|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:RO)
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Lgs,Units 1 & 2. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A8861999-09-13013 September 1999 Safety Evaluation Authorizing First & Second 10 Yr Interval Inservice Insp Plan Requestss for Relief RR-01 ML20212A4481999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Limerick Generating Station,Units 1 & 2.With ML20211E9891999-08-20020 August 1999 LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5 ML20210L7051999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Limerick Generating Station,Units 1 & 2.With ML20209G0211999-06-30030 June 1999 GE-NE-B13-02010-33NP, Evaluation of Limerick Unit 2 Shroud Cracking for at Least One Fuel Cycle of Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 B110078, Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 11998-12-31031 December 1998 Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 1 ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154H5691998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Limerick Generating Station,Units 1 & 2.With ML20151X3511998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Limerick Generating Station Units 1 & 2.With ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20237D1041998-08-17017 August 1998 Books 1 & 2 of LGS Unit 1 Summary Rept for 960301-980521 Periodic ISI Rept 7 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20236X7641998-07-31031 July 1998 Rev 0 to SIR-98-079, Response to NRC RAI Re RPV Structural Integrity at Lgs,Units 1 & 2 ML20237B4711998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Limerick Generating Station,Units 1 & 2 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20151Z4881998-06-30030 June 1998 GE-NE-B1100786-02, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 2 ML20236P9781998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Limerick Generating Station,Units 1 & 2 ML20196K1801998-06-30030 June 1998 Annual 10CFR50.59 & Commitment Rev Rept for 970701-980630 for Lgs,Units 1 & 2. with ML20249B3501998-06-11011 June 1998 Rev 1 to PECO-COLR-L2R4, COLR for LGS Unit 2 Reload 4,Cycle 5 ML20249A5331998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Limerick Units 1 & 2 ML20247M7071998-05-14014 May 1998 Safety Evaluation Supporting Amend 128 to License NPF-39 ML20217Q5101998-05-0404 May 1998 Safety Evaluation Supporting Amend 127 to License NPF-39 ML20247H5071998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Limerick Generating Station ML20216F3601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Limerick Generating Station,Units 1 & 2 ML20217M0791998-03-31031 March 1998 Safety Evaluation Supporting Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216F9471998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Limerick Generating Station,Units 1 & 2 ML20216F3471998-02-28028 February 1998 Revised Monthly Operating Rept for Feb 1998 for Limerick Genrating Station,Unit 1 1999-09-30
[Table view] |
Text
e 10 CPR 50.73 )
1 PHILADELPHIA ELECTRIC COMPANY l LIMERICK GENER ATING ST ATION S AN ATOG A. PENNSYLV ANI A 19464 (Ill) 3271200 mat. 2000 q c2. J. m e c o m u 6 c u. J... p.t. l 6 2 . . . /.' C'. .".'.",".* *. . . .. Noyember 27, 1989 l Docket No. 50-353 :
License No. NPP-85 t U.S. Nuclear Regulatory Commission l Attn Document Control Desk Washington,.DC 20555 .
l
SUBJECT:
Licensee Event Report t Limerick Generating Station - Unit 2 This LER reports an actuation of the Nuclear Steam Supply Shutoff System, an automatic Engineered Safety Feature due to a i personnel error.rosulting from a lack of attention to detail, e
Reference:
Docket No. 50-353
- Report Number 2-89-011 -.
Revision Number: 00 Event Date: October 27, 1989
- Report Date: November 27, 1989 i Facility: Limerick Generating Station P.O. Box A, Sanatoga, PA 19464 ,
This-LER is being submitted pursuant to the requirements of 10 CPR 50.73(a)(2)(iv).
/
y602 %
WGS:ch cca W. T. Russell, Administrator, Region I, USNRC T. J. Kenny, USNRC Senior Resident Inspector, LGS
$5W
\
\ .
f.$[0k$oNbb' S
f
cA muckp2 u;w6 ,37 es iunios. !
i, **c . an.
""- e..::,io e . , !
- u "'m *"3 UCENSEE EVENT REPORT (LER) ,
m.ior, . m ooc n .. m ..c..>
1.imr.ich rencratim erv H m Unit ? o is I o ie i o 13 is i3 1 lod 0 16 ' [
"'* Actuation of the Nuclear rteam Pum1v Photoff Pystem due to a Personnel error ,
moultim fivrn a inck M ettonHnn en antail
.......i.i e u....... . . . . . . . , , , , .......,i......,,,,,,,
.v. o., vu.i vs.a e: " O ,;;'". s c *.?: = cat.l c., ,s.a . .= w,, a -u oonn au-na.
e isic ioici .c i ;
~
Il0 2l7 Rl9 Rl4 0 l 1 l1 nl0 3 l1 ?!7
.......,i.............,,,,...................,._......-,,o 9l9 015ioic3 0, i i .
aat* 1 n u.i n ai.i y w.nanin . nin.
n v.imui pai.nu w.ni.nin.i n.ru.i g.g, g;..g;
,,,, Oini7 n ounui., ...i. ..n mii.n..,
"~""""' _
""""'""" ~
n ==nuw anannua unananano nCh ~5% : ?; W[b.. g f s n ai.nu...
Fb c{ . W q an.. an.m uni.nin.i tetth418 tch,.C7... taisLt.titi
,,1 ,.
,ea. e e aw ...
.... u u C. R. Endriss, Regulatory Enginocr, Linerick Generating Station 21,5i 3, 2 ,7 , ,1,2 ,0 i n CDw.4 8,8 Omt Liset 9 0 4.CM CC*.0hthY 8 8tV.4 ctw.ists in tuts t.c.,113i con mn. co -e e=t ";;;;;*-
- l'o*:.'.'n ' hyyh c vu st a = co-.o i t "t':ll* ";;c:@t' Qg%
m ; m .n ~ , .nc , ,
g l l l l l ) S N$!Nb ; ; 9 g l g g ($khkhh W:$w$
m.m i i i ,
&ra?b,&a$
( 1 i i i i i i iv o .. ,.6 . . .e., n.i eti e n.. c ., i .., i ..
. enterte svowwo. carto no ; l l G vss reo .
......-..a_....__._.-....._.__.._....
On October 27, 1989, at 0611 hours0.00707 days <br />0.17 hours <br />0.00101 weeks <br />2.324855e-4 months <br />, the Unit 2 Nuclear Steam Supply Shutoff System (NSSSS) outboard containment isolation valve logic was de-energized. This resulted in an isolation of the outboard NSSSS isolation valves which is an actuation of an l Engineered Safety Feature. The de-energization occurred during l the performance of a surveillance test when Instrument and Control (I&C) personnel inadvertantly grounded and blew the
- outboard valve logic power supply fuse in an Auxiliary Equipment
- l. Room (AER) panel. A test lead became disconnected from a voltmeter and created a short to ground. The power supply fuse was replaced and the valve isolations were reset by 0735 hours0.00851 days <br />0.204 hours <br />0.00122 weeks <br />2.796675e-4 months <br />.
All isolations and systems actuated as designed. The consequences of this event were minimized due to prompt operator actions. The cause of this event is personnel error due to a lack of attention to detail by two I&C technicians performing the test. The I&C personnel involved with this event were counseled to stress the importance of a higher level of attention to detail while performing work tasks. This event has been discussed at an I&C all-hands meeting and a test lead retaining device is
- currently undergoing trial use. A task force has been developed to thoroughly investigate, identify, and address the root causes of this and similar events, gc,,... u.
r , 1
.Y
}
Wat he anA y g CUC48AS LE%UbaTOMV COMultBION
"" ***aovie o=* =o am-o*
UCENSEE EVENT REPORT (LER) TEXT CONTINUATION
. .. .. . i v ..
paceptr es.mt of pocal1 muuttei tp gen numegn ter Paol (3'
,,,, . . . . . . , . . .o-Limerick ceneratines station, Unit 2 " * * "
o l5 lo 1010 l 315l3 8l 9 -
0 l1l 1 -
010 0l 2 or 0 l6 m, w m . ~ - ~.c o nu u nn i Unit'2 Conditions Prior to the Event:
I Operating Condition: 1 (Power Oparation) !
Power Levelt 67% ;
\
i
. Description of the Event:
OniOctober 27, 1989, at 0611' hours, the Unit 2 Nuclear Steam '
Supply Shutoff System-(NSSSS) (EIIS:JM) outboard valve isolation logic was de-energized. This NSSSS isolation logic de-energization occurred during the performance of Surveillance :
. Test ST-2-042-659-2, "NSSSS - Reactor Vessel Water Level - Levels l'and~2;' Division II A, Channel C Functional Test," when ,
L Instrument and Control (I&C) personnel inadvertantly grounded and i l blew the outboard valve logic power supply fuse (EIIS FU),
'B21-F15D,.in the Auxiliary Equipment Room (AER) panel (EIIStPL) 20C623. This caused de-energitation'of the NSSSS logic and e resulted in an isolation (i.e. valve initially open then closed) '
of the outboard valves, an Engineered Safety Feature (ESP), in the following NSSSS Groups:
l i
o' Residual Heat Removal (RHR) Heat Exchanger (HTX) Vacuum '
Breaker Lines (EIIS BO) .
o Reactor Water Cleanup (EIISICE) o Primary Containment Exhaust to Reactor Enclosure Equipment
. Compartment Exhaust and Nitrogen Block Valves '
\
l o' Primary Containment Instrument Gas Process Lines (PCIG) ;
(EIIS:LK) o Drywell Chilled Water (DWCW) (EIIS KM) and Reactor Enclosure Cooling Water (RECW) (EIIS:CC) to the Recirculation Pumps o Drywell Sump, Suppression Pool Cleanup (EIIS:CG) and PCIG Traversing Incore Probe Supply (TIPS) (EIIS:IG) Purge Supply. ,
, t I
l-
.geo u m.
..s_-.___.- -- __._= _ _------- - - - - - - - -'- - --- - - -
i e..m v s acuestaa aioutma, co . o= i UCENSEE EVENT REPORT (LER) TEXT CONTINUATION *~aevio ous ao sm-eios i I R*iDIS l'U S$
sacepit hewn m pOGhithuuth W gge wguelR 46 Pa08 438
,... ..w. n.. ai v . .o-Limerick Generatina Station, Unit 2 " "
- l 01510 l o l o 13 l 513 8l 9 -
0 l1l1 -
0l0 0l3 or 0l6 The following NSSSS outboard groups received an isolation signal, however no valve movement occurred since the associated valves were already closed due to plant conditions prior to the event.
o Main Steam and Reactor Sampling i
o RHR Shutdown Cooling .
o RHR HTX sample line and drains to Radwaste o Primary Containment Purge Supply and Exhaust (EIIStVA)
At 0611 hours0.00707 days <br />0.17 hours <br />0.00101 weeks <br />2.324855e-4 months <br />, Licensed Main Control-Room (MCR) operators received isolation indication in the MCR for isolations of the above listed NSSSS groups and immediately took actions to restore DWCW, RECW, and PCIG.
MCR operators restored DWCW and RECW at 0613 hours0.00709 days <br />0.17 hours <br />0.00101 weeks <br />2.332465e-4 months <br /> and PCIG at 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br /> using NSSSS isolation bypass switches in accordance ,
with the Event procedure E-2BY160, " Loss of 2B RPS and UPS Power," Off Normal procedure ON-113, " Loss of RECW," and General !
Plant Procedure GP-8, " Primary and Secondary Containment Isolation Verification and Reset." MCR operators recognized the cause of the isolations to be a blown fuse and instructed the I&C personnel, performing the NSSSS surveillance test in the AER, to ,
stop testing. The blown fuse was then replaced by the IGC
- i. technicians. MCR operators then reset and restored the remaining l isolations by 0735 hours0.00851 days <br />0.204 hours <br />0.00122 weeks <br />2.796675e-4 months <br /> using GP-8. All NSSSS isolations l previously mentioned above were reset, restored and placed into ,
~
l service within-one hour and twenty four minutes.
A four hour notification was made to the NRC on October 27, 1989, L at 0919 hours0.0106 days <br />0.255 hours <br />0.00152 weeks <br />3.496795e-4 months <br /> in accordance with the requirements of 10 CPR 50.72 l (b)(2)(ii), since this event resulted in the spurious automatic actuation of an ESF. Accordingly, this report is being submitted in accordance with the requirements of 10 CFR 50.73 (a)(2)(iv).
l Consequences of the Event:
The consequences of this event were minimal. There was no release of' radioactive material to the environment as a result of this event. These NSSSS isolation valves functioned as designed under the loss of logic power condition created by the failed power supply fuse. The isolations were bypassed or reset and the g.;p.. ..
L '
=ac .a o s eve 6taa struaionv commissioi UCENSEE EVENT REPORT (LERI TEXT CONTINUATION
- m. ao sm-o*
".. cget. autsu vocasT muut. A 538 tgesvuuttaten .aSt (31
,,a, . . . ~ , , ....+-
1.imerick nenerating Station, Unit 2 ' " " * " " ' "
o Is lo lo lo 1315l3 81 9 --
0 l111 --
0l0 01 4 or nl6 TEXT t# pure amosv a 8peam9W. ens. eWWeems' MC for8m W .* 1171 systems were restored quickly enough by operators in accordance with plant procedures to prevent any adverse impact on plant systems.
Immediate and follow up actions to this type of event (i.e., Loss of Logic Power) are provided in procedures E-2BY160, ON-113, and GP-8. Licensed operators receive requalification training to review and perform operator responses to transients of this type.
This training provides practice on immediate operator actions and minimizes the length of time certain systems are isolated reducing the impact on the plant. Therefore, as a result of adequate procedural guidance, training, and prompt operator actions, the event duration was limited and no adverse plant i conditions developed.
Additionally, if the fault introduced during the performance of the surveillance test had resulted in this logic system being inoperable, the redundant NSSSS isolation logic channel would have been available in the event that an isolation of the NSSSS system were required.
Cause nf the Event:
The cause of this event is personnel error due to a lack of attention to detail by two I&C technicians performing ST-2-042-659-2. While in the AER panel, these technicians did L not ensure the test leads were adequately connected into the l digital voltmeter at the time measurements were to be taken. As l a result of this lack of attention to detail, one of the test leads connected to the voltmeter became disconnected, dropped downwards within the AER panel and created a short to ground.
This short to ground caused the logic power supply fuse, B21-F15D, to blow initiating the NSSSS outboard containment valve ,
isolations.
The test leads used during the testing was a contributing cause to this event. The test leads did not have insulated connectors nor a retaining device at the point of connection t.o the voltmeter. As a result, one of the I&C technicians was able to dislodge the test lead and this uninsulated lead was able to contact a grounded point in the panel.
- g. o. ...
we . a . v. evetia ciav6avo , co .o=
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION anaovio ous =o si6e-o*
i .... . mi
..can. ... m gonn=g..m s i . .,g . . .., ,ai ai Linerick Generatina station, Unit 2 '""* * "
- o 151010 l0 l 31513 8l 0 -
0l1l1 -
0l0 01 5 0F O lf tert . , . < - =c , asu .,ini Corrective Actions:
On October 27, 1989, at 0611 hours0.00707 days <br />0.17 hours <br />0.00101 weeks <br />2.324855e-4 months <br />, MCR licensed operators evaluated the annunciators which alarmed due to the spurious NSSSS valve isolations and determintd that the NSSSS valve isolations were not due to actual reactor or primary containment transients warranting isolation of these systems. In accordance with procedures E-2BY160, ON-113, and GP-8, DWCW.and RECW isolations were bypassed at 0613 hours0.00709 days <br />0.17 hours <br />0.00101 weeks <br />2.332465e-4 months <br /> and the PCIG isolations were bypassed at 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br />. MCR operators recognized the cause of the isolations to be a blown fuse and the I&C technicians were immediately instructed to halt further performance of ST-2-042-659-2 and replace the logic power supply fuse. MCR operators reset and restored the remaining isolations by 0735 hours0.00851 days <br />0.204 hours <br />0.00122 weeks <br />2.796675e-4 months <br /> per GP-8 returning the plant to pre-transient conditions.
Actions Taken to Prevent Recurrence:
The I&C personnel involved with this event were counseled to stress the importance of a higher level of attention to detail while performing work tasks. The event has been discussed at an I&C-All Hands Meeting with emphasis placed on the need for attention to detail. Additionally, this discussion conveyed the continuous need to use proper techniques during troubleshooting tasks and the importance of using precautions to prevent exposed metal surfaces on test leads and tools from shorting to ground.
A lead retaining device that can be attached to digital voltmeters.to prevent stressing of lead connections was developed and is currently undergoing trial use. A task force has been developed to review this and similar events within the AER. This task force will thoroughly investigate, identify, and address the root causes of these events and evaluate previous corrective actions to determine whether the actions were effective or not.
This review and evaluation is expected to be completed by December 31, 1989.
- g. o. n...
. . . . i
~erac eegh anta V 5 000CLEL3 EtIv62Toay CommittiOh I tlCENSEE EVENT REPORT (LER) TEXT CONTINUATION **=ovie oue ao w-m c.. is ami i f aciutt haut si, pocaat muussa u' tan h6mneta sep Pael la' Limerick reneratinn Station, Unit 2
"'" "D'E*" - D'N '
0 1510101013 ] 5l 3 8l 9 -
0 ]1l 1 -
0]O 0]6 or 0 l r, l raxw- .-,. ..e, n,ni, Previous Similar Occurrences: .
+
LERs 1-84-021, 1-84-030, 1-85-011, 1-85-012, 1-85-049, 1-85-074 l 1-86-045, 1-87-021 1-87-038 and 1-89-006 also reported NSSSS '
isolation due to a blown fuse as a result of personnel error.
._ The review and evaluation will determine whether the corrective !
actions in these previous events were effective or not in preventing future recurrences of those types of events.
Tracking Codes: (A) Personnel Error E
P 3
t t
1 4
g,,. .. . m.
.