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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:RO)
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20195F5911998-09-11011 September 1998 Special Rept:On 980812,addl Unseated Wires Were Discovered. Cause Is Unknown at Present Time.Util Evaluated Number of Unseated/Ineffective Wires & Determined Effect on Containment Structural Integrity.Commitments,Encl ML20196B3711998-09-0808 September 1998 Cycle 8 Operating Limits Rept (Olr) ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20198A0151998-06-18018 June 1998 10CFR50.59 Summary Rept 960619 Through 980618, Vols I & Ii,Consisting of Descriptions & SE Summaries for Changes to Procedural UFSAR Changes,Tests & Experiments & FP Rept.Without Fp,Rept ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247F7711998-05-0808 May 1998 Special Rept:On 980403 & 980503 Seismic Monitoring Sys Was Declared Inoperable.Caused by 5-volt Power Supply & Regulator Card Failure.Imd & Sys Engineering Are Continuing to Identify & Resolve Problems So Sys Can Be Operable ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 1999-09-30
[Table view] |
Text
t ..
j Commonwealth Edison . '
,? * " Braidwood Nucb r P wir St: tion N RoutX1. Box 84 1
,~ ' Brac:vi;b. tilinois 60407.
-* Telephone 815/458-2801 November 3,1989 BW/89-2087 ;
F U. S. Nuclear Regulatory Commission Document Control Desk '
Washington, D.C. 20555
Dear Sir:
The enclosed Licensee Event Report from Braidwood Generating 1
, Station is being transmitted to you in accordance with the requirements of 10CFR50.73(a)(2)(v) which requires a 30-day written report. '
This report is number 89-013-00; Docket No. 50-456.
Very truly yours, t
. E. Querto Station Manager Braidwood Nuclear Station g REQ / ADS /sjs (7126z) . ;
Enclosure:
Licensee Event Report No. 89-013-00 L
cc: NRC Region 111 Administrator i NRC Resident inspector INPO Record Center 3 ,
CECO Distribution List 4
9911090274 891103 ,
TM PDR ADOCK 05000456 i S PDC
\
___._______._i__.________..____. .~ . . . _ _ _ _ . . _ _ _ . . . . . . _ _ .. . . . _ _ _
l LICEWSEE EVfMT REPORT (LER)
Facility Name (1) Docket Number (2) _ Pane (3)
Jr114v.eell 1 0151 OLaLDL.allu J_l_.et}J_la_ )
Title (4) Inadequate incorporation of Isolation Requirements For the Steam Generator 81owdown System Ove to a Preservice Design Deficiency
. . Event.Date (5) LER Nimber (61 Repgr.t J ate (7) Other FACil11101 In10lYtdJEL I Mo!.th Day Year Year Sequential / Revision Month Day ~ Year Facility. East &_JosiaL!haptttris)
/j/j//j
// _ Number /j//j/j/__ Numbe r
._.Jraidioed_L._. JULoLolalJL5L2
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_11 o el 5 81 9 B L9_ _ai113 oIo ii1 of 3 819 0151oLotof 1 I-THl$ REPORT IS SUBMITTED PUR$UANT TO THE RE()UIREMENTS OF 10CFR OPNW LCheik one or.nore of.the.followingl.(11)
I" 6 __
20.402(b) ,_ 20.405(c) ._._ 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(1) _ 50.36(c)(1) 3. 50.73(a)(2)(v) __ 73.7)(c)
LEVEL 20.40$(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vli) Other ($pecify l0 ital ! 20.405(a)(1)(li t ) _ 50.73(a)(2)(1) _., 50.73(a)(2)(vill)(A) in Abstract
._._ 50.73(a)(2)(li) _ 50.73(a)(2)(vili)(B) below and in
=///////////////,/,////////,//_20.405(a)(1)(lv)
//////////////}/}////////}/// 20.405(a)(1)(v) __.50.73(a)(2)(lit) __ 50.73(a)(2)(x) Teut)
(IC E$(E_ CONTACT F08 THIS LER (121 Name TE(EEljQHE NUPSER AREA CODE Jialbgyt. TechnIca1 Silfi lDSlattr ExL. 2489 8l115 4l5lBl_Lil3LoL1 E0t!ELLILONLutiLIDRleflLC0tlP9tfMIJAILURLDESLRIBID._1fLIlill_ REPORT (13)
CAUSE SY$ TEM COMPONENT MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT MANUFAC. REPORTABLE TVRER J0. HERD 1. TURER _10_.NERQ1.
I _L._LJ l i I I I I I I I i 1 L_1 I I I I .__
i i I l - I l -l
$UPPLEMEN?AL_RLEQRT EXPEETED (14] Expected tion.th_LossJanar Submission
_ l.Y.t1_Ill yt12_10f!!R111e EXPECTED SUBMIS110N DATE) X l NO
(
l AB3 TRACT (Limit to 1400 spaces, i.e approximately fifteen single-space typewritten lines) (16)
On October 5,1989 a discrepancy with the design of the Steam Generator Blowdown (SD) system was identified.
The Safety Analysis Report (UFSAR) specifies $D isolation on the ir.itiation of the Auxl11ery Feedwater (AF) ,
l System. This minimizes the AF flow requirements. The current design does not provide for a. stomatic l
1 solation on all AF Initiations. The $0 system mas isolated. Changes were made to Escrgency Procedures l r; quiring SD isolation on AF initiation. After these changes SD Operation was permitted. Engineering m cvaluated the affects on the Accident Analysis of the UF$AR. The impacted scenarios were Loss of Normal Feedater (LONF), Loss of Non-emergency AC Power (LOAC), and Feedwater Pipe Break (FSPB). This was due to the lack of a $G Lo Lo Water Level $D isolation on AF initiation. Calculations were perfomed using actual plant data and taking credit for manual SD isolation within 10 minutes for LONF and LOAC events or credit for r: aching a Phase A initiating setpoint within 6 minutes for FSPB events. It was determined that the UFSAR acceptance criteria was met. Braldwood $tation was justified to continue operation provided the BwCP's were rsvised and the permanent modification is completed on a prudent schedule. The modifications are scheduled.
The cause was a preservice design deficiency for unknown reasons. The UFSAR will be revised to reflect the changes. There are no previous occurrences.
2915m(103189)/2
V .
t . ;
. 's LICEMME EVENT REP 0tf (LEtt TEXT Ciufflitl& TION ~
(arm Rev 2.8 ;
' FACILITY NAME (1) DOCKET NUMBER (2) LER MUMBER (6) Paan (31 ,
h~ "
- - % Year /// $sqteential // Revislan fff
/// Number
/j//
ff
/ Numbat.
.Sie.ldw00d,1 - M_L}_DJ_0J_0 1 41 51 6 a I 9' - oI1I3 - oIo el 2 _or el 4 TEXT- Energy Industry Identification System (Ell 5) codes are identified in the text as (XX)
A. PLANT CONDITIONS PRIOR 70 EVENT: ,
e Unit: Braldwood 1: Event Date: October 5, 1989; Event Time: 1200;
' Mode: 6 - Refuel; Rx Power: 0%;
RC$ (AB) Temperature / Pressure: Ambient ,
Unit: Braidwood 2; , Mode: 1 - Power Operation: Rx Power: 100%;
RCS (AB) Temperature / Pressure: NOT-NOP ,
t B.'. DESCRIPTION OF EVENT:
1 There were no systems or components inoperable at the beginning of the event which contributed to the severity of-the event.
l At approximately 1200 on October 5,1989 Nuclear Engineering Department (NED) notified Braidwood Station of an identified discrepancy with the Steam Generator Blowdown (50) (WI) system. The Updated Fin (L Safety Analysis
~
ReportL (UFSAR) and the Westinghouse functional requirements specify $D isolation on the initfation of the-l Auxillary feedwater (AF) (BA) system. Isolation of $0 minimites the AF flow requirements. The current 50 system .
I design provides for isolation on Containment Phase A Isolation and High Energy Line Break Isolation. With the f cxisting design, isolation of the SD system was not assured upon receipt of the following AF initiation signals. !
- 1. Steam Generator ($G) (AB) Lo Lo Water Level.
- 2. Loss of Power to the Reactor Coolant Pumps.
- 3. Manual System initiation.
The $D system was immediately isolated on Braidwood 2 and an initial evaluation was performed. Based on the results of this evaluation the following actions were taken:
- 1. Temporary procedure changes were made to Braidwood Emergency Procedures (BwEP). These changes require Operator Verification / Performance of SD isolation concurrent with verification / performance of AF inttletion in the BwEP's. When these changes were implemented operation of the SD system was permitted.
- 2. NEDw ~ as requested to evaluate the af f ects of the evisting SD system design on the Accident Analysis of the UFSAR.
- 3. The event was conservatively determined te be a four hour reportable event pursuant to 10CFR50.72(b)(2)(lii).
L The appropriate NRC notification via the EN$ phone system was made at 1332 puisuant to 10CFR50.72(b)(2)(ill).
/.
\ .
d' %.
d 12915m(103189)/3
'.. e a * ._ LICENitt EVENT REPORT (LER) TEXT CONTIIRAATION Fare Rev 2.0_
fACILIT'Y NAE (1) DOCKET NUPSER (2) LER NupeER (6) Pane (3) l Year ///
f Sequential //j ff
/ Revision l
/// Number /// Number _ l Braldwood 1 0 1 5 1 0 1 0 1 0_.I 41 51 6 8l9 - 01113 - 010 01 3 0F_ 0l _4 f tXT : Energy Industry Identification System (Ells) codes are identified in the text as (KK)
- 6. DESCRIPTION OF EVENT:- (cont'd)
On October 25, 1989 Braidwood StatI~on received the itED evaluation of lee af fects of $0 system design on the
.UFSAR Accident Analysis.. The evaluation contained _a justification for interis operation (JIO) prepared by Westinghouse Electric Corporation. The evaluation identified three Accident Analysis scenarios that were
~
impacted by current SD system design:
.1. Loss of Normal Feedwater (LONF)
~
- 2. Loss of Non-emergency AC Power to the Plant Auxl11eries (LOAC).
- 3. Feedwater System Pipe Break (FSPB).
Current SD system design had no imoact on the remaining UFSAR Accident Analysis. The conclusions of the ;
cvaluation are summarized below:
- 1. 'The Accident Analysis is affected by the lack of a SG Lo Lo Water Level $D isolation. The Accident Analysis is not af fected by a lack of SD isolation for any other type of AF initiation.
- 2. While the plants were outside the Analysis presented in the UFSAR, at no time were the plants in a ,
condition that posed a risk to the health and safety of the public. .
- 3. Calculations were performed using measured values from actual plant data. These calculations also took credit for manual SD isolation within 10 minutes for LONF and LOAC events or credit for reaching a Phase !
A initiating setpoint within 6 minutes for FSPB events. Based on these calculations it has been determined that the UFSAR acceptance crlieria was met and the conclusions of the UFSAR are valid.
'4 Braldwood Station is justified to continue operation. This justification specifies the following: l
- a. Revisions to the BwEP's to Verify / perform SD system isolation on Af initiation. -e
- b. The permanent modifications will be completed on a prudent schedule during the next outage of sufficient duration. The scheduling will allow for engineering design, material procurement, and outage scheduling.
The BwCP revisions have been made. This was completed on October 5, 1989. The Installation of the modifications are currently scheduled for the first refueling outage for Braidwood 2 and the second refueling cutage for Braidwood 1.
The JID's-detailed discussion of the effects on each accident scenario is included in the Safety Analysis section of Byron LER 89-009-00: Docket No. 50-454.
This event is being reported pursuant to 10CFR50.73(a)(2)(v) - any event or condition that alone could have '
prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the '
consequences of an accident.
2915m(110389)/4
,m ', -
LICEN$EE EVENT. REPORT iLER) TEXT CONTINuaT10N Fere Rev 2.3
-FACit!TY NAME (l) DOCKET NUPSER (2) LER NupBER f61 panal31 '
j' Year /// Sequential /// Revision .
//j/ff ff j//
l Number / Number
.Braidwood 1 01510l010141516 8l9 - 01113 - 0l0 01 4 0F Old TEXT Energy Industry identification $ystem (Ell $) codes are identified in the text as (XX)
, C. CAU$E OF EVENT: .
l
- l The root calse of tHs event was a preservice design ' deficiency. Isolation of $D was specified in the system I functional requirer,ents but was not included in original design documents. The cause of the failure to e I
incorporate the 'pecified'$D isolation requirements into current system design is unknown. The investigation to determine the cause is still in progress. The investigation will be tracked to completion by action item '
456 200-89-17101. Any significant information pertaining to the cause of this failure will be documented in a supplemental report.
D. $AFE b ANALY$l$:
L l This event had no effect on the safety,0f the plant or the public. Based on the NED and Westinghouse l
Evaluation. plant operation has always been within the acceptance criteria of the UFSAR.
l i l- 'Under the worst case condition of sustained inadequate AF flow. the emergency procedures provide for either i
the establishment of feed to the $Gs from the normal feedwater system or cooldown and depressurization of the i RC$ to a point where the Residual Heat Removal System can be placed in service using redundant ECC$
- components.
l l E. CORRECTIVE ACTIONS:
l *
$D was isolated on Braldwood 2, Braidwood I was in Mode 6 with $D and AF removed f rom service. Temporary [
t Procedure changes were made to the BwEP's., these changes require operator Verification / Performance of $0 . ,
- i. itolation on AF initiation events. Upon implementation of these changes, $0 system opetation was permitted.
The SD system will be modified to isolate per the system functional requirements. This Modification is
( currently scheduled for the first refuel outage on Unit 2. This is modification M20-2-89-031 and it will be l' tracked to completion by action item 456-200-89-17102. The modification is currently scheduled for the I
second refuel outage on Unit 1. This is modification M20-1-89-033 and it will be tracked to completion by ection item 456-200-89-17103. -
t The UF$AR will be revised to reflect the correct functional requirements for $0 Isolation as th(y relate to the various AF initiation conditions. This will be tracked to completion by action ite 456-200-89-17104.
F. PREVIOUS OCCURRENCES:
s None l
G. COMPONENT FAILURE DATA: J NIne l
l l
l
~ 1 1
1 2915m(103189)/5
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