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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:RO)
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Lgs,Units 1 & 2. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A8861999-09-13013 September 1999 Safety Evaluation Authorizing First & Second 10 Yr Interval Inservice Insp Plan Requestss for Relief RR-01 ML20212A4481999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Limerick Generating Station,Units 1 & 2.With ML20211E9891999-08-20020 August 1999 LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5 ML20210L7051999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Limerick Generating Station,Units 1 & 2.With ML20209G0211999-06-30030 June 1999 GE-NE-B13-02010-33NP, Evaluation of Limerick Unit 2 Shroud Cracking for at Least One Fuel Cycle of Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 B110078, Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 11998-12-31031 December 1998 Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 1 ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154H5691998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Limerick Generating Station,Units 1 & 2.With ML20151X3511998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Limerick Generating Station Units 1 & 2.With ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20237D1041998-08-17017 August 1998 Books 1 & 2 of LGS Unit 1 Summary Rept for 960301-980521 Periodic ISI Rept 7 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20236X7641998-07-31031 July 1998 Rev 0 to SIR-98-079, Response to NRC RAI Re RPV Structural Integrity at Lgs,Units 1 & 2 ML20237B4711998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Limerick Generating Station,Units 1 & 2 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20151Z4881998-06-30030 June 1998 GE-NE-B1100786-02, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 2 ML20236P9781998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Limerick Generating Station,Units 1 & 2 ML20196K1801998-06-30030 June 1998 Annual 10CFR50.59 & Commitment Rev Rept for 970701-980630 for Lgs,Units 1 & 2. with ML20249B3501998-06-11011 June 1998 Rev 1 to PECO-COLR-L2R4, COLR for LGS Unit 2 Reload 4,Cycle 5 ML20249A5331998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Limerick Units 1 & 2 ML20247M7071998-05-14014 May 1998 Safety Evaluation Supporting Amend 128 to License NPF-39 ML20217Q5101998-05-0404 May 1998 Safety Evaluation Supporting Amend 127 to License NPF-39 ML20247H5071998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Limerick Generating Station ML20216F3601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Limerick Generating Station,Units 1 & 2 ML20217M0791998-03-31031 March 1998 Safety Evaluation Supporting Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216F9471998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Limerick Generating Station,Units 1 & 2 ML20216F3471998-02-28028 February 1998 Revised Monthly Operating Rept for Feb 1998 for Limerick Genrating Station,Unit 1 1999-09-30
[Table view] |
Text
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PHILADELPHIA ELECTRIC COMPA'NY i
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LIMERICK GENA"R ATING ST ATION -
SAN ATOG A. PENNSYLV ANI A 19464 tais) 3:7-iroo =n. 2000 February-26, 1990 i a. u.conuicx. a... e,s. Docket Nos. 50-352 u....7".',."'.",C".6,,.., 50-353 License Nos. NPF-39 4 NPF-85
- U.S. Nuclear Regulatory Commission
- Attnt Document Control Desk
'Wanhington, DC- 20555 m
SUBJECT:
Licensee Svent Report i
ilmerici~denerating Station - Units 1 and 2
= ,
c
-This=LER reporte aspects of the Main Control Room (MCR)
- Ventilation,.and Air Conditioning system which are outside of the
- design basia of the plant as described in the Limerick Generating Station Final' Safety Analysis Report. This condition resulted from a failure-to consider the MCR ventilation isolation to isolation modes of operation.
Reference:
Docket Nos. 50-352 50-353
-Report Number: 1-90-002 Revision Number: 00 h Event Date: January 25, 1990 Report Date: February ~ 26,-1990
~ Limerick Generating Station
-Facility:
P.O. Box-A, Sanatoga, PA 19464 F ,
This LER is being submitted pursuant to the requirenents of lik 10-CFR-50.73(a)(2)(ii)(B).
- Very truly yours,
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T. J. Kenny, USNRC Senior Resident Inspector, LGS F
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o l5 l o lo l o l 31512 1 loFl 0lg W . The Main Control Room Ventilation System is outside of the design basis due to misapplication of the design basis assumptionu.
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9lg 9 l3 9 l9 On January 25, 1990, a condition outside the design basis was ,
identified in that, if the Main Control Room (MCR) ventilation system is in the radiation isolation mode-and an automatic chlorine isolation is required, a single failure could prevent the full chlorine mode isolation. Also, the Final Safety Analysis Report does not state any exception 3 to the automatic entry of the MCR ventilation system into the radiation isolation mode. When the MCR ventilation system is in the chlorine isolation mode and a high-radiation signal is received,.the MCR ventilation system will not enter the radiation isolation mode.
An analysis shows that there is adequate protection in any MCR ventilation operating mode to prevent a habitability concern.
The: finding that the chlorine isolation mode of the MCR ventilation does not meet the single failure criterion when the
, MCR ventilation is in the radiation isolation mode is due to the failure'to consider that the radiation isolation mode may be entered under non-accident conditions. The failure to provide automatic entry into the radiation isolation mode from a chlorine isolation mode is due to the failure to consider the transition of the system from one mode of isolation to another mode. When the design ba.ses are clarified with the NRC, the appropriate corrective actions will be taken.
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0 10 012 0F 019 rent er . , e, w.mn Uni't Conditions Prior to the Event:
Unit 1 Unit 2 i,
Operating Condition: 1 (Power Operation) 1 Power Level: 100% 100%
BACKGROUND
- The Limerick < Generating-Station (LGS), Units 1 and 2, Main Control Room (MCR) Heating, Ventilation, and Air Conditioning '
(HVAC) system (EIIS:VI) has several modes of operation (see Figure 1). There is a normal mode where outside air is circulated through the MCR and maintains.it at a slight positive
, pressure. In the normal mode, the normal outside air intake-isolation dampers are open and the Control Room. Emergency-Fresh
~
Air Supply-(CREFAS)' System outside air intake dampers.are closed.
In the event of the presence of radiation in the normal outside
- air intake plenum, the normal MCR HVAC supply and exhaust flow paths are isolated from outside air and the CREFAS System is operated.in the radiation isolation mode'. The radiation isolation mode..is a partial recirculation mode with the normal outside air intake isolation dampers closed and a maximum of 525 scfm of filtered outside . air- that enters the MCR through-the
.CREFAS outside air intake dampers to maintain the positive
. pressure. In the event of the presence of chlorine or other toxic gases in the normal outside ait intake. plenum, the normal MCR HVAC system supply and exhaust flow paths are isolated from outside air and the CREFAS system is operated in the-chlorine isolation mode. The chlorine isolation mode is a full recli O 9 tion mode with no outside air entering the MCR. In this mode, the positive pressure in the MCR decays to atmospheric pressure due to exfiltration. In both isolation modes, the recirculated or outside air flows through charcoal and High Efficiency Particulate Air (HEPA) filters.
The chlorine isolation logic for the normal outside air intake isolation dampers is shown on Figure 2. Two chlorine detectors
'must detect chlorine to actuate the isolation logic resulting in closure of one of the two series tormal outside air intake isolation' valves.
.The major functional difference between the two isolation modes is:the-operation of the CREFFS system filtered outside air intake g ... .
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'UCENSEE EVENT REPORT (LER) TEXT CONTINUATION **aovie ove no sm.om i : ,i in eacettTT haast IH , 00Catt huheet A la' tan musseta tal - ,l P ACE (3s
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0 lo 014 " oI9 rm . . . - .e, - ,nn dampers. .These isolation dampers only open in the radiation isolation mode and are closed in the normal and chlorine isolation modes. Following a modification on this system, the, new chlorine isolation logic for the CREFAS system outside air-intake dampeJs is shown as on Figure 3. Presently, all~four chlorine detectors must detect chlorine to actuate the isolation logic to close the CREFAS outside air intake dampers in both filter train supply lines.
The configuration of the CREFAS system filtered ottside air intake dampers and the associated chlorine logic was originally designed to conform with single failure proor criteria when the system is in the radiation isolation mode.
Description of the Event: ,
On January 25, 1990, it was determined that, if the MCR HVAC system is in the radiation isolation mode and an automatic ,
chlorine mode isolation is required due to the presence of chlorine,.a single failure in the chlorine isolation logic could prevent the CREFAS outside air intake isolation dampers from closing and completing the chlorine mode isolation. The possible single failures that could occur are a chlorine detector probed <~'
failure or a relay failure in the isolation logic. This is contrary to the description in the Final Safety Analysia Report (FSAR) sections-6.4.1.j-and 7.3.2.10, which describe the MCR habitability system and indicate that the chlorine isolation design meets the single failure criteria.
In addition, during the review of the above system, station personnel discovered that the FSAR Section 6.1 did not state any exceptions to the automatic entry into the radiation isolation
-mode on receipt of a high radiation signal. However, by the original ' design, if the CREFAS system is in the chlorine isolation mode and a high radiation signal is received, then the CREFAS system Will not automatically switch to the radiation isolation mode but will remain in the chlorine isolation mode.
The FSAR describ'es the MCR HVAC system operation from the normal mode of operation to an isolation mode (chlorint, or radiation) of operation. The FSAR states that the MCR HVAC system is in conformance with Regulatory Guide (RG) 1.78, " Assumptions for Evaluating the Habitability of Nuclear Power Plant Control Room During a Postulated Hazardous Chemical Release," and RG 1.95,
" Protection of Nuclear Power Plant Control Room Operators Against.
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Lan' Accidental. Chlorine Release." However, th'e FSAR and the RGs' are unclear regarding the necessity of the MCR HVAC system to automatically switch from one mode of isolation-to another -
mode (e.g. chlorine isolation during testing to a radiation isolation). As a result oL the ambiguities in the FSAR and the RGs, the requirement of automatic transition between isolation
- modes was not considered be necessary.
The above conditions are considered to constitute operation outside the design basis of.the plant as currently described in the PSAR and a one hour notification was made to the NRC at 1044 hours on January;25, 1990, in accordance with 10CFR 50.72(b)(1)(ii)(B). Accordingly, this report is oeing submitted in accordance with 10CFR 50.73(a)(2)(li)(B).
Consequences of the Event:
1The consequencet of-these_ conditions are minimal, as shown b'y analysis. Sufficient time exists while in any of the operating modes of the MCR HVAC and CREFAS system (normal, radiation isolation, or chlorine isolation) for the appropriate protective actions to be taken in response.to a high chlorine condition to prevent a habitability concern. Sufficient radiation protection is provided when the CREFAS system is in the chlorine isolation; mode since the MCR ventilation is complet(ly isolated in this mode and the MCR-atmosphere is filtered through the CREFAS system.
charcoal filters. The MCR operators' actions of donning Self-Contained Breathing Apparatus (SCBA) and inserting a manual isolation signal to reinforce the expected automatic actions are covered in plant procedures and licensed operator training. The
_ probability of having to go from one isolation mode to the other isolation mode is' low si'nce operation in any one isolation mode for. prolonged periods of time is low.
'Cause of'the Event:
-The cause of the lack of protection from a single failure in the transfer of the MCR ventilation system from the radiation isolation mode to the chlorine isolation mode is the failure to consider that the radiation isolation mode may be entered under
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. - .nc i-., nn noni accide'nt conditions. In addition, the FSAR and the applicable RGs did not discuss operations between isolation E modes. This failure occurred during the development of a i .
Temporary Circuit Alteration (TCA) and a subsequent permanent modification to the chlorine isolation logic. When the TCA and later the modification were developed the fact that the final design did not sutisfy the single failure criterion while CREFAS system is in the radiation isolation mode was identified.
However, this issue was evaluated from the point of view that entry into the radiation isolation mode was one accident and the chlorine isolation would be a second accident and requiring the single; failure criteria between modes would be beyond the design requirements. However, there is a possibility of the CREFAS
-being in the radiation isolation mode because of maintenance, testing or Technical Specifications (TS) requirements and then having an automatic chlorine isolation sig~nal which would require
.the single failure criterion to be met. The TCA was' installed from 1985 to 1989 and the: modification was installed on September 7, 1989. Therefore the design did not meet the single failure criteria from 1985 until present.
The cause of the failure to provide automatic entry into the radiation isolation mode from a chlorine isolation mode is that only entrance from the normal mode of operation to a single isolation mode of operation was considered when the FSAR was written. . In addition, the applicable RGs did not discuss operation between isolation modes. Isolation to a single isolation mode of operation was not considered and as a result was not described in the FSAR.
No immediate actions were taken as the existing procedures
-provide sufficient guidance to the MCR operators to take protective actions within the time frame specified in the results of the analysis discussed in the Consequences Section.
A conference call was held between PECo personnel and the NRC
~
Technical Reviewers on February 15, 1990. These conditions were discussed and arrangements were made for a subsequent meeting between PECo personnel and the NRC reviewers to further discuss
.this issue and to decide on appropriate steps that should be taken to clarify the design basis. A supplement to this LER will 1
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Actions Taken to. Prevent Recu"rence: ,
'A revision to:the FSAR_will be developed to further explain the design when the ambiguities ~of the design basis'for the various g isolation modes are resolved. The FSAR revision will provide sufficient;information of the system design basis to prevent misinterpretation in'the future.
<l Previous Gimilar/ Occurrences:
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Tracking Codes:
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