ML20086D795

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Updated AO 73-07:on 730302,steam Leak Noted Around Bonnet of Steam Exhaust Line Check Valve.Hpci Exhaust Stop Check Valve Gagged Shut,Check Valve Bonnet Gasket Replaced & Bonnet Retightened
ML20086D795
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 03/09/1973
From: Riley B
VERMONT YANKEE NUCLEAR POWER CORP.
To:
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20086D797 List:
References
AO-73-07, AO-73-7, VYV-2504, NUDOCS 8312050123
Download: ML20086D795 (2)


Text

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Director (o

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Directorate of Licensing LLJ L

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Uashington, D.C.

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Abnormal Occurience No. An-73-07

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Dear Sir:

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An defined by Technical Specifications for the Verrnont Yankee Nuclear

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Pou,r nrar tem prtinn f,. 7. n,1 un nrn vnnnreina enn (n11n..<no Aher,v.

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)I At approxinately 2300 on March 2, 1973 during conduct of an

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operability check of the High Pressure Coolant Injection (HPCI) Systen, a stean Icak was noted around the bonnet of the steam exhaust line j

check valve (llPCI-65). Although the HPCI systen was observed to be

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operable, repair of the check valve was elected as an innediate course of actlon.

Replacenent of the gasket precluded HPCI operability as

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required by Section 3.5.1:.1.a of Technical Specifications.

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was operating at approxinately 60Z power at the time of this incident.

The :lPCI exhaust line stop check valve uns ganged shut and the check valve bonnet ganket pas replaced and the bonnet retightened.

Con c u r re n t. l y, the operability verification required by Section 4.5.E.2 l

of Technical Specifications was initiated.

At 0230 on March 3, 1973 the llPCI operability tnst van repeated satisfactorily, and no leakage was detected fron the bonnet of !!PCI-65.

The Plant Operations Review Committen concluded that although the valve bonnet leaked, the UFCI systen was still operable and would have perf orned i t:. designed function prior to gan);ing shut the exhaust line utop check valve.

Additionally, to determine whether or not this failure was a ttributable to conditiens during system operation, the valve bonnet 8312050123 730309 fd f

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!!:irch 9, 1973 Page 2 l

stu<l tightneun will be checked follouing each IIPCI Tamp operability tent f

during the next three months.

Very truly yours, i

l VI:1:MONT YANKEE NUCLEAR POWER CORPORATION f

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B.U. Riley 1

i Plant Superintendent l

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