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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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Text
F'R.I C) A.IMY'ACCELERATED'RIDS PROCESSIYv)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESS'ION NBR:9503200375 DOC.DATE: 95/03/10 NOTARIZED: NO DOCKET FACIL:50-260 Browns Ferry Nuclear Power Station, Unit 2, Tennessee 05000260 AUTH. NAME AUTHOR AFFILIATION WALLACE,J.E. Tennessee Valley Authority MACHON,R.D. Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 95-002-00:on 950209,reactor scram resulting from turbine trip due to sensed generator load unbalance condition caused actuation of ESF sys.Caused by leaking cooling water line.
Leaking cooling water line replaced.W/950310 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES I D CODE/NAME PD2-4-PD LTTR ENCL 1 1 ID CODE/NAME WILLIAMS,J.
LTTR ENCL 1 1 INTERNAL: ACRS 1 1 AEOD/S PD/RAB~ 2 2 AEOD/SPD/RRAB 1 1 CENTE~02 1 1 NRR/DE/ECGB 1 1 N DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/D IS P/PI PB 1 1 NRR/DOPS/OECB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1' RES/DSIR/EIB 1 1 RGN2 FILE 01 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1
,NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE PIELP US TO REDUCE iVASTE! CONTACTTHE DOCUifENTCONTROL DESK, ROOilI PI-37 I EXT 504'2083 ) TO ELIXIINATE YOUR NAiIE PRO~I DISTRIBUTION LISTS I:OR DOCl CLIENTS YOU DON "I'EED FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28
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R. D. tRickj Machon Vce P.esca-.. B. cvics =eg v cea >a",l March 10, 1995 U.S. Nuclear Regulatory Commission 10 CFR 50.73 ATTN: Document Control Desk Washington, D.C. 20555
Dear Sir:
BROWNS FERRY NUCLEAR PLANT (BFN) UNZTS 1~ 2~ AND 3 - DOCKET NOS. 50-259~ 50-260~ AND 296 FACZLZTY OPERATZNG LZCENSE DPR-33~ 52~ AND 68 LZCENSEE EVENT REPORT 50-260/95002 The enclosed report provides details concerning a reactor scram on February 9, 1995, that resulted from a turbine trip.
The turbine trip occurred as part of a sensed generator load unbalance condition. The reactor scram subsequently resulted in actuating the engineered safety feature system.
This report is submitted in accordance with 10 CFR 50.73 (a)(2)('v) as a condition that resulted in the automatic actuation of any engineered safety feature.
Sincerel
~ p, Q)QaL ~
R. D. Machon Site Vice President Enclosure cc: See page 2 9503200375 950310 PDR ADOCK 05000260 S
PDR
41
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U;S. Nuclear Regulatory Commission Page 2 March 10, 1995 Enclosure cc (Enclosure):
INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, G'eorgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West Hartford, Connecticut 06107 NRC Resident Inspector Browns Ferry Nuclear Plant Route 12, Box 637 Athens, Alabama 35611 Regional Administrator U.S. Nuclear Regulatory Commission Region 101 II Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 Mr. J. F. Williams, Project Manager U'.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852 E. V. Imbro, NRR/RSIB U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockvi.'lie, Maryland 20852 E. J. Leeds, NRR/DRPW U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike
.Rockville, Maryland 20852
NRC FORK.366 '.S. IRJCLEAR REGULATQIY CQNIISSIQI APPROVED BY QRI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY lllTH THIS INFORHATIOH COLLECTIOH REOJEST: 50.0 HRS ~
LXCENSEE EVENT REPORT (LER) FORNARD COHHEHTS REGARDIKG BURDEN ESTlllATE TO THE IHFORHATIOH AND RECORDS HANAGEHENT BRANCH (HHBB 7714), U.ST KUCLEAR REGULATORY COHHISSIOH, (See reverse for required nunber of digits/characters for each block) MASNINGTOH, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3110-0104), OFFICE OF HAKAGEHENT AND BNJGET llASHINGTOK DC 20503.
FACILITY NNK (1) DOCKET IRMGI (2) PAGE (3)
Browns Ferr Nuclear Plant BFN Unit 2 05000260 1OF7 TITLE (4) Reactor scram resulting from a turbine trip due to a sensed generator,'load unbalance condition caused the actuation of the ESF system.
'EVENT DATE 5 LER IRMKR 6 REPQIT DATE 7 OTHER FACILITIES INVOLVED 8 FACILITY NAHE NA DOCKET NlÃSER SEGUENTIAL HONTH DAY TEAR YEAR NUHBER'EVISION NUHBER HOHTH DAY TEAR FACILITY KAHE NA DOCKET KUHBER 02 09 95 95 002 00 03 10 OPERATING THIS REPQIT IS SH3HITTED PIKISUANT TO THE REEÃJIRGKHTS OF 10 CFR: Check one or more 11 IKIE (9) N 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b) 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
RXKR 100 50.36(c)(2) 50.73(a)(2)(vii)
LEVEL (10) 20.405(a)(1)(ii) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i)(B) 50.73(a)(2)(viii)(A) (Specify in 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) Abstract below and in Text, 20.C05(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A I.ICENSEE CQITACT FOR THIS LER 12 NAHE TELEPHONE KIKIBER (Include Area Code)
James E. Wallace, Compliance Licensing Engineer (205)729-7874 CQC>LETE OHE LINE FOR EACH'COPOIENT FAILURE DESCRIBED IN THIS REPQIT 13 REPORTABLE REPORTABLE CAUSE SYSTEH COHPOKENT HANUFACTURER CAUSE STSTEH COHPOHENT HANUFACTURER TO HPRDS TO NPRDS RPPLHKNTAL REPORT EXPECTED 1C HOKTH OAY YEAR EXPECTED TES SIKNIISS I ON (If yes, complete EXPECTED SUBHISSIOH DATE). DATE .(15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten Lines) (16)
On February 9, 1995, at '0028 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br />, the Unit 2 reactor scrammed due to a turbine trip.
This trip was a result of a sensed generator load unbalance condition. The scram then
- resulted in the automatic actuation of the engineered safety feature (ESF) system. This event is, therefore, reportable in accordance with 10 CFR 50.73 (a)(2)(iv) as a condition.
responsible for an automatic actuation of the ESF system. The root cause of the event was a degraded subcomponent. Specifically, a leaking cooling water line manifold dripped water on the rectifier circuitry potentially creating a path to ground. Additionally, two generator field rectifier banks had a low-resistance to ground condition. Corrective actions to preclude recurrence are: (1) the leaking cooling water line was replaced,,and (2) a determination will be performed, for additional corrective actions based on a failure analysis of the leaking cooling water manifold and analytical tests of the rectifier cooling water tubes.
KRC FORH 366 (5-92)
4l HRC FORN 366A U.S. IN)CLEAR REGULATQIY CQHIISSIQI APPROVED BY QHI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTINATED BURDEN PER RESPONSE TO CONPLY HITH THIS INFORNATION COLLEC'IIOH REQUEST: 50.0 HRS. FORHARD CQBIENTS REGARDIHG BURDEN EST INATE TO THE INFORNAT ION AND RECORDS NANAGENENT BRANCH (NHBB 7714), U.S. NUCLEAR REGULATORY CQBIISSIOHg LICENSEE EVENT REPORT IIASHIHGTOH, DC 20555-0001, ANO TO THE PAPERIJORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF NANAGENEHT AND M)GET ~
WASHINGTON OC 20503 FACILITY IWK <<1) DOCKET IRRRER (2) LER INHALER (6) PAGE (3)
YEAR SEQUEHTIAL REVISION NQIBER NWER Browns Ferry Unit 2 05000260 95 002 00 2 of 7 TEXT lf sere s ce Is r fred use edditfonaI c Ies of MRC Form 366A (1/)
PLILNT CONDITIONS At the time this event was discovered, Unit 2 had been operating at 100 percent power for 66 days. Units 1 and 3 were shutdown and defueled.
II'ESCRIPTION OF EVENT A. Event At 0028 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> Central Standard Time (CST) on February 9, 1995, Unit 2 experienced a reactor scram while the unit was at full power. The Unit 2 main generator field ground relay '[TL, RLY) actuated and provided a Unit 2 main generator exciter ground alarm in the control room due to a grounding condition. The generator output breaker [TL, BKR] (PCB224) opened after a generator load unbalance was sensed. Subsequently, a generator load reject signal caused the turbine control valves (TCV) [FCV) to fast close because the turbine first stage pressure was greater than 154 psig. The TCV fast closure resulted in a reactor scram signal.
This reactor scram actuated the primary containment isolation system, specifically, group 2- shutdown cooling mode of the residual heat removal system [BO); group 3- reactor water cleanup system [CE); group 6- primary containment purge and vent
[JM), Unit 2. reactor zone ventilation [VB), refueling zone ventilation [VA), standby gas treatment system [BH) initiation, and control room emergency ventilation [VI] initiationI and group, 8- transverse in-core probes [IG] withdrawal.
On February 10, at 0657 hours0.0076 days <br />0.183 hours <br />0.00109 weeks <br />2.499885e-4 months <br /> CST the reactor was restarted and synchronized to the TVA system grid.
This event is reportable in accordance with 10 CFR 50.73 (a)(2)(iv) as a condition responsible for an automatic actuation of the ESF system.
B. Ino erable Structures Cpm nents or S stems that Contributed to the Events None.
II
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NRC FERN 36QL U.S. IRICLEAR REGUIATERY CQSIISSI ON APPROVED SY QRI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY llITH THIS INFORHATIOH COLLECT I OH REOUEST I 50 ~ 0 HRS. FORNARD CQBEENTS REGARDING BURDEN EST IHATE TO THE INFORHATION AND RECORDS HANAGEHENT BRANCH (HHBB 7714), U.S. NUCLEAR REGULATORY CQHIISSIOH, LICENSEE, EVENT REPORT MASH INGTON, DC 20555-0001, AND TO THE PAPERHORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF HAHAGEHEHT AND BUDGET, l!ASH INGTOH DC 20503 FACILITY NA% (1) DOCKET IRMKR (2) LER IRMKR (6) PAGE (3)
'YEAR SEQUENTIAL REVISION NUHBER HIHEBER
'Browns Ferry Unit 2 05000260 95 002 00 3 of 7 TEXT lf more s ce is r ired use edditionei co ies of NRC Form 3 66A (17)
Co Dates and A roximate Times of Ma or OccurrencesI February 9, 1995 at 0028 CST The Unit 2 reactor scrammed due to a turbine trip. The Unit 2 emergency operating instruction (2-EOI-1) was entered because of a low reactor water level.
February 9,- 1995 at 0030 Reactor water level was normalized, Unit 2 was stable, and 2-EOI-1 was exited.
February 9, 1995 at 0225 TVA provided a 10 CFR 50.72(A)(2)(ii) notification to NRC operations center that the reactor scrammed and the ESFs automatically actuated.
February 9, 1995 at 2000 Control rods were being pulled to restart the Unit 2 reactor.
February 10, 1995 at 0657 The reactor was restarted and synchronized to the TVA system grid+
D~ Other S stems or Seconda Func'.ons Affected:
None.
Eo Method of Discove This condition was discovered when the control room received the Unit 2 main generator exciter ground alarm and subsequent turbine and reactor trips.
Fo 0 erator Actions!
Once the reactor scrammed, Operations personnel [licensed, utility]water entered 2-EOI-1 to control the reactor for a low level condition. Operations personnel then reactor responded to the scram in accordance with the approved reactor scram procedure (2-AOI-100-1), and the reactor was stabilized within two minutes. The EOI was then exited'.
0 I'
NRC F(WN 366A U.S. IN)CLEAR REGULATORY C(NBIISSI(NI APPROVED BY (NNI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESl'IHATED BURDEN PER RESPONSE TO CONPLY UITH THIS INFORNATION COLLECTION REQUEST: 50 ~ 0 HRS ~ FORMARD COINIENTS REGARDING BURDEN EST INATE TO THE INFORNAT ION AND RECORDS NANAGENENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COINIISSION, LZCENSEE EVENT REPORT NASH INGTON, DC 20555-0001, AND TO THE PAPERNORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFF ICE OF HAMAGEHENT AND BUDGET, llASHINGTON DC 20503 FACILITY NAlK (1) DOCKET IRRRER (2) LER IWIER (6) PAGE (3)
YEAR SEQUENTIAL REVISION NIIIBER HINGE R Browns Ferry Unit 2 05000260 95 002 00 4 of 7 TEXT If more s ce is r ired use additions( co les of NRC Form 366A ('17)
G. Safet S stem Res nsesl All safety systems responded as designed for th'is type of event.
II'AUSE OF THE EVENT A. Zsuaediate Cause:
The immediate cause of the 'event was the Unit 2 main generator exciter ground relay activated eventually resulting in a reactor scram.
B. Root Causes TVA's investigation of'his event determined that .the cause of the event was a degraded subcomponent. Specifically, a stator cooling water leak from the top of the generator field rectifying cooling water manifold in PRC 1 (See Figure 1) dripped on rectifier components potentially creating a path to ground. Additionally, two generator field PRCs (2 and 5) had a low-resistance to ground state due to internal deposition of corrosion products (copper oxides) in their teflon insulating tubes.
IV. ANALYSIS'F THE EVENT The BFN FSAR contains an analysis of a generator load re)ect/scram transient. In that transient, the FSAR assumes a starting point of greater than 100 percent power and associated steam flow. The analysis also assumes that the turbine bypass valves fail to open.
Plant systems are designed to respond to such a transient. This LER event was much less severe than the analyzed FSAR transient. Thus, this event was bounded by the plant safety analysis.
The main generator PRCs take the AC output voltage of the alternator exciter and rectifies it to produce a DC voltage which is applied to the main generator. Each rectifier circuit contains diodes that are mounted on a rectangular copper heat sink through which deionized water from the generator cooling system is circulated. The deionizing water is carried between heat sinks through metal piping and teflon insulating tubes which, also serve as electrical insulation from ground. The "as found" condition revealed two anomaliesl (1) a water leak from the upper metal manifold in PRC 1, and (2) low-resistance path to ground in two cubicles (PRCs 2 and 5).
NRC FQUI 366A U.S. IN)CLEAR REGULATORY CQBIISSIQI APPROVED BY QNI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPOHSE TO COMPLY IJITH THIS INFORMATION'OLLEC'I IOM REQUEST: 50.0 HRS. FORMARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (HHBB 7714), U.S. NUCLEAR REGULATORY CQBIISSIOH ~
LICENSEE EVENT REPORT HASHIMGTON, DC 20555-0001, ANO TO THE PAPERlORX REDUCTION TEXT CONTINUATION PROJECT (3150.0104), OFFICE OF MANAGEMENT AND BLSGETg
'WASHINGTON DC '20503 FACILITY IWK (1) NXXET IRMKR (2) LER RMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION NLNBER MIN(BER Browns Ferry Unit 2 05000260 95 002 00 5 of tf more 7'EXT s ce is r ired use edditioneL c ies of NRC Form 366A (17)
During this event, the turbine and reactor protective systems actuated as designed to mitigate a scram from 100 percent power, and Operations personnel actions brought the reactor to a stable condition within two minutes to minimize the effect of the plant scram. Consequently, the plant parameters remained well within the bounds of the BFN safety analysis. Therefore, the health and safety of plant personnel and the public as a result of this event were not compromised.
V CORRECTIVE ACTIONS A Immediate Corrective Actions:
personnel responded to the reactor scram. Operations and Technical Support personnel isolated and meggered the main generator circuitry, and identified that PRCs lg 3g 4g and 6 had B'perations a resistance of 10M ohms to ground while PRCs 2 and 5 had a resistance of 300K ohms and 100K ohms to ground, respectively.
Associated circuitry included the Alterrex stator and PRC circuitry measured in the "as found'ondition had 100K ohms of resistance to ground. When this electrical troubleshooting was being performed, a water leak was identified from the top of the PRC 1 cooling water line manifold onto rectifier components below. The PRCs 2 and 5 low-resistance conditions were eliminated by 'the cleaning/replacing of the teflon insulating tubes of the cooling water lines until a 1.5M ohms resistance was achieved in the associated circuitry.
Corrective Actions to Prevent Recurrence:
Corrective actions to preclude recurrence are: (1) PRC 1 leaking cooling water line manifold was replaced, and (2) a determination will be performed for additional corrective actions based on a failure analysis of the leaking cooling water manifold and analytical tests of the rectifier cooling water tubes.
If the results of this analysis significantly alter either the root cause or corrective actions for this event, a supplemental report will be submitted.
VI. ADDITIONAL INFORMATION Failed Com nents:
The main generator power rectifierB had multiple grounds as described i.n section III.
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NRC FORK 366A U S. WCLEAR REGULATIXIY IXXSIISSIIXI APPROVED BY (BNI NO. 3150-0104 (5-92) EXPIRES 5/3'I/95 ESTIKATED BURDEN PER RESPONSE TO CO(PLY UITH THIS INFORKATIOH COLLECTIOH REQUEST: 50.0 HRS. FORllARD CQIBIENTS REGARDIHG BURDEN ESTIKATE TO THE IHFORKATION AND 'RECORDS KANAGEKENT BRANCH (KNBB 7714), U.ST NUCLEAR REGULATORY COIBIISSIOH, LICENSEE EVENT REPORT llASHINGTON~ DC 20555-0001, AND TO THE PAPERIJORX REDUCTION TEXT CONTINUATION PROJECT (3150 0104), OFFICE OF KANAGEKENT AND BUDGET, UASHINGTON DC 20503 FACILITY IWK (1) DOCXET IRBSER (2) LER IRBIBER (6) PAGE (3)
TEAR SEQUENTIAL REVISIOH NIR(BER NIR(BER Browns, Ferry Unit 2 05000260 95, 002 00 6 of 7 TEXT tf more s ce is r ired use additional co ies of NRC Form 366A (17)
Previous LERs on Similar Eventst LER 259/84024 provided details concerning a reactor scram resulting from a turbine-generator trip. The corrective action to preclude a recurrence was to reduce the size of the in-line filter to minimize the deposition of iron and copper onto the teflon insulating tube. Since that time, TVA'as initiated a preventive maintenance task to chemically clean the teflon tubes every 36 months to further reduce the recurrence of this type of event. The change to reduce the size of the in-line filter would not have precluded this event (LER 260/95002).
VII. Co itments Not all actions described in section V of this report are Regulatory Commitments. That is, they are not actions required to restore compliance with obligations. Obligations mean an action that is a legal binding requirement imposed through applicable rules, regulations, orders, and licenses. The only commitment is identified below:
A determination will be performed'or additional corrective actions nd based on a failure analysis of the leaking cooling water manifold analytical tests of the rectifier cooling water tubes. This determination will be completed by June 16, 1995.
Energy Industry Identification System (EIIS) system and component codes are identified in the text with brackets (e.g., [XX].
~I NRC FORN 366A U.S NUCLEAR REGULATORY CONIISSION 'APPROVED BY (BIB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTINATED BURDEN PER RESPONSE TO CONPLY MITH THIS INFORNATIOH COLLECTION REQUEST: 50.0 HRS. FORl!ARD CONHENTS REGARDING BURDEN ESTIMATE TO THE INFORHATION AHD RECORDS NANAGENENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY CONNISSION, LICENSEE EVENT REPORT NASHINGTON, DC 20555-0001, AND TO THE PAPERHORK REDUCTIOH TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF NANAGEHEHT AND BUDGET, NASHINGTOH DC 20503 FACILITY NANE (1) DOCKET HI%BEN (2) LER Hi%HER (6) PAGE (3)
YEAR SEQUENTIAL ,REVISION HUNBER NURSER Browns Ferry Unit 2 05000260 95 002 00 7 of 7 TEXT tf more s ece is r uired use eddittonel co ies of NRC Form 366A (17)
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