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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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NRC FORM 366 U.S. NUCLEAR REGULATORY COHHISSION PPROVED BY OMB No 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE To COMPLY WITH THIS INFORHATION COLLECTION REaUEST: 50.0 HRS ~
LICENSEE EVENT REPORT (LER) FORWARD COMHENTS REGARDING BURDEN ESTIHATE TO THE INFORHATION AND RECORDS HANAGEMENT BRANCH (HNBB 7714), U.ST NUCLEAR REGULATORY COMHISSION, (See reverse for required number of digits/characters for each block) WASHINGTON, Dc 20555.0001 AND To THE PAPERWORK REDUCTION PROJECT (3110-0104), OFFICE OF MANAGEHENT AND BUDGET WASHINGTON DC 20503.
FACILiTY NAME (1) DOCKET NUHBER (2)
Browns Ferry Nuclear Plant (BFN) Unit 2 05000260 PAGE (3) 1 of 6 TITLE (4) Main steam Safety Relief Valves Exceeded the Technical Specifications Required Setpoint Limit as a Result of Disc/Seat Bonding EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SEQUENTIAL REVISION FACILITY NAME DOCKET NUHBER MONTH DAY YEAR YEAR NUHBER NUMBER MONTH DAY YEAR NA FACILITY NAME DOCKET NUHBER 02 07 95 95 003 02 4 09 97 NA OPERATING THIS REPORT IS SUBMITTED PURSUAHT To THE REQUIREMENTS OF 10 CFR 5: (Check one or mor e) (11)
MODE (9) N 20.402(b) 20.405<c) 50.73(a)(2)(iv) 73.71(b) 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
POWER LEVEL (10) 100 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405<a)(1)(iii) 50.73(a)(2)(i)(B) 50.73<a)(2)(viii)(A) (Specify in 20 '05(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) Abstract below and in Text, 20.405(a)(1)<v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A)
LICEHSEE CONTACT FOR THIS LER (12)
NAHE TELEPHONE NUMBER (Include Area Code)
James E. Wallace, Licensing Engineer (205)729-7874 COHPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IH THIS REPORT (13)
SYS REPORTABLE REPORTABLE CAUSE COMPONENT MANUFACTURER CAUSE SYSTEH COMPONENT MANUFACTURER TEM To NPRDS To NPRDS X SB RV T020 SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED HONTH DAY YEAR YES SUBH I SS ION (lf yes, complete EXPECTED SUBMISSION DATE).
X NO DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typeMritten lines) (16)
On March 1, 1995, Wyle Laboratories notified TVA that 11 of the 13 Unit 2 main steam safety/relief valves (SRVs) failed the setpoint acceptance tests. The SRV setpoints were found outside the Technical Specification (TS) limit of +/- one-percent setpoint tolerance. This condition is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by the plant's TS. The apparent cause was attributed to corrosion bonding of the SRV pilot disc/seat interface resulting in an upward setpoint drift. TVA has implemented the Boiling Water Reactor Owners Group (BWROG) recommendation to replace the main steam SRV pilot cartridges with cartridges that have a 0 ' percent platinum alloyed stellite pilot disc. During the Unit 2 Cycle 7 refueling outage, TVA removed the SRV pilot cartridges from the Unit 2 main steam SRVs and replaced them with the BWROG zecolomended cartridges. Using the platinum alloyed disc should help to reduce corrosion bonding and decrease setpoint drift problems in the future.
9704i50ii8 970409 05000260 PDR ADOCK S PDR NRC FORM 66 ( -92)
0 ~l NRC FORM 36QL U S. NUCLEAR REGULATORY COHMISSION APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY MITH THIS INFORHATION COLLECTION REOUEST: 50.0 NRS. FORNARD COHHENTS REGARDING BURDEN EST IHATE TO THE INFORMATION AND RECORDS HANAGEMENT BRANCH (MNBB 7714), U.S..NUCLEAR REGULATORY COHHISSION, LZCENSEE EVENT REPORT NASNINGTON, DC 20555-0001, AND TO THE PAPERMORK REDUCTION TEXT CONTINUATION PROJECT (3'150-0104), OFFICE OF HANAGEHENT AND BUDGET, WASHINGTON DC 20503 FACILITY HAME (1) DOCKET'UMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION NUHBER NUHBER Browns Ferry Unit 2 05000260 2 of 6 TEXT lf more s ace is r uired use additional co ies of N C Form 366A (17)
Z. PLANT CONDZTZONS At the time of the event, Unit 2 was in its Cycle 7 refueling outage.
Units 1 and 3 were shutdown and defueled.
zz. DESCRZPTZON OF EVENT A. Event:
On March 1, 1995, Wyle Laboratories notified TVA that 11 of the 13 Unit 2 main steam [SB] SRVs [RV](Target Rock Two-Stage SRV Model No. 7576F) failed the setpoint acceptance tests. The SRV setpoints were found outside the Technical Specification (TS) limit of +/- one-percent setpoint tolerance.
During the Unit 2 Cycle 7 refueling outage, the .SRV pilot cartridges were removed from the Unit 2 main steam SRVs and sent to Wyle Laboratories for testing. On February 7, 1995, the first two SRV pilot cartridges were bench tested, and the test results showed that the pilot cartridges caused the SRVs to open outside the TS limit (i.e., the test results were +3.85 percent and +1.95 percent, respectively). On March 1r 1995I bench test results on 'the remaining SRV cartridges indicated 9 more SRVs opened outside the one-percent setpoint tolerance (from +2.93 percent to +9.80 percent). Altogether, 11 valves failed the setpoint test acceptance criteria.
The above condition is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by the plant's TS.
B. Zno erable Structures, Co onents, or S stems that Contributed to t e Event:
None.
C. Dates and A roximate Times of Ma or Occurrences:
During the Unit 2 Cycle 7 outage (October 1, 1994 through November 23, 1994), SRVs pilot cartridges were removed'rom the Unit 2 main steam SRVs and shipped to Wyle Laboratories for testing. On February 7, 1995, TVA was notified on the results of the first two SRVs tested. On March 1, 1995, Wyle testing results.
Laboratories notified TVA of the remaining SRV
4i S Lr
NRC .FORH U.S. NUCLEAR >REGULATORY COMHISSION APPROVED BY 0MB'NO. 3150-0104 366A'5-92)
EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY 'MITH THIS INFORMATION COLLECTION REQUEST: 50.0 NRS ~ FORNARD COMHENTS REGARDING BURDEN EST IHATE TO THE INFORMATION AND RECORDS MANAGEHENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, LICENSEE EVENT REPORT llASHINGTON, DC 20555-0001, AND TO THE PAPERMORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFF ICE OF HANAGEHENT AND BUDGET,
'WASHINGTON DC 20503 I
'FACILITY NAHE (1) DOCKET NUMBER (2) LER NUHBER (6) PAGE ( )
YEAR SEQUENTIAL REVI SION NUMBER 'NUMBER Bzowns Ferry Unit 2 05000260 3 of 6 TEXT f more s sce is r uired use additional co ies of NRC Form 366A (17)
D. Other S stems or Seconda Functions. Affected:
None.
E. h5sthod of Discove The deviation from the SRV setpoints was identified during the scheduled performance of valve bench testing at Wyle Laboratories in Huntsville, Alabama.
F. erator Actions:
None ..
G. Safet S stem Res onses:
None.
ZIZ. CAUSE OF THE EVENT A. Immediate Cause:
The immediate cause was due to SRV pilot disc/seat bonding resulting in the SRV setpoints deviating outside the TS setpoint limit of +/- one-percent.
B. Root Cause:
The apparent cause of this bonding was attributed to corrosion at the two-stage SRV pilot disc/seat interface. Since corrosion bonding caused an increase in the valve opening pressure due to the need for additional opening force above the setpoint value, this resulted in an upward setpoint drift.
ANALYSIS OF THE EVENT Thirteen SRVs on the main steam piping. perform the safety/relief function for the primary reactor system boundary. Each valve is des'igned to open at a pressure sensed in the valve body of 1105, 1115, or 1125 psig providing a safety/relief function. The safety/relief function of the SRVs is to limit primary reactor system pressure to (1375 .psig in the event of a pressurization transient resulting from a turbine trip or a main steam isolation valve closure.
TVA performed a limiting pressuri'zation transient analysis fox Unit 2 Cycle 6 assuming a spectrum of SRV failures and setpoint drifts. The analysis concluded that even if four SRVs completely fail,to open and the remainder operate at ten percent above setpoint, the primary
0 A(
HRC.FORM 366A U.S. NUCLEAR REGULATORY COMMISSIOH APPROVED BY OHB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORHATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION/
LZCENSEE EVENT REPORT WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF MANAGEMENT AHD BUDGET, WASHIHGTON DC 20503 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER Browns Ferry Unit 2 05000260 4 of 6 TEXT If more s ce is e ired use additional co les of NRC Form 366A (17) reactor system pressure would not exceed the TS safet'g 1imit of 1375 psig. Considering the conservative inputs to this analysis and the low sensitivity of the pressurization transient to cycle-by-cycle loading differences, the failures observed in this event would not have zesulted in exceeding the TS safety limit during any abnormal operational transient. Thus, the plant and public safety would not have been adversely affected and the safety of plant personnel was not co111proIM sede CORRECTZVE ACTZONS A. Zmmediate Corrective Actions:
The out-of-tolerance valves are currently being retested and recertified by Wyle Laboratories for future use at BFN.
B. Corrective Actions to Prevent Recurrence:
The setpoint drift is a generic concern experienced by utilities using this brand of SRV in boiling water reactors (BWR) and is being investigated by the BWR Owners'roup (BWROG) SRV Drift Fix Development Committee and the manufacturer, Target Rock Corporation.
The Committee recommended replacing the existing stellite 6B pilot disc with a 0.3 percent platinum alloyed stellite or installing several parts in the pilot disc/seat area with catalyst plated platinum alloy to act as a recombiner of excess oxygen, thereby reducing the oxygen available for corrosion.
(Note: corrosion is being attributed to radiologically produced oxygen collecting at the disc/seat interface.)
At this time, TVA has elected to replace the Unit 2 stellite 6B pilot discs with platinum alloyed stellite dies. During the Unit 2 Cycle 7 refueling outage, TVA removed the SRV pilot cartridges from the Unit 2 main steam SRVs and replaced them with cartridges refurbished with a 0.3 percent platinum alloyed stellite pilot disc.
Additionally, pez TS requirements, the SRVs aze bench tested and checked for any increased setpoint deviation or drift at the end of each operating cycle. As a SRV Drift Fix Committee member, TVA is continuing to participate in the BWROG evaluation on the long term solution concerning the SRV setpoint drift problem.
Following this Unit 2 operating cycle, TVA plans to evaluate the SRV test results, as well as relevant industry operating experience, to detexmine future actions foz BFN Units 1, 2, aIld 3.
Cl HRC FORH 366A U.S. NUCLEAR REGULATORY COHHISSIOH APPROVED BY OHB NO. 3150-0104 (5-92) EXPIRES'5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 .HRS. FORWARD COHHEHTS REGARDING
. BURDEN ESTIMATE TO THE INFORMATION AHD RECORDS MAHAGEHENT BRANCH (HNBB 7714), U.ST NUCLEAR REGULATORY COHHISSION, LICENSEE EVENT REPORT WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION TEXT'ONTINUATION PROJECT (3150-0104), OFFICE OF MAHAGEHENI'ND BUDGET/
WASHINGTON DC 20503 FACILITT NAME ('I) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR 'EQUENTIAL REVISION NUMBER NUMBER Browns Ferry Unit 2 05000260 5 of 6 TEXT lf more s ce is r uired use edditionsi co ies of NRC Form 366A (17)
VZ ~ ADDZTZONAL ZNFORMLTZON A. Failed Co onents:
Target Rock Two-Stage SRVs Model No. 7567F.
B. Previous LERs on Similar Events:
Since the early 1980s, TVA has issued several LERs (e.g.,
296/81074, 259/83036, 260/87005, 259/88053, 260/93003) regarding main steam SRV setpoint drift due to disc/seat corrosion bonding. The BWROG and,the valve manufacturer are pursuing corrective actions for the disc/seat corrosion bonding problem.
TVA expects the corrective .action of using platinum alloy for disc/seat interface should help toward reducing corrosion bonding and thus, decreasing setpoint drift problems in the future. I VZZ. Commitments None Energy Industry Identification System (EIIS) system and component codes are identified in the text with brackets (e.g., [XX]).
Ol I
NRC FORM 366A U.S NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104
,(5-92) EXPIRES 5/31195 ESTIMATED BURDEN PER RESPONSE TO COMPLY'WITH THIS"INFORMATION COLLECTION REQUEST: 50.0 HRS. FORIIARD COMMENTS'EGARDING
'URDEN ESTIMATE TO THE INFORMATION AHD RECORDS MANAGEMENT BRANCH (MNBB 7714), U.'S. NUCLEAR REGULATORY COMMISSION, LICENSEE EVENT REPORT IIASHINGTON, DC 20555-0001, AND TO THE PAPERNORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF MAHAGEHENT AND BUDGET, NASHINGTON DC 20503 FACILITY NAME (1) DOCKET NUMBER (2) LER NUHBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION NUMBER NUMBER Browns Ferry Unit 2 05000260 6 of 6 TEXT If more s sce is re uired use edditionei co ies of HRC Form 366A (17)
SRV AS-FOUND DATA RESULTS Eleven of the following thirteen Unit' main steam SRVs failed to meet the required TS tolerance. Six served as Automatic Depzessurization System (ADS) valves.
Valve Pilot Disc Nameplate As-Found Percent Cartridge Setpoint Actuation Difference Serial Number Pressure Pressure (>)
(S/N) (psi) (psi) 1019 1125 1147 + 1.95 1023. ADS 1105 1148 + 3.89 1024 1'125 1161 + 3.'20 1029 1125 1134 + 0.80 1030 1115 1202 + 7..80 1031 ADS 1105 1167 + 5.61' 1059 ADS 1105 1225 9.80 1061 ADS 1115 1115 + 0.00 1063 1105 1225 + 9.80 1065 ADS 1115 1159 + 3 '5 1073 1125 1158 + 2.93 1085 1125 1163 + 3.38
0 I