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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:RO)
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Lgs,Units 1 & 2. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A8861999-09-13013 September 1999 Safety Evaluation Authorizing First & Second 10 Yr Interval Inservice Insp Plan Requestss for Relief RR-01 ML20212A4481999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Limerick Generating Station,Units 1 & 2.With ML20211E9891999-08-20020 August 1999 LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5 ML20210L7051999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Limerick Generating Station,Units 1 & 2.With ML20209G0211999-06-30030 June 1999 GE-NE-B13-02010-33NP, Evaluation of Limerick Unit 2 Shroud Cracking for at Least One Fuel Cycle of Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 B110078, Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 11998-12-31031 December 1998 Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 1 ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154H5691998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Limerick Generating Station,Units 1 & 2.With ML20151X3511998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Limerick Generating Station Units 1 & 2.With ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20237D1041998-08-17017 August 1998 Books 1 & 2 of LGS Unit 1 Summary Rept for 960301-980521 Periodic ISI Rept 7 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20236X7641998-07-31031 July 1998 Rev 0 to SIR-98-079, Response to NRC RAI Re RPV Structural Integrity at Lgs,Units 1 & 2 ML20237B4711998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Limerick Generating Station,Units 1 & 2 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20151Z4881998-06-30030 June 1998 GE-NE-B1100786-02, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 2 ML20236P9781998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Limerick Generating Station,Units 1 & 2 ML20196K1801998-06-30030 June 1998 Annual 10CFR50.59 & Commitment Rev Rept for 970701-980630 for Lgs,Units 1 & 2. with ML20249B3501998-06-11011 June 1998 Rev 1 to PECO-COLR-L2R4, COLR for LGS Unit 2 Reload 4,Cycle 5 ML20249A5331998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Limerick Units 1 & 2 ML20247M7071998-05-14014 May 1998 Safety Evaluation Supporting Amend 128 to License NPF-39 ML20217Q5101998-05-0404 May 1998 Safety Evaluation Supporting Amend 127 to License NPF-39 ML20247H5071998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Limerick Generating Station ML20216F3601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Limerick Generating Station,Units 1 & 2 ML20217M0791998-03-31031 March 1998 Safety Evaluation Supporting Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216F9471998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Limerick Generating Station,Units 1 & 2 ML20216F3471998-02-28028 February 1998 Revised Monthly Operating Rept for Feb 1998 for Limerick Genrating Station,Unit 1 1999-09-30
[Table view] |
Text
_ . _ _ _ _ _ _ . - _. _
. 10 CFR 50.73 PHILADELPHIA ELECTRIC COMPANY LIMERICK GE NC R ATING ST ATION P. O. DO X A S AN ATOG A PENNSYLV ANI A 19464
(#16) 337 1200 env.3000 february 27, 1991
- .St .' " '." h .'." ' Docket No. 50-352
........................ License No. NPf-39 U.S. Nuclear Regulatory Commission '
Attn: Document Control Desk Washington, DC 20555
$UBJECT: Licensee Event Report Limerick Generating 5tation - Unit 1 ,
This LER reports an Engineered Safety feature actuation resulting f rom a spurious Divisicn 1 High Drywell Pressure (HDP) signal. The spurious HDP signal occurred while an Instrumentation and Controls technician incorrectly restored a pressure differential switch to operation.
Reference:
Docket No. 50 352 Report Number: 1 91-005 Revision Number: 00 Event Date: January 30, 1991 Report Date: February ?7, 1991 facility: Limerick Generating Station P.O. Box A, Senatoga, PA 19464 This LER is being submitted pursuant to the requirements of 10 CfR 50.73(a)(2)(iv).
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Very truly yours,
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}{l,l. 0 %m DMS:rgs cc: T. T. Martin, Administrator, Region 1. USNRC T. J. Kenny, USNRC Senior Resident inspector, LGS 7,[g3Og{,g(( M g2 )
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,E ' incorrect Restoration of a Pressure Differential Switch initiates a Spuricus High Drywell Pressure Signal Causing an Engineered Safety Feature Actuation. ,,_
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On 1/30/91, during performance of a Surveillance Test (51) procedure, an Instrumentation and Controls (ILC) technician incorrectly restored a pressure differential switch (PDS) to operation causing a spurious Division 1 High Drywell Pressure (HDP) signal. The spurious Division i HOP signal initiated an Engineered Safety feature (ESf) actuation, and various partial logic actuations.
The ESF actuation and the partial logic actuations were immediately reset by Operations personnel. The actual consequences of this event were minimal. Had
! this event occurred during an ope. tional condition in which the Reactor l
Pressure Vessel (RPV) pressure was below 455 psig, the potential for an l unexpectedEmergencyCoreCoolingSystem(LCCS)injectionexisted. The primary cause of this event was proce t al non-compliance by an I&C technician. A significant contributino factor to the cause of this event was that the valving sequence for restorin( the PDS is unusual and is reversed from the normal method in which other PDM in the plant are restored. The !&C technicians involved in this event were counseled regarding the requirement for strict procedural compliance. To prevent the recurrence of a similar event, the equalizing valves forfour(4)subjectPOSSwillbeclosedandtheirrespectivevalvehandleswill be removed. The associated ST procedures for these POSs will be revised to reflect this change. Until this corrective action is completed, warning labels have been installed on the PDSs.
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o lo o 12 o' o it Unit Conditions Prior to the Event:
Unit 1 Operational Condition was 1 (Power Operation) at 100% power icvel. There were no structures, systems or components out of service which contributed to this event.
Description of the (vent:
On January 30, 1991, contractor employed Instrumentation and Controls (If,C) technicians were performing Surveillance Test (ST) Procedure S1-2-059-602-1,
" Channel A Calibration / functional Test of the Primary Containment Instrument Gas isolation on Low Differential Pressure." At 2202 hours0.0255 days <br />0.612 hours <br />0.00364 weeks <br />8.37861e-4 months <br />, a technician opened the L0 side isolation valve to restore to operation pressure differential switch P05-59-106A(Ells:PDS)(seefigure1)whichresultedinaspuriousDivision1 High Drywell Pressure (HDP) signal. The spurious HOP signal occurred when greater than 1.68 psig was momentarily sensed by drywell pressure transmitters PT-42-lNOSOA, PT-42-1N094A, and PT-42-1N094E.
The spurious Division 1 HDP signal initiated the following Engineered Safety Feature (ESF) actuation (Ells:JE),asdesigned.
- o. A partial Group VIC (Primary Containment Sampling /Recombiner) Primary ContainmentandReactorVesselisolationControlSystem(PCRVICS) actuation (Ells:JM) was generated by PT-42-lN050A. This resulted in the automatic closure of SV-57-133, SV-57-183 and SV-57-191, three (3) Primary Containment H2/02CombustibleGasAnalyzer(CGA)(Ells:BB)samplelineisolationvalves.
Thiscausedone(1)ofthetwo(2)operatingH2/02CGAstoisolateand recirculate its air flow.
Additionally, the spurious HDP signal caused the following partial logic actuations to occur, as designed.
o AChannel'Al'ReactorProtectionSystem(RPS)(Ells:JC)halfscram actuation was generated by PT-42-lN050A.
o EmergencyCoreCoolingSystem(ECCS)partiallogicactuationsweregenerated by PT-42-lN394A and PT-42-IN094E. No Residual Heat Removal (RHR) System (Ells:BO), Core Spray (CS) System (Ells:BM), Emergency Diesel Generator (EDGi (Ells:EK), or Automatic Depressurization System (ADS) actuations occurred due to the absence of a concurrent low Reactor Pressure vessel (RPV)pressuresignal(RPVpressurebelow455psig). l The ESF actuation, and the partial logic actuations were reset at approximately i 2205 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.390025e-4 months <br /> by Operations personnel. A four (4) hour notification was made to the NRC at 0106 hours0.00123 days <br />0.0294 hours <br />1.752645e-4 weeks <br />4.0333e-5 months <br /> on January 31, 1991, in accordance with the requirements of 10CFR50.72(b)(2)(ii) since the event resulted in the automatic actuation of an ESF, This report is being submitted in accordance with the requirements of 10CFR50.73(a)(2)(iv).
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The actual consequences of this event were minimal. All system actuations which occurred as a result of this event initiated as designed, and were immediately reset by Operations personnel. The redundant Primary Containment H2/02 CGA was in operation during this event, and was monitoring the Primary Containment atmosphere for H2/02 concentrations. No abnormal H2/02 concentrations were .
identified prior to, during, or following this event. There was no release of radioactive material to the environment as a result of this event.
Had this event occurred during an operational condition in which the RPV pressure was below 455 psig, the potential for overfilling the RPV existed due to an unexpected ECCS injection. In response to this type of transient.
Operations personnel would have initic*ed Operational Transient (OT) Procedure, OT-110, Reactor High Level," which provides direction for mitigating an unexpected / unexplained rise in Reactor water level. Licensed operators receive requalification training to review and practice responses to simulated plant transients of this type. The procedure, training, and operator actions would have mitigated the consequ2nces of this type of event.
Cause of the Event:
The primary cause of this event was personnel error in that the I&C technicians performing the ST procedure failed to comply with the restoration section in the ST procedure. The sections for testing and calibration of PDS-59-106A-in ST procedure ST-2-059-602-1 were satisfactorily completed and complied with by the I&C technicians; however, the section for the restoration of PDS-59-106A was not complied with by the l&C technicians.
-Additionally, the following contributing factors which lead to the cause of this event, are as follows, o The valving sequence for restoring PDS-59-105A, PDS-59-1068 PDS-59-206A, and PDS-59-2068 is unusual and is reversed from the normal method in which all other PDSs and transmitters in the plant are restored. Therefore, the
' mind set' that the 1&C technicians had for normal restoration of PDSs and transmitters in the plant affected how the 1&C technician manipulated the valves for PDS-59-106A.
o There were no warning iabels on the four (4) PDSs discussed above. As a result of a previous similar event reported in LER 1-90-025, warning labels were to be added to the four (4) PD$s. These labels were to be used to alert I&C technicians of the PDSs unusual valving sequence. However, the labels were not installed at the time this event occurred.
o The I&C technicians did not follow normal work practices and training.
Normal work practice training instructs techniciat.s to work as a team until an ST procedure is fully completed, and to use ' repeat backs' after actions e
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, in procedural steps of an ST are completed. During the restoration of PDS-
) 59-106A,one(1)l&Ctechnicianwascleaninguptheworkareawhilethe other !&C technician was restoring the PDS. Therefore, the I&C technicians did not work together as a team during the restoration of the PDS, and no
. ' repeat backs' were utilized.
In this event, after the PDS-59-106A was tested and calibrated, the H1 and LO sideisolationvalvesforPDS-59-106A(seefigure1)wereclosed,andthe equalizing valve was open. The H1 side to PDS-59-106A is connected to the PrimaryContainmentInstrumentGas(PC10)systemwhichwasinserviceoperating at'100 psig pressure. Just prior to the restoration section in the 51 ,
procedure, a CAUTION statement exists which alerts l&C technicians to follow the valving sequence for restoration of PDS-59-106A. In the restoration section of the ST procedure, the procedural steps direct the l&C technicians to restore PDS-59-106A by opening the L0 side isolation valve first, closing the equalizing valve second, and finally opening the H1 side isolation valve last. While one (1)I&Ctechnicianwascleaninguptheworkarea,theotherl&Ctechnician, i
! having the ' mind set' to restore the PDS to operation using the normal valving i sequence for restoring PDSs and transmitters in the plant, proceeded to restore PDS-59-106A without the use of the ST procedure. The technician opened the HI side isolation valve to PDS-59-106A first, pressurizing thr,t instrument line up to the L0 side isolation valve to 100 psi. The equalizintj volve was then closed. Finally, the L0 side isolation valve was opened which released the pressurized air trapped between the equalizing valve an's the to side isolation valve down the instrument line such that PT-42-lN050A, PT-42-lN094A, and PT ,
IN094E momentarily sensed the high pressure and initiated the EST actuation.
Corrective Actions:
- 1. :The !&C technicians involved in this event were counseled regarding proper work practices'and the requirement for strict procedural compliance.
- 2. Warning labels to alert Ir.C technicians of the PD$s unusual valving sequence have been installed on the four (4) POSs.
3.- This event will be discussed at the'next series of 1&C foreman Team Meetings
-with emphasis placed on the need for procedural compliance. The I&C ,
technicians involved in this event will present " Lessons Learned" from this event at each meeting. These meetings are expected to be completed by March 23, 1991.
-4. ~P05 59-106A, PDS-59-1068.-PDS-59-206A, and PDS-S9-206B are the only PDSs in the plant which have a restoration valving sequence that is reversed from the normal method-in which all other PDSs and transmitters in the plant are restored. To prevent the recurrence of a similar-event, and to preclude the
_ potential for an unexpected ECCS injection when the RPV pressure is below 455psig,theequalizingvalvesforthesefour(4)PDSswillbeclosedand their respective valve handles will be removed. All of the Unit I and 2 g...nu
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- procedures which isolate and restort these PD$s will be revised to remove the actions which require the manipulation of-the equalizing valves. This
- specit.) valve manipulation is similar to other PDSs and transmitters existing in the plant that have had their equalizing valve handles removed.
ILC technicians are made aware of these special cases throu".h training, and through the proper valve sequencing that is included in the applicable procedures. This corrective action is expected to be completed and . .
implemented by April 1, 1991.
After this corrective action has been completed, the warning labels which were installed on the PDS$ will no longer be necessary and will be removed.
, Previous Similar Occurrences:
i .
4
. LER 1-90-025 reported ESF actuations resulting from a spurious Loss of Coolant Accident (LOCA)signalinitiatedbytheimpropervalvingrestorationofPDS~9-106A. As a result of LER 1-90-025, the ST procedures for ensuring that the sensing ilnes are clean for PDS-59-106A PDS-59 1068, PDS-59-206A, and PDS-69
! 206B were revised. These ST procedures are only performed during refueling operations. These revisions incorporated caution statements to alert I&C technicians to follow the restoration valving sequence, and incorporated the.
correct valving sequence for restoration of the PDSs. The ST procedures for ensuring that.the sensing lines are clean do not test or calibrate the PDS$.
Additionally, warning labels were to be added to the four-(4) PDSs; however, the labeling was not completed at the time this event being reported occurred.
-All of the ST procedures which test or calibrate the PDSs (including ST-2-059-602-1 being reported in this event) contained the caution statements and the correctvalvingrestorationsequenceforthefour(4)PDSspriortothe-event reported in LER 1-90-025. The warning labels were-not considered to be essential.in preventing a similar event since the monthly ST procedures for calibration and testing of these PDSs have been successfully and properly performed many times in the pa!.t by I&C technicians. However, had the warning labels discussed above been installed prior to the occurrence of this event
- being reported, the spurious HDP signal caused by procedural non-compliance may have been prevented.
Tracking Codes: A2 failure to follow implementing procedures ,
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