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 Issue dateTitleTopic
ML20086D7959 March 1973Updated AO 73-07:on 730302,steam Leak Noted Around Bonnet of Steam Exhaust Line Check Valve.Hpci Exhaust Stop Check Valve Gagged Shut,Check Valve Bonnet Gasket Replaced & Bonnet Retightened
ML20086D8035 March 1973AO 73-07:on 730302,steam Leak Noted Around Bonnet of Steam Exhaust Line Check Valve.Hpci Exhaust Line Stop Check Valve Gagged Shut,Check Bonnet Gasket Replaced & Bonnet Retightened
ML20086D8068 March 1973Updated AO 73-06:on 730302,chemist,while Attempting to Draw Offgas Sample,Discovered Improper Flow Through Offgas Sample/Monitoring Sys.Caused by Two Lines to Offgas Monitoring Sys Rolled During Mods
ML20086D8142 March 1973AO 73-06:on 730302,chemist,while Attempting to Draw Offgas Sample,Discovered Improper Flow Through Offgas Sample/ Monitoring Sys.Caused by Two Lines to Sys Rolled During Mods Made During Plant Outage
ML20086D83926 February 1973AO 73-05:on 730117,noble Gas Release Rate Exceeded Tech Spec Limit.Scram Resulted from Vessel Low Level Imposed by Feed Flow Transient Induced When Technician Returned Level Instrument Back to Svc After Surveillance Testing
ML20086D84726 February 1973AO 73-04:on 730116,feedback Signal to Recirculation Pump a Decreased,Causing Momentary Increase in Pump Speed.Caused by High Resistance,Normally Open,Relay Contact in Circuit Board.Relay Located,Tested & ReplacedFuel cladding
ML20086D88316 January 1973AO 73-03:on 730115,loop a Injection Valve Failed to Open, Rendering LPCI a Subsystem Inoperable.Caused by Valve Motor Being Unusually Warm & Motor Breaker Trip.Surveillance Conducted
ML20086D88622 January 1973Updated AO 73-02:on 730115,fan 1 on West Cooling Tower Failed in Forward Direction After Completion of Deicing Cycle.Caused by Bearing Failure in Reduction Gear Unit.Fan Disassembled & Angle Speed Reducer Drive Replaced
ML20086D89215 January 1973AO 73-02:on 730115,fan 1 on West Cooling Tower Failed in Forward Direction After Completion of Deicing Cycle.Caused by Bearing Failure in Reduction Gear Unit.Repair & Return to Normal Operation of Fan Expected by 730122
ML20086D89515 January 1973AO 73-01:on 730109,during Reactor Startup from Cold Shutdown,No Indication Observed on Intermediate Range Monitor (IRM) Channels B,D & F While Increasing Power from Source Range Monitor Range to Irm.Caused by Blown Fuse
ML20086D8973 January 1973AO 72-20:on 721222,HPCI Inverter Tripped,Rendering HPCI Sys Inoperable.Trip Spurious & Not Related to Operational Conditions.Inverter Reset & Verified Operable
ML20086D8998 November 1973AO 73-31:on 731107,reactor Scram Occurred Based Upon High Flux Signal from Intermediate Range Neutron Monitoring Sys. Investigation Revealed Rod 30-23 Fully Withdrawn W/Rod 26-23 Withdrawn for Friction Test
ML20086D90510 October 1973Updated AO 73-29:on 731002,drywell High Pressure Switch Failed to Actuate at Required Setpoint.Caused by Instrument Drift.Switch Reset,Functionally Tested & Declared Operable
ML20086D9103 October 1973AO 73-29:on 731002,drywell High Pressure Switch Failed to Actuate at Required Setpoint.Switch Reset,Functionally Tested & Declared Operable
ML20086D92312 October 1973AO 73-30:on 731005,fuel Channel Insp Begun,Due to Discovery of Condition at Another Bwr.Initial Results Indicate of Seven Channels Inspected,Five Exhibit Signs of through-wall- Wear.Program for Ultimate Resolution Developed
ML20086D9265 October 1973AO 73-30:on 731005,fuel Channel Insp Begun,Due to Discovery of Condition at Another Bwr.Initial Results Indicate of Seven Channels Inspected,Five Exhibit Signs of through-wall- Wear.Further Insp in Progress
ML20086D93218 September 1973Updated AO 73-28:on 730910,microswitch Installed in Differential Pressure Indicating Switch 2-129B Failed to Actuate at Required Setpoint.Complete Assembly Replaced When Insp Revealed Excessive Binding in Switch Actuating Arm
ML20086D93511 September 1973AO 73-28:on 730910,microswitch Installed in Differential Pressure Indicating Switch 2-129B Failed to Actuate at Required Setpoint.Sensor Rendered Operable by Replacing Microswitch Assembly
ML20086D93917 September 1973Updated AO 73-27:on 730909,apparent Detonation in Offgas Sys Caused Sufficient Back Pressure to Fracture Air Ejector Rupture Disc,Thereby Degrading Boundary Designed to Contain Radioactive Matl
ML20086D94510 September 1973AO 73-27:on 730909,apparent Detonation in Offgas Sys Caused Sufficient Back Pressure to Fracture Air Ejector Rupture Disc,Thereby Degrading Boundary Designed to Contain Radioactive Matl
ML20086D95011 September 1973Updated AO 73-26:on 730903,apparent Detonation in Offgas Sys Caused Sufficient Back Pressure to Fracture Air Ejector Rupture Disc,Thereby Degrading Boundary Designed to Contain Radioactive MatlsLoop seal
ML20086D9584 September 1973AO 73-26:on 730903,apparent Detonation in Offgas Sys Caused Sufficient Back Pressure to Fracture Air Ejector Rupture Disc,Thereby Degrading Boundary Designed to Contain Radioactive Matls
ML20086D9677 September 1973AO 73-25:on 730831,during Severe Electrical Storm in Which Direct Lightning Strike to Top of Plant Ventilation Stack Observed,Both Plant Gas Monitoring Sys & Area Gamma Radiation Monitors on Fence Became InoperableLoop seal
ML20086D97231 August 1973AO 73-25:on 730831,during Electrical Storm in Which Direct Lightning Strike to Top of Plant Ventilation Stack Observed, Both Plant Stack Gas Monitoring Sys & Area Gamma Radiation Monitors on Perimeter Fence Became Inoperable
ML20086D97922 August 1973Updated AO 73-24:on 730816,instrument Lines Monitoring Suppression Chamber Pressure Found Incorrectly Tubed to Differential Pressure Sensors Which Activate Breaker Operation,Causing Actuation
ML20086D99217 August 1973AO 73-24:on 730816,instrument Lines Monitoring Suppression Chamber Pressure Found Incorrectly Tubed to Differential Pressure Sensor Which Activates Breaker Operation,Causing Actuation W/Positive Pressure
ML20086D9989 August 1973Updated AO 73-23:on 730802,gamma Radiation Monitor on Perimeter Fence Became Inoperable.Caused by Power Supply Associated W/Monitor Failing,Causing Immediate Downscale Indication.Component Replaced & Monitor Returned to Svc
ML20086E0013 August 1973AO 73-23:on 730802,gamma Radiation Monitor on Perimeter Fence Became Inoperable.Caused by Power Supply Associated W/ Monitor Failing,Causing Immediate Downscale Indication. Efforts to Determine Cause of Failure Currently in Progress
ML20086E0097 August 1973Updated AO 73-22:on 730730,source Calibr of Radiation Monitors Associated W/Reactor Bldg Vent Exhaust Duct & Refueling Floor Zone Discovered Not Performed Since 720408. Monitors Calibr Upon Discovery of Omission
ML20086E01531 July 1973AO 73-22:on 730730,source Calibr of Radiation Monitors Associated W/Reactor Bldg Vent Exhaust Duct & Refueling Floor Zone Found Not Performed Since 720408.Monitors Calibr Upon Discovery of Omission
ML20086E0459 June 1975AO 75-12:on 750609,standby Liquid Control Pump B Delivered High Flow Rate.Cause Under Investigation
ML20086E07212 May 1975AO 75-11:on 750511,intermediate Range Monitor Channel E Failed to Respond to Increasing Neutron Flux Level.Cause Not Stated.Reactor Protection Sys Trip Sys a Manually Tripped
ML20086E08119 July 1973Updated AO 73-21:on 730711,microswitch Installed in DPIS-2-129B Failed to Actuate at Required Setpoint.Vendor Contacted to Reiterate Need for Improving Design of Actuating Arm Bearing.Actuating Arm Realigned
ML20086E10112 July 1973AO 73-21:on 730711,microswitch Installed in DPIS-2-129B Failed to Actuate at Required Setpoint.Channel Made Operable by Realigning Actuating Arm & Rechecking Trip Point Actuation
ML20086E11610 July 1973Updated AO 73-20:on 730706,drywell Purging & Vent Exhaust Valve V16-19-7A Would Not Close.Mechanical Binding Will Be Investigated & Valve Overhauled During Future Shutdown.Valve Presently Deactivated in Closed Position
ML20086E1246 July 1973AO 73-20:on 730706,drywell Purging & Vent Exhaust Valve V16-19-7A Would Not Close.Inoperability Exceeded Limiting Conditions for Operation.Reactor Shut Down & Cooling Down at Time of Incident
ML20086E14530 April 1975AO 75-10:on 750429,low Water Level Switch Associated W/ Differential Pressure Indicating Sensor 2-3-58B Actuated Low.Switch Adjusted
ML20086E1558 April 1975AO 75-08:on 750408,air Ejector Suction Valve Isolation Time Delay Relay Timer 17-157A Actuated Slow.Cause Not Stated. Timer Reset
ML20086E22221 February 1975AO 75-05:on 750220,sample Accumulator Isolation Valve to Condenser OG-9069 Found Shut,Rendering Radiation Monitors Inoperable.Cause Not Stated.Valve Immediately Opened
ML20086E2445 February 1975AO 75-04:on 750204,gradual Flow Reduction Discovered in Air Ejector Offgas Monitoring Sys.Caused by Removal of 3-way Solenoid Valve for Cleaning & Repair.Valve Replaced
ML20086E3465 February 1975AO 75-03:on 750204,spray Sys Pump Discharge Pressure Sensor PS-14-44A Actuated at 82 Psig,Below Tech Spec Min. Sensor Replaced & Calibr
ML20086E3859 January 1975AO 75-02:on 750108,personnel Discovered That Carbon Filter Beds Changed on Standby Gas Treatment Sys Train a Instead of Planned Train B.Carbon Beds in Train B Replaced
ML20086E3889 January 1975AO 75-01:on 750108,LPCI Low Reactor Pressure Permissive Switches on Instrument 2-3-52D Actuated High.Caused by Improper Calibr Technique.Switch Reset
ML20086E40016 December 1974AO 74-16:on 741214,containment Air Sampling Sys Found Inoperable.Caused by Nonfunctioning Heat Tracing Circuit.Sys Repaired
ML20086E40720 December 1974AO 74-17:on 741219,suppression Chamber Outboard Sample Valve Stuck in Open Position.Caused by Accumulation of Dirt Causing Binding of Solenoid Piston.Valve Cleaned
ML20086E4083 December 1974AO 74-15:on 741202,scram Discharge Vol High Level Scram Switch 3-231A Would Not Actuate Respective Scram Relay. Caused by Fissure in Switch Casement.Switch ReplacedScram Discharge Volume
ML20086E41116 October 1974AO 74-14:on 741015,primary Containment Leak Discovered. Caused by Missing 1/2-inch Test Connection Plug on Drywell Penetration X-16A.Plug Installed
ML20086E41815 July 1974AO 74-11:on 740705,08 & 09,both Plant Stack Monitoring Sys Failed.Caused by Direct Lightning Strikes to Ventilation Stacks During Electrical Storms.Radiation Exposure to Personnel NegligibleGrab sample
ML20086E4288 July 1974AO 74-11:on 740705,both Plant Stack Monitoring Sys Failed Following Direct Lightning Strike During Severe Electrical Storm.Generator Turbine Tripped Causing Reactor Scram.Repair of Damaged Equipment Complete
ML20086E4323 July 1974AO 74-10:on 740626,HPCI Inverter Tripped,Rendering HPCI Sys Inoperable.Caused by Poor Connection Between Printed Circuit Board & Companion Jack.Connections Cleaned