ML17207A808: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:REGULATORY
{{#Wiki_filter:REGULATORY
'ORMATION DISTRIBUTION SYS(RIDS)ACCESSION NBR;8002110517 DOC~DATE:80/01/25NOTARIZED; NOFACIL:50-335 St.LuciePlantiUnitiiFloridaPower8LightCo.50-389St~LuciePlantiUnit2iFloridaPowerLLightCo.AUTH~NAMEAUTHORAFFILIATION HETHYzC~MDFloridaPower3LightCo,RECIP,NAME RECIPIENT AFFILIATION DOCKET¹0500033505000389
'ORMATION DISTRIBUTION SYS (RIDS)ACCESSION NBR;8002110517 DOC~DATE: 80/01/25 NOTARIZED; NO FACIL:50-335 St.Lucie Planti Unit ii Florida Power 8 Light Co.50-389 St~Lucie Planti Unit 2i Florida Power L Light Co.AUTH~NAME AUTHOR AFFILIATION HETHYzC~MD Florida Power 3 Light Co, RECIP,NAME RECIPIENT AFFILIATION DOCKET¹05000335 05000389


==SUBJECT:==
==SUBJECT:==
RO33580Agon800124:feederbreaker(2845)fromBstartuptransformer toB4160Vvitalbuswasopen,Causedbyimproperly labeledbresker,Breaker cubiclesA8BhavebeenlockedIIaresurvei11eddai1y~DISTRIBUTION CODE>>M007SCOPIKSRECEIVED:LTR LENCL+SIZE>>TITLE:LER(Backfit)FC~NOTES.AINTERNAL:
RO 335 80 Agon 800124: feeder breaker (284 5)f r om B star tup transformer to B 4160V vital bus was open, Caused by improperly labeled br esker,Breaker cubicles A 8 B have been locked II are survei 1 1 ed dai 1 y~DISTRIBUTION CODE>>M007S COPIKS RECEIVED:LTR L ENCL+SIZE>>TITLE: LER (Backf i t)FC~NOTES.A INTERNAL: RECIPIENT ID CODE/NAME EG FILE 04'PA R IRELAND COPIES LTTR ENCL RECIPIENT ID CODE/NAME 02 NRC PDR AEOD NSIC S HANAUER COPIES LTTR ENCL EXTERNAL: 03 LPDR~~~~'88O O TOTAL NUMBER OF COPIES REQUIRED: LTTR 10 ENCL tq
RECIPIENT IDCODE/NAME EGFILE04'PARIRELANDCOPIESLTTRENCLRECIPIENT IDCODE/NAME 02NRCPDRAEODNSICSHANAUERCOPIESLTTRENCLEXTERNAL:
+4 If'I*Il If r4'h POST OFF IC X 128, FT.PIERCE, FLORIDA 33450 CMW-PSL Ltr Bk f/837 Copies to: CtR, JHB, CAW, GMV, RRJ Offsite: ADS, JRB, COW, MAS, REU, KNH I To: Mr.J.P.O'Reilly, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission Atlanta, Georgia 30303 From: Mr.C.M.Wethy, Plant Manager St Lucie Plant-DPR 67 Florida Power 6 Light Company Miami, Florida: c FLORIDA POWER BIGHT COPIIPANY I7 January 25@.980~i 0~~''~
03LPDR~~~~'88OOTOTALNUMBEROFCOPIESREQUIRED:
LTTR10ENCLtq
+4If'I*IlIfr4'h POSTOFFICX128,FT.PIERCE,FLORIDA33450CMW-PSLLtrBkf/837Copiesto:CtR,JHB,CAW,GMV,RRJOffsite:ADS,JRB,COW,MAS,REU,KNHITo:Mr.J.P.O'Reilly,
: Director, RegionIIOfficeofInspection andEnforcement U.S.NuclearRegulatory Commission Atlanta,Georgia30303From:Mr.C.M.Wethy,PlantManagerStLuciePlant-DPR67FloridaPower6LightCompanyMiami,Florida:cFLORIDAPOWERBIGHTCOPIIPANY I7January25@.980~i0~~''~


==Subject:==
==Subject:==
hiEMOFORFACSIMILE TRANSMISSION TOCONFIRMPROMPTREPORTABLE OCCURRENCE 335-80-4IMPROPERELECTRICAL LINEUPThismemoistoconfirmthetelephone notification madetoMr.Martinofyourofficeon1/24/80.Atabout3:00PMon1/24/80itwasnotedthatafeederbreaker(2B4-5)fromtheBStartuptransformer totheB4160Vvitalbuswasopen.Thiscondition hadexistedsince5:00PMon1/18/80andwasnotincompliance withT.S.3.8.1.1.Actiona.regarding offsiteA.C.powersupplieswhichrequiretestingofthe"B"DieselGenerator (D/G)every8hourswhenthe"B"Startuptransformer isoutofserviceandlimitstheoutofserviceperiodto72hours.Additionally for5-1/2hourson1/24/80theAD/Gwastakenoutofserviceforperiodicmaintenance.
hiEMO FOR FACSIMILE TRANSMISSION TO CONFIRM PROMPT REPORTABLE OCCURRENCE 335-80-4 IMPROPER ELECTRICAL LINEUP This memo is to confirm the telephone notification made to Mr.Martin of your office on 1/24/80.At about 3:00 PM on 1/24/80 it was noted that a feeder breaker (2B4-5)from the B Startup transformer to the B 4160V vital bus was open.This condition had existed since 5:00 PM on 1/18/80 and was not in compliance with T.S.3.8.1.1.Action a.regarding offsite A.C.power supplies which require testing of the"B" Diesel Generator (D/G)every 8 hours when the"B" Startup transformer is out of service and limits the out of service period to 72 hours.Additionally for 5-1/2 hours on 1/24/80 the A D/G was taken out of service for periodic maintenance.
Thesur-veillance requirements andtimelimitsofT.S.3.8.1.1.Actionb.weremet.AlsotheBD/Gwastestedsatisfactorily on1/18/80andagainon1/24/80soitwasoperableduringtheperiodinquestionaswasthe"A"Startuptransformer, and(exceptfortheperiodon1/24/80)"A"D/G.Thebreakerwasclosedby3:15PMon1/24/80.Theapparentcauseisanimproperly labeledbreaker.Forinterimprotection untilthismatterhasbeenthoroughly investigated, theAandBbreakercubicleshavebeenlockedandarebeingsurveilled daily.(Thebreakerswerecheckedevery2hoursuntilthisactionwascompleted.)
The sur-veillance requirements and time limits of T.S.3.8.1.1.Action b.were met.Also the B D/G was tested satisfactorily on 1/18/80 and again on 1/24/80 so it was operable during the period in question as was the"A" Startup transformer, and (except for the period on 1/24/80)"A" D/G.The breaker was closed by 3:15 PM on 1/24/80.The apparent cause is an improperly labeled breaker.For interim protection until this matter has been thoroughly investigated, the A and B breaker cubicles have been locked and are being surveilled daily.(The breakers were checked every 2 hours until this action was completed.)
Also,noswitching ordersonthissystemwillbeperformed untilwearesuretheproblemhasbeenthoroughly investigated andisfullyunderstood.
Also, no switching orders on this system will be performed until we are sure the problem has been thoroughly investigated and is fully understood.
Investigation andeval-uationwillbecontinued andfinalresultsincluding furthercorrective actionwillbereported.
Investigation and eval-uation will be continued and final results including further corrective action will be reported.ethy Pl nt Manager St.Lucie Plant CMW:RRJ:bmh 699@TI~ZQ PEOPLE....
ethyPlntManagerSt.LuciePlantCMW:RRJ:bmh 699@TI~ZQPEOPLE....
SERVING PEOPLE C' 4t 4}}
SERVINGPEOPLEC' 4t4}}

Revision as of 19:34, 7 July 2018

RO 335-80-4:on 800124,feeder Breaker from Startup Transformer B to 4160-volt Vital Bus B Was Open.Caused by Improperly Labeled Breaker.Breaker Cubicles a & B Were Locked & Are Checked Daily
ML17207A808
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 01/25/1980
From: WETHY C M
FLORIDA POWER & LIGHT CO.
To:
References
NUDOCS 8002110517
Download: ML17207A808 (4)


Text

REGULATORY

'ORMATION DISTRIBUTION SYS (RIDS)ACCESSION NBR;8002110517 DOC~DATE: 80/01/25 NOTARIZED; NO FACIL:50-335 St.Lucie Planti Unit ii Florida Power 8 Light Co.50-389 St~Lucie Planti Unit 2i Florida Power L Light Co.AUTH~NAME AUTHOR AFFILIATION HETHYzC~MD Florida Power 3 Light Co, RECIP,NAME RECIPIENT AFFILIATION DOCKET¹05000335 05000389

SUBJECT:

RO 335 80 Agon 800124: feeder breaker (284 5)f r om B star tup transformer to B 4160V vital bus was open, Caused by improperly labeled br esker,Breaker cubicles A 8 B have been locked II are survei 1 1 ed dai 1 y~DISTRIBUTION CODE>>M007S COPIKS RECEIVED:LTR L ENCL+SIZE>>TITLE: LER (Backf i t)FC~NOTES.A INTERNAL: RECIPIENT ID CODE/NAME EG FILE 04'PA R IRELAND COPIES LTTR ENCL RECIPIENT ID CODE/NAME 02 NRC PDR AEOD NSIC S HANAUER COPIES LTTR ENCL EXTERNAL: 03 LPDR~~~~'88O O TOTAL NUMBER OF COPIES REQUIRED: LTTR 10 ENCL tq

+4 If'I*Il If r4'h POST OFF IC X 128, FT.PIERCE, FLORIDA 33450 CMW-PSL Ltr Bk f/837 Copies to: CtR, JHB, CAW, GMV, RRJ Offsite: ADS, JRB, COW, MAS, REU, KNH I To: Mr.J.P.O'Reilly, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission Atlanta, Georgia 30303 From: Mr.C.M.Wethy, Plant Manager St Lucie Plant-DPR 67 Florida Power 6 Light Company Miami, Florida: c FLORIDA POWER BIGHT COPIIPANY I7 January 25@.980~i 0~~~

Subject:

hiEMO FOR FACSIMILE TRANSMISSION TO CONFIRM PROMPT REPORTABLE OCCURRENCE 335-80-4 IMPROPER ELECTRICAL LINEUP This memo is to confirm the telephone notification made to Mr.Martin of your office on 1/24/80.At about 3:00 PM on 1/24/80 it was noted that a feeder breaker (2B4-5)from the B Startup transformer to the B 4160V vital bus was open.This condition had existed since 5:00 PM on 1/18/80 and was not in compliance with T.S.3.8.1.1.Action a.regarding offsite A.C.power supplies which require testing of the"B" Diesel Generator (D/G)every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> when the"B" Startup transformer is out of service and limits the out of service period to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.Additionally for 5-1/2 hours on 1/24/80 the A D/G was taken out of service for periodic maintenance.

The sur-veillance requirements and time limits of T.S.3.8.1.1.Action b.were met.Also the B D/G was tested satisfactorily on 1/18/80 and again on 1/24/80 so it was operable during the period in question as was the"A" Startup transformer, and (except for the period on 1/24/80)"A" D/G.The breaker was closed by 3:15 PM on 1/24/80.The apparent cause is an improperly labeled breaker.For interim protection until this matter has been thoroughly investigated, the A and B breaker cubicles have been locked and are being surveilled daily.(The breakers were checked every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> until this action was completed.)

Also, no switching orders on this system will be performed until we are sure the problem has been thoroughly investigated and is fully understood.

Investigation and eval-uation will be continued and final results including further corrective action will be reported.ethy Pl nt Manager St.Lucie Plant CMW:RRJ:bmh 699@TI~ZQ PEOPLE....

SERVING PEOPLE C' 4t 4