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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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REGULA"I.Y INFORMATION DISTR I BUT I 0 YSTEM (R IDS)ACCESSION NBR: 8720070026 DOC.DATE: 87/10/02 NOTARIZED:
NO DOCKET FACIL: STN-50-530 Palo Verde Nuclear Station>Unit 3p Arizona Pub li 05000530 AUTH.NAME AUTHOR AFFILIATION BRADISHp T.R.Arizona Nuclear Poeer Prospect (Formerly Arizona Public Serv HAYNESp J.G.Ari zona Nuclear Power,pro Ject (Formerly*ri zan'a Public Serv REC IP.NAME RECIPIENT*FFILIATION
SUBJECT:
LER 87-003-00:
on 870929i condition identiFied that iF not corrected~could have resulted in impToper operation oF two shutdown cooli'ng isolation valves in redundant trains.Caused tg vendor.error.Bolting replaced.W/871002 lir.DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR i ENCL SIZE: TITLE: 50.73 Licensee Event RepoT t (LER)I Incident Rpti etc.NOTES: Standardized plant.05000530 RECIPIENT ID CODE/N*ME PD5 LA LICITR*.E INTERNAL: ACRS MI CHELSON AEOD/DOA AEOD/DSP/ROAB DEDRO NRR/DEBT/CEB NRR/DEST/I CSB NRR/DEBT/MTB NRR/DEST/RSB NRR/DLPG/HFB NRR/DOEA/EAB NRR/DREP/RPB NRR/PMAS/ILRB RES DEPY QI RES/DE/EIB EXTERNAL: EG4G GROHp M LPDR NSIC HARRISI J NOTES: COPIES LTTR ENCL 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 2 2 1 5 5 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PDS PD DAV I Si M ACRS MOELLER AEOD/DSP/NAS AEOD/DSP/TPAB NRR/DEST/ADS NRR/DEST/ELB NRR/DEST/MEB NRR/DEST/PSB NRR/DEST/SQB NRR/DLPG/GAB NRR/DREP/RAB NR IB F IL 02 FORDp J RGN5 FILE 01 H ST LOBBY WARD NRC PDR NSIC MAYSi G COPIES LTTR ENCL 1 1 1 2 2 1 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45 4l~i NRC Form 355 (9.5 3 I LICENSEE EVENT REPORT (LER)US.NUCLEAR REOULATORY COMMISSION APPAOVED OMB NO.31504)BC EXP)ASS: 5/31/SS FACILITY NAME (II Palo Verde Unit 3 DOCKET NUMBER (2)0 5 0 0 0 PA 1 oF0 6 Valve Bolting Nonconformances Could Potentially Result In the Inability of Two Shutdown Coolin S stem Valves to Perform The'ir Functions MONTH OAY YE'AR EVENT DATE (4)YEAR LER NUMBER (5)SEQUENTIAL a" REYtCSQN NUMBER:?ya NUMCEll REPOAT DATE (7)MONTH DAY YEAR OTHER FACILITIES INVOLVED ISI FACILITY NAMES Palo Verde Unit 1 DOCKET NUMBER(S)05000528 0 9 OPERATINO MODE (Sl 8 7 POWER LEVEL p p p wNk<<0 5 0 0 0 5 0 3 0 0 THIS REPORT IS SUBMITTED PURSUANT T 20.C02(5 I 20A05(~l(1)B)20.405(c)(1)(ll) 20.405(~I (ll(rill 20.C05(el(1
)(lvl 20.C05(c)II)(v) 1 0 0 2, 8 7 Palo Verde Unit 2 O THE REQUIREMENTS OF 10 CFR (I;(Check one or more of the follow/nfl (11)20.405(c)50.35(cl(1) 50.35(cl (2)50.73(e I (2)(II 50.73(c)(2)(li)50.73(c l(2)I ill l 50.73(c)(2 I(lv)50.73(el(2)(vl 50.73(e)l2)(v BI 50.73(cl(2)(vBll(A) 50.73(c)(2)(vlEI(B)50.73(~)(2)(c)73.71(ls)73.71(cl OTHER ISpeclfy in Aotrrect Below emf In FerL Assr)C Form$FSAI Part 21 NAME LICENSEE CON'TACT FOR THIS LER (12)Thomas R.Bradish, Compliance Supervisor TELEPHONE NUMBER AREA CODE 602 393-3531 COMPLETE ONE LINE FOA EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANVFAC.TURER EPORTABLE~&@5k SYSTEM COMPONENT MANUFAC.TVRER EPORTAB(.E TO NPRDS SUPPLEMENTAL REPORT EXPECTED (ICI YEs llf yee, complne fxpEctED stisrstISsioff DATE)NO ABSTRACT (LImit to te00 tpecet, I~., epprorimerely fsfteen tlnpre.tpece typewritten linn!II~I P sAco(r?g@k
'gg(?~jg%$~ikP?'?'A>N..:.NC<%?MONTH DAY YEAR EXPECTED SUBMISSION DATE (15I On September 29, 1987, with Unit 3 in Mode 5 (COLD SHUTDOWN), a condition was identified that if left uncorrected, could have resulted in the improper operation of two Unit 3 shutdown cooling isolation valves in redundant trains.This determination resulted from an Engineering Evaluation Request which had been dispositioned to resolve identified valve yoke to motor operator bolting nonconformances.
The root cause of this event has been determined to be vendor error.Two valves supplied to the Arizona Nuclear Power Prospect (ANPP)did not have the required design changes implemented prior to shipment nor did the vendor provide notification of these changes to ANPP.The cause for the vendor error has not been determined at this time.As corrective action, the"as-installed" bolting has been replaced with alternative bolting material.An inspection was conducted to ensure that the similar shutdown cooling isolation valves in Units 1 and 2 had adequate design margin and were acceptable for continued operation.
The results of the inspection indicate that no modifications are required at this time.In order to prevent recurrence, a Quality Assurance and an Engineering representative will conduct an evaluation at the vendor's facilities to determine the extent of these deficiencies and the potential for transportability to other valves supplied by that vendor.871007002b 87i002 PDR ADOCK 05000DRO NRC form 355 4l Oi C' NRC FPIIII 355A (94131 LICENSEE EVENT REPORT HLER)TEXT CONTINUATION US.NUCLEAR REOULATORY COMMI55/ON APPROVED OMS NO 3150 010l EXPIRES: 0/31/N FACILITY NAME III DOCKEt SIUMRER 131 LER NUMSER IEI YEAR,.'M 55OUENTIAL
'~~Issy/5ION NUM sk...rP NUM FA PACE tll Palo Verde Unit 3 TEXT lll ANyp u>>cp iS ISPwwE vsp aIRIS>>AS/H/IC hym 3054's/Illl o so oo530 87-00-0 02 QF 0 6 On September 29, 1987, with Unit 3 in Mode 5 (COLD SHUTDOWN), a condition was identified that if left uncorrected, could have resulted in the improper operation of two Unit 3 shutdown cooling isolation valves in redundant trains.This determination resulted from an Engineering Evaluation Request which had been dispositioned to resolve identified valve yoke to motor operator bolting nonconformances.
In June, 1987, with Unit 3 in Mode 5, shutdown cooling isolation valve SI-651 was observed during preventative maintenance to have loose bolting between the motor operator and the valve yoke.An evaluation of the loose bolting determined that the cause may be attributed to system vibration.
The bolts were retorqued.
Units 1 and 2 were evaluated at this time, based on observation of the valves during previous maintenance activities, to not exhibit this problem.Subsequent to the Unit 3 bolts being retorqued, the bolts were again found to be loose.Investigation into the cause of the problem revealed that the valve yoke to motor operator bolting for valves SI-651&SI-652 did not match the vendor drawings or the design report for all three units.The specified configuration as shown on the current valve outline drawing for valves SI-651&SI-652 requires eigh't (8)-7/8 inch, ASTM A193 Grade B7 (carbon steel), bolts between the adapter plate and the valve operator and sixteen (16)-7/8'inch, ASTM A193 Grade B8M (stainless steel), bolts between the valve yoke and the adapter plate.For valves SI-651&SI-652, the"as-installed" bolting between the valve yoke and adapter plate, and between the adapter plate and the motor operator for each unit is described below: Unit 1 Yoke to Adapter: Both valves contain sixteen (16)7/8" stainless steel bolts.Adapter to Operator: Both valves contain eight (8)7/8" non-magnetic bolts.Unit 2 Yoke to Adapter: Both valves contain one (1)circle of eight (8)7/8"-stainless steel bolts and one (1)circle of eight (8)-unused 5/8" holes.Adapter to Operator: Both valves contain eight (8)7/8" non-magnetic bolts.NAC~IIIIU SPSA 19 53>
i~>
NAC Foim 455A l9451 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.NUCLEAR REOUL*TOAY COMMISSION APPAOVED OMS NO 3150-0105 EXPIRES: 4/$1/44 FACILITY NAME III DOCKET NUMSER IXI LEA NUMSER (4)~AOE 151 YEAR Ki.'m:iS:, 55OVENTIAL i g?NVM 5R REVISION NVM 5A Palo Verde Unit 3 TEXT/lime+NMCP/I/PFVFRE I/w/A/5/m5/AAC fomi~4/IITI 0 5 0 0 0 5 3 P 8 7 0 0 0.0 3 OF 0 6 Unit 3 Yoke to Adapter: Both valves contain eight (8)5/8" stainless steel studs with nuts and one (1)circle of eight (8)unused 5/8" holes.Adapter to Operator: Both valves contain eight (8)7/8" non-magnetic bolts.The shutdown cooling isolation valves were manufactured by Borg-Warner Corp., (B-W)Nuclear Valve Division, (Valve Assembly-16xl2x16 inch, 1512 Lb., Gate, Cres, With Motor Oper.)and supplied by Combustion Engineering.
Information on the"as-installed" valve to motor operator bolting configurations was provided to B-W and Combustion Engineering (C-E)for their evaluation.
The evaluations demonstrated that the bolts securing the motor operator to the valve (motor operator to adapter plate-bolting and valve yoke to adapter plate bolting)were adequate for Palo Verde Units 1 and 2 (i.e., system design criteria was met).A similar evaluation indicated that the elastic stress limits were exceeded for the Unit 3 valves (SI-651&SI-652)bolting when exposed to normal operating loads.These stresses, if repeatedly=experienced by the valves, could potentially have resulted in fatigue failure of the bolts, rendering the valves inoperable.
For each Palo Verde unit there are four (4)valves (SI-653,-654,-655,&-656)similar in"valve body design to SI-651&SI-652.However, the original sizing of valve SI-651&SI-652 motor operators required a larger motor operator (Limitorque Model SMB-3-100) than was required on valves SI-653,-654,-655,&-656 (Limitorque Model SMB-1-40).
At approximately the same time the valves were being seismically analyzed (prior to valve shipment), B-W determined that the valve yoke to adapter plate bolting on valves SI-651&SI-652 was overstressed.
To correct this deficiency B-W issued an Engineering Change Notice (ECN)to upgrade the yoke to adapter plate bolting to sixteen (16)-7/8 inch, ASTM A193 Grade B8M, bolts on valves SI-651&SI-652.When this ECN was incorporated on Revision F of the B-W valve outline drawing, B-W indicated that the ECN was implemented on the Unit 1 valves previously shipped to the Palo Verde Jobsite.A later revision, Rev.H, of the valve outline drawing changed the material of the eight (8)-7/8 inch adapter plate to motor operator bolts from ASTM A193 Grade B8M to ASTM A193 Grade B7.At the time Rev.H of the valve outline drawing was issued, the Unit 1 and 2 valves had been@hipped.The Rev.H drawing was to be used by B-W for the manufacture of the Unit 3"valves.A comparison of the"as-installed" valve to motor operator bolting configuration and the revisions of the valve outline drawings follows: 4RC FORM 555A I9 45 I 4t r 4 NRC Fotw SSSA IQ BS)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REOULATORY COMMISSION APPROVED OMB NO.3150 01'XPIRES:
BIB)/44 FACILITY NAME I)l DOCKET NUMBER LTI YEAR LE 4 NUMBER IS)SKOVKNTIAL AVM TA TV%ION AVM SEA~AOE IS)Palo Verde Unit 3 TEXT N Auuu NMcu N nyund, uM~lYl)C%%dnn SNAB))IT)0 s o 0 0 5 3087 0 0 3 0.04 oF0 6 Unit 1-Valves SI-651&SI-652 currently reflect the valve to motor operator bolting configuration on Revision F of the valve outline drawing.Since C-E has no records of authorizing field bolting changes for these valves and Bechtel has no records of receiving or implementing the bolting changes, it is concluded that B-W shipped the valves incorporating the bolting changes described on the ECN which was later incorporated in Revision F of the valve outline drawing.Unit 2-At the time of shipment, the unit 2 valve to motor operator bolting configuration should have conformed with the valve outline drawing Revision F.The"as-installed" bolting configuration does not reflect any revision of the valve outline drawing.Since C-E has no records authorizing field bolting changes for these valves and Bechtel, has no records of receiving or implementing bolting changes, it is concluded that B-W shipped the valves partially incorporating the bolting changes described on the ECN which was later incorporated in Revision F of the valve outline drawing.Unit 3-By the shipping date of 9-12-80, the valves should have been modified to incorporate all of the bolting changes (i.e., Revision H of the valve outline drawing.)The bolting configuration however does not reflect the requirement of any revision of the drawing (i.e., studs and nuts were used between the valve yoke and adaptor plate in lieu of bolts).The root cause of this event has been determined to be vendor error.The SI-651 and SI-652 valves supplied to the Arizona Nuclear Power Project (ANPP)did not have the required design changes implemented prior to shipment nor did the vendor provide notification of these changes to ANPP.The cause for the vendor error has not been determined at this time.The other sixteen inch gate valves supplied by B-W were inspected to determine if a similar condition exists.This investigation revealed that valves SI-653,-654,-655,&-656 had similar valve bodies (16x12x16 gate)however, they were provided with a different (smaller)'motor operator which has a different bolting configuration to the valve yoke.As a prudent measure the revisions to the valve outline drawings for these valves were reviewed for consistency and the"as-installed" configurations were verified as acceptable.
Based on the results of the evaluation, ANPP has determined that Palo'erde Units 1 and 2 can be operated with the"as-installed" valve bolting configuration.
It has been determined that the bolting for the Palo Verde Units 1 and 2 valves is adequate and does not require modification.
~4AC FOAM SuSA IS Sh
1 I NRC form 344A/9431 LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.d.NUCLEAR REOULATORY COMMI551ON APPROVEO OMd NO.3150&195 EXPIRES'/31/dd FACILITY NAME 111 OOCKET NUMEER Ql LER NVMEER (4)x.od 55OUENT/AL v.9 NIZAM 5 II AEVr5ION rrvM 5A~AOE 13)TEXT///moro 5ooco//roduuod.u5o k/5juimo/I
//RC form 3/f1/Ad/I'l)o s o o o 5 3087-0 03-0 05 oFO 6 As described, the Unit 3 shutdown cooling isolation valves had inadequate bolting as analyzed.Therefore the potential for improper operation existed for both valves and this condition is being reported in accordance with 10CFR 50.73 (a)(2)(v)This condition could have affected the ability to cool the Unit down to Mode 5 without operator actions from outside the control room.Since the nonconforming bolting was identified and corrected prior to Unit 3 reaching initial criticality, the consequences described above were never encountered.
Therefore, this event did not adversely affect the safe operation of the plant or the health and safety of the public.This condition is evaluated as reportable under the requirements of 10CFR21 since it constitutes a known defect of a basic component and a substantial safety hazard.This LER satisfies the reporting requirements of 10CFR 21 with the exception of paragraph 21.21 (b)(3), subpart vi with regards to the names and locations of other facilities which may be affected.The evaluation of the"as-installed" valve to motor operator bolting has determined that eight (8)-7/8 inch ASTM-A193 Grade B-7 bolts are adequate for the bolting between the valve yoke and the adapter plate as well as between the motor operator and the adapter plate for valves SI-651&SI-652.To assure consistency however, B-W has shipped the following bolting to Palo Verde: uantit/Valve Descri tion 7/8 inch-9 x 3" LG.Hex Bolt, ASTM-A-193 GR.B-7 (replacement for Find No.56 of B-W drawing 77850/77850-1).
7/8 inch-9 x 2 I3" LG.Hex Bolt, ASTM-A-193 GR.B-7 (replacement for Find No.55 of B-W Drawing 77850/77850-1).
This bolting will be used to replace the"as-installed" bolting as described below: Unit Schedule Sco e of Boltin ,Re lacement First Refueling Outage 1.Replace existing adapter plate to motor operator bolts with new bolts provided.2.Replace existing valve yoke to adapter plate bolts with new bolts provided utilizing the outer bolt circle.4RC~OIIM 355k 19 43r
~4 Ot NRC Form 344A 194)3)LICENSEE EVENT REPORT{LER)TEXT CONTINUATION U.S.NUCLEAR REOULATORY COMMISSION APPROV EO OMS NO.3)SOW)CO EXPIRES: 4/31/NI FACILITY NAME 11)OOCKET NUMSER LT)LER NUMSER IS)saaI/ar/T/AL NVM ao avrsroN rrUM ao PACE IS)Palo Verde Unit 3 TEXT///moro Nrooo/I ooror'ra ooo a//roar//H/IC Forrrr 3/NAS)()7)050004)3087 0 0 0 0 6 QF 0 First Refueling Outage 1.Replace existing adapter plate to operator bolts with new bolts provided.2.Replace existing valve yoke to adapter plate bolts eight (8)with new bolts provided.Completed 1.Remove existing valve yoke to adapter plate and adapter plate to motor operator bolts.2.Drill out valve yoke to accept the new 7/8 inch bolts utilizing the outer bolt circle dimensions.
3.Replace the adapter plate to motor operator bolts with the new bolts provided.4.Replace the valve yoke to adapter plate*bolts with the new bolts provided (utilizing the new holes drilled in the valve yoke and the existing adapter plate 7/8 inch threaded holes, previously unused.The modifications described above will provide consistency between the three units.In addition B-W will update the required documentation (outline drawings and seismic qualification report)to reflect the modifications implemented.
Additionally, in order to prevent recurrence, a Quality Assurance and an Engineering representative will conduct an evaluation at the vendor's facilities to determine the extent of these deficiencies and the potential for transportability to other valves suplied by that vendor.There were no structures, components, or systems that were inoperable at the start of the event, other than those previously described, that contributed to the event.There were no unusual characteristics of the work location which contributed to the event.There were no automatic or manually initiated safety system responses.
No operator actions were required as a result of the event.Should other concerns or information pertinent to this event be discovered, a supplement to this report will be issued.There have been no previous similar Licensee Event Reports submitted.
Moc r orrM oooo SS S)r
~~(~i Arizona Nuclear Power Project P.O.BOX 52034~PHOENIX.ARIZONA 85072-2034 192-00288-JGH/TRB/TJB October 2, 1987 Document Control Desk U.S.Nuclear Regulatory Commission Washington, D.C.20555
Reference:
(A)Telephone conversation between W.J.Wagner and T.R.Bradish on September 29, 1987.
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)Unit 3 Docket No.50-530 Licensee Event Report 3-87-003-00 File: 87-020-404, 87-006-216, 87-001-211 Attached please find Licensee Event Report (LER)No.3-87-003-00 prepared and submitted pursuant to 10CFR 50.73.In accordance with 10CFR 50.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V Office.Additionally, in accordance with Reference (A), the NRC was notified that this condition is reportable under 10CFR 21.This LER is our written report regarding this condition and satisfies the reporting requirements of 10CFR 21 with the exception of paragraph 21.21 (b)(3), subpart vi with regard to the names and locations of other facilities which may be affected.A copy of this report will be sent to Borg-Warner for their evaluation.
If you have any questions, please contact T.R.Bradish, Compliance Supervisor at (602)393-3531.Very trul yours, j/g~~~~</>g J.G.Haynes Vice President Nuclear Production JGH/TJB/cld Attachment cc: 0.M.DeMichele (all w/a)E.E.Van Brunt, Jr.J.B.Martin J.R.Ball R.C.Sorenson E.A.Licitra A.C.Gehr INPO Records CenterlgAS i e~~