ML20009C686

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LER 81-019/03L-0:on 810608,section of Piping W/Hand Valve Found to Have Never Been Leak Tested.Review of Plant Documents Failed to Determine Time of Installation or Purpose.Request Issued to Remove Valve & Seal Weld Piping
ML20009C686
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 07/07/1981
From: Palmer R
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20009C675 List:
References
LER-81-019-03L-01, LER-81-19-3L-1, NUDOCS 8107210359
Download: ML20009C686 (1)


Text

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.- .- LICENSEE EVENT REPORT COf tyROL F LOCK
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6 (PLEASE PRINT OR TYPE ALL REQUICED INFORMATION)

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h iOlat lDURING SURVEILLANCE TESTING IN MODE 5, A SECTION OF PIPING WITH A HAND VALVE WAS NOTED I i o ,3 i ; AT PENETRATION CPN-30, WHICH HAD NEVER BEEN LEAK-TESTED AS PER 10 CRF 50 APPENDIX J. l ioici lTHIS IS CONTRARY TO TECHNICAL SPECIFICATION 4.6.1.2.d. l

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44 47 CAUSE DEScalPTION AND CORRECTIVE ACTIONS Iil0llA REVIEW 0F THE PLANT DOCUMENTS FAILED TO DETERMINE WHEN THE PIPING AND VALVE WERE I l ,, ,, , ; INSTALLED, OR FOR WHAT PURPOSE THEY WERE TO BE USED. TYPE C LEAK TEST WAS PERFORMED ON i

(,,,,,;THEVALVEWITHARESULTOF0 LEAKAGE. A REQUEST FOR CHANGE (RFC-01-1855) WAS ISSUED T0 i g l REMOVE THE VALVE AND SEAL WELD THE REMAINING PIPING. THIS WILL RESTORE THE PENETRATION l i, ,4, i T0 THE CONFIGURATION AS SHOWN ON PLANT DRAWINGS. l STA  % POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION l i i s l [H_j@ l 0 l 0 ! 0 l@l NA l [,Bj@l SURVEILLANCE TEST l l ACTIVITY CO TENT l RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE -

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