uv hu 'm" ' Q'fM MONTM DAY vtAR 01510 l 0 l 01 l l
~ ~
0l 9 d7 9 0 9l0 0 l0l7 0 l0 0l9 2l 8 9l 0 0 1 5 '1 0 1 0 1 0l l l TMis Att.,nT is suSMitito evnevANT TO YME RioviRtMENT: O, i0 C,R i <C c. . ., ., < ,.<,. ,, iiii ;
'
- 30 402thi 20 4064 1 X 80 73iaH2H vl 73.716h1 l n 30 4064aHtlN u 34(aHti to 73teH2Hel 73.711el 1106 0 l 010 30 4esi.iiiHiii _
o0.3ei.H2i e0.73i.H2iewi
_ g O M3 g g a,e,* g 4 i g ,; 30 405leH1Hetil 80 73taH2}M to.73teit28ted611A1 Js6Al
, 30 40stell1Havl 90.736eH His) 10.73teH2Hvi46Hel l
4 30 40slaH1Het to.73teH2Hid) to ?3ieH2Het LICENSEE CONT ACT FOR THIS LER (131 l' NAME TELtPMONE NUM9tn ARI A CODE Georae D. Schnaars, Onerational Ocrnnliance Encineer 5i1l6 Qi 2I9l -l813l010 !
COMPLtf t ONt LINE FOR 1 ACM COMPONENT P AILUME DESCRISED IN TMi$ RIPORT 4131 ll L R P CAust sv8ttM COMPCNENT "#% ^C' "$'oOR, Tan s' CAvst SYSTEM COMPONENT Mg%AC C PRII' $
I I I i i i i i i i i i i i j i i i ; Iiii i i t i i i i SUPPL E Mf S 1.6 REPORT E XPECit0 (14l MONTM DAY vtAR SVOMi$$10N I Ti$ It! res tem..ern Ex9tCTED SV06*,3. 'ON t - ko l- l l AnuACT90.. , <,... . - ,A% ..,<,,......,n., 1 On September 7, 1990 at 1037, an unplanned actuation of the "A" trains of the Engineered Sciety Featui.es Reactor- i
'Bui2 ding Standby Ventilation System (RBSVS) and Control Room
. Air Conditioning (CRAC) occurred. This actuation. occurred
'during the performance of surveillance procedure SP44,650.16. Reactor Building Dif lerential Pressure - Low, Channel Functional Test. During this test.two pairs of i leads were removed from terminal strips to prevent the'ESF system.actuations. However, in this event the technician
. ,also t' aped each pair of leads together which allowed the RBSYS and CRAC initiating relays to energize during the d- functional test. The test was stopped, the RBf'IS and CRAC systems were reset at 1118 and plant management personnel were notified. The NRC was notified at 1134 per 10CFR50.72 Lf' (b)(2)(ii). Corrective actions to prevent this from recurring include procedure revisions and adding a report of j this event to the required reading list for the I&C Section.
i l
. NRC Fe,m 384 (64W
'4 us. CaA... mATa,e ,
=,==.A- ,
EXPtRES 4%22 -
LICENSEE EVENT REPORT (LER)- ' Wo'**15,o,fyggfia,ol'go",$1,7%cfTg o ,*&",'"'! --
- TEXT _ CONTINU ATION - Co"*A*4*Alo,*MM N ginit'J"f,'j,!? lT,5 L',jM5
- P APERwo K Rt flON A N IC ,
r OF MANAGEMENT AND SUDGET,W A5HINGTON, DC 20603, DOCEtt NUtdSER L23 - LER husfDER 161 ' PA04 (31 J ;); 9&C6LtTV esaast til Ytam 88 ff,Q,"L yy*,y,"
Shoreham Nuclear Power Station Unit 1 0 15 ] 0 l 0 l 0 l 3] 2 ]2 91 0 0 l0 l~7 -
0 l0 0l2 0F 0l4 vent . . - t, w mic % w.,im 1 - PLANT AND SYSTEM IDENTIFICATION General Electric - Boiling Water Reactor Energy industry Identification System-(EIIS) codes are identified in the text as [xx].
IDENTIFICATION OF THE EVENT ESF Actuations . (Control Roota Air Conditioning [VI) "A" and iReactor Building Standby Ventilation System [BH] "A") caused by
" inadequate surveillance procedure.
Event Date: .09/07/90 m
.r.
Report Date: 09/28/90
- CONDITIONS PRIOR TO THE EVENT Reactor Defueled - All fuel assemblies-stored in the Spent' Fuel-Pool
-Mode Switch - Refuel Power Level - 0 RPV-Pressure - O psig RPV Tamperature = 121 Degrees F 4s
'i t .
K C P.em SetA (640)
g3 PonM sesA us.mucttAOC w uta m v m _
t xants. Usos? .
"
, ' LICENSEE EVENT R' PORT (LER) *Ss',t'Mo'#a8EdM'Mo*j's,'%
c cog gNgig
"^
En'n'o'#t M,%*0i&Tf',115/c'Ul@"t4'!!NA
, TEXT CDNTINUATl3N- 1
- PA tmwo t Ti N J l'3 N I OF MANAGEMtedT AND DVDot7,W ASM:NOToN.DC 70603 ,
ACILITY ,sAME 11 DOCEti NUMSER (3) - PA06 (3) - '
LIR NUMSER tel "aa "=t' ';'#s7:
$ ,_Sforeham-Nuclear Poser Station Unit 1 0l3 0F 0 l4 0 l5 l0 l0 l0 l 3l2 l 2 9l0 -
0 l 0l7 -
0 l0 !
FIO A mov ausst 4 me.csst asse ash,ewist NAC Asme m W {17) J f
I DESCRIPTION OF'THE EVENT :
.On' September 7, 1990, I&C Technicians were performing Technical 1 Specificati'on Surveillance 4.3.2.1 Table 4.3.2.1-1,_ Item 2.d per SP _44.650.16,. Reactor Building Differential Pressure-Low, Channel L Functional Test.. During the performance of this procedure, 2 I sets of leads were lifted from terminal strips to prevent the o i initi'ation'of the Reactor Building Standby Ventilation System I
(RBSYS) and-the-Control Room Air Conditioning (CRAC) System ~"A" trains. .When the air'was vented off pressure differential; transmitter 1T46*PDT-043A at 1037, an unplanned actuation of the Engineered Safety Feature Systems RBSVS "A" and CRAC "A" occurred. The surveillance test was stopped and RBSYS "A" and p 'CRAC "A" were-reset at 1118. Plant management personnel were l
n'otified and the event was determined to be reportable per 10CFR :y
'50.72(b)(2)(ii). The NRC was notified of the event at 1134. :
L.
SP44.650.16 is a functional test of one of the initiating signals for RBSVS and CRAC. To prevent these systems from' actuating during the test, procedure steps required that two pairs of leads a
'.. be " removed and icolated" from two terminal-strips. Although the i procedure did not say it,= it was the intent of these steps to u separate the leads in order to remove this accident. signal from ii :the RBSYS an'd CRAC initiating circuits. - However, in this event, L as the technician removed each pair of leads from the terminal strips, he also taped.them tog (ther.
This was done because the ,
leads had to be isolated from tre rest of the panel and the technician was under the impression that lifting the leads from the terminal strips alone would prevent th: ESF actuation. By Ltaping the. leads together continuity was maintained in the RBSYS "cnd'CRAC "A" initiating circuits and allowed their initiating L relays to energize when the pressure differential transmitter was E vented.. .
CAUSE'OF THE EVENT The cause of the event was an inadequate procedure. The procedure only stated that lifting the leads would prevent RBSVS
,, :end CRAC automatic initiations. However, it did not specify that
,y each pair of leads had to be individually separated. ,
l
,sRC Peat 30BA 16491 l
~
5
?.
g,,, A 4... .. J J 7 1 ,co ..
EXPIRES:4/30T2 '
] ;
9 ,
. UCENSEE EVENT REPOi;T (LER) - ',7&'y.W120',fiS[ycP,of,' Pay,1,'%Cf'l',?2 Ig",'J!
ic
+
TEXT CONTINUATION . if,',",'o?,16fdi"d 'i# til!'c',"yllO"l Td!'#! .,
P APE RWO Rt U TION R C 6 60 0 0F MANAGEMENT AND DVDGET, WASHINGTON. DC 20603.
- m. l1 P AC,4f7V NAhet (1) . DOCKET NUtdsE A (2) . gg ggg g pggg g ;
- .at it YEAa seg sal p sa 0F 0 l4
~
Shoreham Nuclear Power Station Unit 1 o l5 l 0 l 0 l c 13 l 2 l2 9l 0 -
0 l0 l 7 -
0l 0 O'l 4 TuxT w=s = w wmacr assonm
, ANALYSIS OF THE EVENT There was no safety significance to this event. The plant-is ,
1 ~ chutdown and has been defueled since August 1989. Even if the 1 plant had been operating at ' full powc c the safety significance would be insignificant. Following the unplanned actuation, the i L RBSVS and CRAC "A" systems operated as designed.
HQFRECTIVE ACTIONS
- 1. SP44.650.16 was revised to require that the leads be lifted ,
and individually separated. Additionally, an explanation of-7 how lifting these leads prevents the RBSYS and CRAC i initiations was added to this procedure.-
L '2. This event was discussed in a meeting with I&C. Technicians.
A report of this event will be read by all'I&C personnel.
'3.
' ADDITIONAL INFORMATION
- a. Manufacturer and model number of' failed components (al NoTie L' b. LER numbers of previous similar events LER 85-050,86-026, 86-038,86-044, 88-003,89-010 L
L
.t li NIc ew n assA stam 1
4---- ._ - _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _
. .m ,,
}.
.i.
' -f:
c_ ,. ,
4
':y ; :.
/t t 3.':
%g:'
ps:
!? a. ,
- c , .
i .
l S. -
Institute of Nuclear Power Operations l
Suite 1500:
'1100. Circle 75 Parkway j
Atlanta, Georgia 30339-3064
[. .
(;
American Nuclear Insurers 1:
l The Exchange , Suite 245 li '270 Farmington Ave. d Farmington, CT 06032 Regional' Administrator, US NRC Region 1 10 475 Allendale 7oad la King of Prussi4, PA. 19406 a 1
i.
~
ll_ ,
p i
I' l;
l.
l
(
l } .' r -
- i. 9
- f. ~
r en h
_s
.Jh '
i _ _ _ _ _ _ _ _ _ _ . . _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ .